Event Notification Report for July 23, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 07/22/1999 - 07/23/1999 ** EVENT NUMBERS ** 35944 35945 35946 35947 +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 35944 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: IDAHO NAT ENGR & ENVIRONMENTAL LAB |NOTIFICATION DATE: 07/21/1999| |LICENSEE: IDAHO NAT ENGR & ENVIRONMENTAL LAB |NOTIFICATION TIME: 22:17[EDT]| | CITY: Idaho Falls REGION: 4 |EVENT DATE: 07/21/1999| | COUNTY: STATE: ID |EVENT TIME: 19:55[MDT]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 07/22/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ELMO COLLINS R4 | | |LARRY CAMPER NMSS | +------------------------------------------------+FRANK CONGEL IRO | | NRC NOTIFIED BY: JOE GARCIA |CHARLIE BAGWELL FEMA | | HQ OPS OFFICER: DOUG WEAVER |BILL BEECHER PAO | +------------------------------------------------+DOE (fax) | |EMERGENCY CLASS: | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DOE ALERT DECLARED DUE TO A BRUSH FIRE ON SITE PROPERTY | | | | The licensee declared a DOE ALERT due to a brush fire that has burned onto | | the Idaho National Engineering and Environmental Laboratory (INEEL) site | | property. No radioactive material is currently threatened by the fire. The | | use of some communications towers has been interrupted because the fire | | burned a telephone pole connecting the towers to the facility. | | | | The licensee notified the state of Idaho and local county officials, DOE and | | the Fort Hall Indian Reservation. | | | | * * * UPDATE AT 0047 ON 07/22/99 FROM ED BROWN TO JOLLIFFE * * * | | | | The brush fire has burned to within 11 miles of the nearest site building. | | The wind is presently blowing from 320� (Southeast, away from site | | buildings) at 4 MPH. The outside temperature is 65�F. The fire is being | | fought by the Bureau of Land Management. There is no threat to site | | facilities. | | | | * * * UPDATE AT 0137 ON 07/22/99 FROM ED BROWN TO JOLLIFFE * * * | | | | The wind is now blowing from 224� (Northeast, away from site buildings). | | | | * * * UPDATE AT 0211 ON 07/22/99 FROM ED BROWN TO JOLLIFFE * * * | | | | At 2347 MDT on 07/21/99, the licensee terminated the DOE ALERT. The fire is | | now under control and there is now no ongoing fire on INEEL site property. | | | | The licensee notified the state of Idaho and local county officials, DOE and | | the Fort Hall Indian Reservation of the termination of the DOE ALERT. | | | | The NRC Operations Officer notified R4DO Collins, NMSS EO Camper, IRO | | Congel, FEMA Bagwell, PAO Beecher, DOE (fax), USDA (fax), HHS (fax) and EPA | | (NRC) (fax) of the termination of the DOE ALERT. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35945 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TX DEPT OF HEALTH BUR OF RAD CONTRL |NOTIFICATION DATE: 07/22/1999| |LICENSEE: GENERAL INSPECTION SERVICES, INC |NOTIFICATION TIME: 14:20[EDT]| | CITY: AUSTIN REGION: 4 |EVENT DATE: 07/22/1999| | COUNTY: STATE: TX |EVENT TIME: 10:00[CDT]| |LICENSE#: 02319 AGREEMENT: Y |LAST UPDATE DATE: 07/22/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ELMO COLLINS R4 | | |LARRY CAMPER NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JIM OGDEN (FAX) | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | |BAE1 20.2202(b)(1) PERS OVEREXPOSURE | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | RADIATION EXPOSURE TO AN INDUSTRIAL RADIOGRAPHER | | | | A WHOLE BODY DOSE OF 6.965 REM WAS RECEIVED BY A GENERAL INSPECTION | | SERVICES, INC INDUSTRIAL RADIOGRAPHER ACCORDING TO HIS APRIL BADGE READING. | | HE HAS BEEN REMOVED FROM WORK EXPOSING HIM TO IONIZING RADIATION UNTIL | | 01/01/00. THIS IS TX INCIDENT #7481. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35946 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 07/22/1999| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 15:24[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 07/22/1999| +------------------------------------------------+EVENT TIME: 14:30[EDT]| | NRC NOTIFIED BY: CHARLES KOCSIS |LAST UPDATE DATE: 07/22/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES NOGGLE R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OUTSIDE DESIGN BASIS ISSUE | | | | In a conversation with Westinghouse on 07/22/99, the Licensee was advised of | | the preliminary results of a reanalysis of main steam line break (MSLB) at | | 70% and 102% power to address a non-conservative assumption made with regard | | to feedwater addition. The original assumption was 800 cubic feet of | | unisolable volume which has been determined to be 3,783 cubic feet. This | | represents the volume from the main boiler feed pump discharge isolation | | valves to the steam generator (the feedwater isolation valve on the faulted | | generator is assumed to fail). Westinghouse advised that the preliminary | | calculation showed that the containment design pressure would be exceeded | | unless there were changes to the design input assumptions that are part of | | the Indian Point Unit 3 licensing basis. Based upon this, the Licensee | | considers Unit 3 to be outside the design basis. | | | | The Licensee evaluated plant operability based upon the telecon with | | Westinghouse. Westinghouse advised that the MSLB peak pressure would not | | exceed the current calculated pressure of 42.4 psig for the MSLB assuming a | | 2.6% shutdown margin with credit for 2300 ppm boron in the emergency core | | cooling injection line. This analysis changes assumptions in UFSAR Section | | 14.2.5 of 1.3% shutdown margin (this is the required margin per Technical | | Specification 3.10.1.1) and unborated water in ECCS lines from the refueling | | water storage tank. Unit 3 currently meets the changed assumptions. The | | Licensee considers Unit 3 to be operable based on the Westinghouse | | preliminary calculation and additional conservatism in this calculation | | (e.g. feedwater addition for 120 seconds when the valve shuts in about 70 | | seconds, no credit for restriction of feedwater as the valve shuts). | | | | Administrative controls will have to be put into place to maintain the plant | | shutdown margin and the boron concentration. The Westinghouse reanalysis | | was initiated by the Licensee following industry information (Ginna, in LER | | 50/244/99-01, identified the non-conservative assumption of 800 cubic feet | | in WCAP-8822). | | | | The Licensee plans to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35947 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: TURKEY POINT REGION: 2 |NOTIFICATION DATE: 07/22/1999| | UNIT: [3] [] [] STATE: FL |NOTIFICATION TIME: 15:05[EDT]| | RXTYPE: [3] W-3-LP,[4] W-3-LP |EVENT DATE: 07/22/1999| +------------------------------------------------+EVENT TIME: 09:25[EDT]| | NRC NOTIFIED BY: B. STAMP |LAST UPDATE DATE: 07/22/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |EDWARD MCALPINE R2 | |10 CFR SECTION: |TAD MARSH NRR | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNSATISFACTORY RESULTS FROM A DRUG TESTING LABORATORY | | | | ON 07/21/99, THE LICENSEE SUBMITTED A BLIND SPECIMEN WHICH HAD BEEN SPIKED | | WITH 1839 NG/ML OF AMPHETAMINE AND 1860 NG/ML OF METHAMPHETAMINE TO A DRUG | | TESTING LABORATORY IN LEESBURG, FL TO BE ANALYZED. THE RESULTS WERE | | RECEIVED BY THE LICENSEE AT 0925 ON 07/22/99 AND THEY WERE REPORTED AS | | NEGATIVE. THE LICENSEE IS CONDUCTING AN INVESTIGATION. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021