Event Notification Report for June 2, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/28/1999 - 06/02/1999 ** EVENT NUMBERS ** 35666 35772 35774 35775 35776 35777 35778 35779 35780 35781 35782 35783 35784 35785 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35666 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SALEM REGION: 1 |NOTIFICATION DATE: 05/03/1999| | UNIT: [] [2] [] STATE: NJ |NOTIFICATION TIME: 13:12[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/03/1999| +------------------------------------------------+EVENT TIME: 10:00[EDT]| | NRC NOTIFIED BY: JOSEPH SULLIVAN |LAST UPDATE DATE: 06/01/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES LINVILLE R1 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ONE HIGH HEAD SAFETY INJECTION LINE DETERMINED NOT TO HAVE FLOW DURING | | TESTING | | | | "During performance of the 18 month high head charging valve throttle test, | | it was discovered that the #21 high head cold leg injection line did not | | pass flow until the other three lines for high head cold leg injection were | | closed. At that point, an audible indication was heard and flow was | | observed through the #21 cold leg. All cold leg injection flows were | | subsequently balanced. The cause of this is under investigation and will be | | resolved prior to Mode 4." | | | | The licensee notified the NRC Resident Inspector and will be notifying the | | local government agencies. | | | | * * * UPDATE AT 1212 ON 6/1/99 BY SIMPSON TAKEN BY WEAVER * * * | | | | On 5/3/99, Salem Unit 2 reported an event concerning a safety injection | | system cold leg injection line which appeared to not pass flow during the | | performance in an 18 month surveillance test for flow balancing. The | | discrepancy appeared to be due to a stuck check valve. At the time of the | | event it was not known how long the condition had existed thus a 50.72 call | | was made. The valve in question (21SJ17) was subsequently physically | | removed from the system and inspected. No failure mode was determined. No | | evidence was found that the valve had been inoperable for any length of | | time. These valves do not have a history of negative performance in this | | application. A review of' industry data did not identify any similar | | sticking problems, generally the failure reported concerned leakage. | | Therefore, the guidance of NUREG 1022 applies. This guidance states that | | the out of service time is calculated using the time of discovery unless | | there is firm evidence based on a review of relevant information (e.g. the | | equipment history and cause of failure) to believe the discrepancy existed | | previously. Based on the time of discovery being the event date, this | | event is not reportable because the requirements of the Technical | | Specifications were being met for the current mode of operations and the | | event is bounded by current design. Further review of the design bases is | | underway to confirm assumptions. | | | | The licensee informed the NRC resident inspector. The Operations Center | | informed R1DO (Conte). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 35772 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: WILLIAM BEAUMONT HOSPITAL |NOTIFICATION DATE: 05/27/1999| |LICENSEE: WILLIAM BEAUMONT HOSPITAL |NOTIFICATION TIME: 13:41[EDT]| | CITY: ROYAL OAK REGION: 3 |EVENT DATE: 05/26/1999| | COUNTY: STATE: MI |EVENT TIME: 14:30[EDT]| |LICENSE#: 21-01333-01 AGREEMENT: N |LAST UPDATE DATE: 05/28/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ROGER LANKSBURY R3 | | |FRED COMBS NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: CHERYL SCHULTZ, RSO | | | HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - HOSPITAL DOSIMETER MEASURED A DOSE READING OF GREATER THAN 1000 RADS - | | | | AT 1430 ON 05/26/99, LYNN [LAST NAME UNKNOWN] EMPLOYED BY LANDAUER RADIATION | | BADGE DOSIMETRY COMPANY, GLENWOOD, IL, REPORTED TO CHERYL SCHULTZ, RADIATION | | SAFETY OFFICER (RSO), WILLIAM BEAUMONT HOSPITAL, ROYAL OAK, MI, THAT ONE OF | | BEAUMONT HOSPITAL'S RADIATION DOSIMETERS MEASURED A DOSE READING OF GREATER | | THAN 1000 RADS. THE RADIATION DOSIMETER IS A LUXEL ALUMINUM OXIDE FILMLESS | | RADIATION DOSIMETER THAT HAS BEEN USED IN THE INDUSTRY SINCE THE FALL OF | | 1998. THIS TYPE OF DOSIMETER HAS BEEN USED AT BEAUMONT HOSPITAL SINCE | | JANUARY 1999. THE HOSPITAL MEDICAL TECHNOLOGIST WHO USED THIS DOSIMETER | | WORKS IN A BLOOD BANK AND LAST USED A BLOOD IRRADIATOR IN APRIL 1999. THE | | IRRADIATOR CONTAINS A SELF CONTAINED SEALED 10,000 CURIE CESIUM-137 | | RADIATION SOURCE. | | | | THE HOSPITAL RSO STATED THAT THE IRRADIATOR IS FUNCTIONING PROPERLY AND THAT | | THE TECHNOLOGIST DID NOT RECEIVE THIS HIGH DOSE. THE RSO FURTHER STATED | | THAT HOSPITAL PERSONNEL HAVE NEVER RECEIVED GREATER THAN 0.06 MR/HR MAXIMUM | | DOSE RATE WITH THE IRRADIATOR SOURCE EXPOSED. THE RSO BELIEVES THAT THE | | DOSE READING IS INCORRECT OR THAT THE DOSIMETER SOMEHOW BECAME IRRADIATED. | | THE DOSIMETRY COMPANY REPRESENTATIVE STATED THAT THE DOSIMETER READINGS WERE | | OBTAINED TWICE AND THE DOSIMETER IS NOT DAMAGED. | | | | THE HOSPITAL RSO PLANS TO OBTAIN A BLOOD SAMPLE FROM THE TECHNOLOGIST AND | | HAVE IT ANALYZED ON 05/27/99. | | | | * * * UPDATE 5/28/99 FROM BRIAN SMITH (NMSS) TAKEN BY STRANSKY * * * | | | | The blood irradiator is a CIS-US Model IBL-473C with a source strength of | | approximately 2,000 Ci, contrary to the information provided in the initial | | report. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35774 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: GEORGIA DEPT. OF NATURAL RESOURCES |NOTIFICATION DATE: 05/28/1999| |LICENSEE: THERAGENICS, INC. |NOTIFICATION TIME: 10:05[EDT]| | CITY: BUFORD REGION: 2 |EVENT DATE: 05/26/1999| | COUNTY: STATE: GA |EVENT TIME: 08:00[EDT]| |LICENSE#: GA 881-2MD AGREEMENT: Y |LAST UPDATE DATE: 05/28/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |THOMAS DECKER R2 | | |FRED COMBS NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: TOM HILL | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INFORMATION REPORT RECEIVED FROM AN AGREEMENT STATE INVOLVING AN UNPLANNED | | CONTAMINATION EVENT | | | | "Description of Event : In accordance with Rule .03(14)(b)2. of the Rules | | and Regulations for Radioactive Material, Joseph Rodgers, Deputy RSO, ((770) | | 271-0233) notified the Department of an unplanned contamination event. | | While transporting a shielded 100 milliliter volumetric flask containing 24 | | Curies of purified liquid Pd 103 (cyclotron produced) the transport cart | | struck an object in the lab and the flask toppled out of the shield onto the | | floor. The Chemist immediately exited the area and notified health physics. | | Steps were immediately implemented to: minimize any exposure; prevent the | | spread of contamination; and initiate timely gross decontamination. Access | | to the room remains restricted and monitoring will continue with | | decontamination planned for the end of next week after the radiation levels | | are reduced by decay of the Palladium. Emergency processing of the film | | badges for the three involved employees was initiated with the following | | range of exposures reported for whole body: DDE 55 mrem to 277 mrem; LDE 61 | | mrem to 326 mrem; SDE 65 mrem to 355 mrem; and for extremities: SDE 170 mrem | | to 4040 mrem. Nasal swabs of the affected employees were negative. Results | | from a fixed air sampler, whose intake is directly above the area of the | | spill, indicated the 10 CFR Part 20 Appendix B values for inhalation were | | not exceeded. No radioactive materials were released outside the restricted | | area. Representatives of the Radiation Control Program visited the site on | | 5/27/99. The Licensee will submit a written report within 30 days, implement | | short term corrective actions and resume operation in this facility in early | | June, 1999." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35775 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/29/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 01:45[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/28/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 09:45[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/29/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |TONY VEGEL R3 | | DOCKET: 0707002 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC SPAETH | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR NRC BULLETIN 91-01 REPORT INVOLVING LOSS OF CRITICALITY CONTROL | | | | "On 5/28/99 at 0945 hrs operations personnel discovered a 5" polybottle | | containing uranium bearing material leaking solution from around the top of | | the container. The lid was found to be loose on the polybottle. An onsight | | NCS Engineer responded to the scene and assessed the condition to be a loss | | of control such that only one double contingency control remained in place. | | NCSA-PLANT006 requirement #2 and requirement #12 state in part: lids provide | | a barrier against spilling the material and the container is not moved while | | the lid is loose. | | | | "THERE WAS NO RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF | | THIS EVENT. | | | | "SAFETY SIGNIFICANCE OF EVENTS: | | | | "Safety Significance is low due to the small amount of material that leaked | | (10-20 ml) and the fact that the container was upright and spaced. | | | | "POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO[S] OF HOW | | CRITICALITY COULD OCCUR): | | | | "Sufficient leakage could have accumulated in an unfavorable geometry, i.e., | | a building drain. With a high enrichment to create a criticality. | | | | "CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.): | | | | "Geometry and spacing are the controlled parameters. | | | | "ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE OF CRITICAL MASS): | | | | "Amount of material is 10-20 ml of UF4 contaminated oil at 10.77% | | enrichment. | | | | "NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES: | | | | "The geometry of the container was deficient when the lid was left loose | | enough to allow material to slosh inside and seep through the threads. | | | | "CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED: | | | | "The material was cleaned up and some material decanted into another | | polybottle at approx. 1230 hrs. Remaining storage areas were policed for | | polybottles with loose lids, none were found." | | | | Operations informed the DOE Site Representative and the NRC Resident | | Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35776 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/29/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 01:45[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/28/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 08:10[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/29/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |TONY VEGEL R3 | | DOCKET: 0707002 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC SPAETH | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR NRC BULLETIN 91-01 REPORT INVOLVING LOSS OF CRITICALITY CONTROL | | | | "On Friday, May 28, 1999 at 0810 hours, Operating personnel discovered that | | a Nuclear Criticality Safety Approval (NCSA) Requirement was not being | | maintained in the X-705 Decontamination Facility. NCSA-PLANT 053.A01 titled | | 'Uranium Analysis and Sampling' requirement #8 states in part, Samples may | | be grouped together but groups shall be spaced a minimum of two feet edge-to | | edge. Six 250 ml sample bottles containing uranium bearing material were | | found within 16 inches of a polybottle. | | | | "THERE WAS NO LOSS OF HAZARDOUS/RADIOACTIVE MATERIAL OR | | RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF THIS EVENT. | | | | "SAFETY SIGNIFICANCE OF EVENTS: | | | | "The Safety Significance is low since all the material is less than 10% | | enrichment, the sample batch is less than 2 liters, and some spacing was | | provided. | | | | "POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO[S] OF HOW | | CRITICALITY COULD OCCUR): | | | | "Numerous spacing violations of highly concentrated uranium solutions can | | lead to a criticality in the absence of volume and/or geometry controls. | | | | "CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.): | | | | "Volume arid Interactions were the controlled parameters. Interactions was | | lost. | | | | "ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE OF CRITICAL MASS): | | | | "Six 250 ml sample bottles were involved containing various uranium bearing | | solutions of uranyl nitrate and/or uranyl fluoride. Enrichment is not | | expected to be greater than 10%. | | | | "NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES: | | | | "The applicable controls are volume and spacing. Spacing between the samples | | and the polybottle was lost. | | | | "CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED: | | | | "The spacing controls were corrected at 0900 hrs." | | | | Operations informed the DOE Site Representative and the NRC Resident | | Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35777 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/29/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 07:45[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/28/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 17:14[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/29/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |TONY VEGEL R3 | | DOCKET: 0707002 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: KEITH VANDERPOOL | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NON-CFR REPORT INVOLVING ACTUATION OF A SAFETY SYSTEM | | | | "ON MAY 28, 1999, AT APPROXIMATELY 1714 HOURS THE HOIST BRAKES ON THE SOUTH | | TAILS WITHDRAWAL CRANE ACTUATED. THE ACTUATION OCCURRED WHILE A FULL 14-TON | | LIQUID UF6 CYLINDER WAS BEING PLACED ON A RAIL CAR TO BEGIN THE REQUIRED | | 5-DAY COOL DOWN PERIOD. THE CRANE BRAKES FUNCTIONED AS DESIGNED TO PREVENT | | FURTHER MOVEMENT OF THE LIQUID UF6 CYLINDER. FOLLOWING THE ACTUATION. THE | | CYLINDER WAS SUSPENDED APPROXIMATELY TWELVE (12") INCHES ABOVE THE RAIL CAR | | CRADLE. THE EXACT CAUSE FOR THE ACTUATION IS CURRENTLY UNDER INVESTIGATION. | | HOWEVER, THE ACTUATION IS BELIEVED TO HAVE BEEN CAUSED BY A MALFUNCTION OF | | THE MECHANISM THAT KEEPS THE BRAKES IN AN OPEN POSITION WHEN LOADS ARE BEING | | RAISED AND LOWERED. PENDING FURTHER INVESTIGATION INTO THE CAUSE FOR THE | | BRAKE ACTUATION, THE BRAKE ACTUATION IS BEING CONSIDERED A VALID SAFETY | | SYSTEM ACTUATION AND REPORTABLE IN ACCORDANCE WITH THE SAR,TABLE 6.9, | | CRITERIA J2. | | | | "AS A PRECAUTIONARY MEASURE THE PLANT SHIFT SUPERINTENDENT DIRECTED THAT ALL | | LIQUID UF6 HANDLING CRANES BE TAGGED OUT-OF-SERVICE PENDING THE NOTED | | INVESTIGATION. NOTE AS A PRECAUTIONARY MEASURE SUPPORT CRADLES HAVE BEEN | | POSITIONED TO SUPPORT THE SUSPENDED LIQUID UF6 CYLINDER. CURRENT PLANS ARE | | TO LET THE CYLINDER COMPLETE THE REQUIRED 5-DAY COOL DOWN PERIOD PRIOR TO | | INITIATING FURTHER ACTIONS TO LOWER THE CYLINDER ONTO THE RAIL CAR. | | | | "THERE WAS NO LOSS OF HAZARDOUS/RADIOACTIVE MATERIAL OR | | RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF THIS EVENT." | | | | OPERATIONS INFORMED THE DOE SITE REPRESENTATIVE AND THE NRC RESIDENT | | INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35778 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 05/29/1999| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 18:37[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 05/29/1999| +------------------------------------------------+EVENT TIME: 17:24[EDT]| | NRC NOTIFIED BY: DAVID WALSH |LAST UPDATE DATE: 05/29/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD CONTE R1 | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 18 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | COURTESY CALL DUE TO UNIT SHUTDOWN | | | | "Susquehanna Unit 1 was manually shutdown on 5/29/99 to repair Fast Acting | | Solenoid Valves on the EHC System. At 1055 on 5/29/99, a controlled shutdown | | was commenced by reducing recirc flow and then inserting control rods. At | | 1704 on 5/29/99, the Main Turbine was manually tripped with power at 18%. At | | 1724, the reactor mode switch was taken to shutdown placing the unit in | | condition 3. Rx Water level dropped to approximately -0.5 inches as recorded | | on wide range instrumentation and was restored using Feedwater. There were | | no ECCS initiations or Diesel Generator starts. There were no challenges to | | containment as a result of the shutdown. - | | | | "This event does not represent a shutdown required by Technical | | Specifications. The ESF actuation of the Reactor Protection System and the | | resulting level 3 isolations are not reportable since it is procedurally | | recognized as preplanned. | | | | "The unit will be taken to cold shutdown to repair Fast Acting Solenoid | | Valves on the EHC System. Unit 2 was not affected by this event and is | | currently in Condition 1 at 100% power." | | | | The NRC resident inspector has been informed of this notification by the | | licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35779 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BROWNS FERRY REGION: 2 |NOTIFICATION DATE: 05/30/1999| | UNIT: [] [2] [] STATE: AL |NOTIFICATION TIME: 08:00[EDT]| | RXTYPE: [1] GE-4,[2] GE-4,[3] GE-4 |EVENT DATE: 05/30/1999| +------------------------------------------------+EVENT TIME: 05:22[CDT]| | NRC NOTIFIED BY: JOE BENNETT |LAST UPDATE DATE: 05/30/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS DECKER R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 EXPERIENCED VARIOUS ESF ACTUATIONS IN RESPONSE TO THE UNEXPECTED TRIP | | OF THE "2B" RPS MOTOR GENERATOR SET. | | | | "AT 0522CDT ON 5/30/99, THE '2B' REACTOR PROTECTION SYSTEM (RPS) MOTOR | | GENERATOR (MG) SET TRIPPED. THE CAUSE OF THE RPS MG SET TRIP HAS NOT BEEN | | DETERMINED. THE LOSS OF POWER RESULTED IN AN ISOLATION OF PRIMARY | | CONTAINMENT ISOLATION SYSTEM (PCIS) GROUPS 6 (VENTILATION) AND 8 (TIPS), AND | | PARTIAL ISOLATIONS OF GROUPS 3 (RWCU) AND 2 (DRYWELL SUMP ISOLATION VALVES). | | ADDITIONALLY, THE STANDBY GAS TREATMENT AND CREV SYSTEMS AUTOMATICALLY | | INITIATED. AT 0538CDT, ALTERNATE POWER WAS RESTORED AND THE SYSTEMS WERE | | RETURNED TO NORMAL. | | | | "THIS [EVENT] ALSO REQUIRES A 30 DAY WRITTEN REPORT PER 10 CFR | | 50.73(a)(2)(iv)." | | | | THERE WAS NO ONGOING ELECTRICAL MAINTENANCE AT THE TIME. THE LICENSEE | | INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35780 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DIABLO CANYON REGION: 4 |NOTIFICATION DATE: 05/30/1999| | UNIT: [1] [2] [] STATE: CA |NOTIFICATION TIME: 17:04[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/30/1999| +------------------------------------------------+EVENT TIME: 12:10[PDT]| | NRC NOTIFIED BY: DAVID PIERCE |LAST UPDATE DATE: 05/30/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GAIL GOOD R4 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION OF THE CAPTURE AND SUBSEQUENT RELEASE OF A GREEN SEA | | TURTLE | | | | The following text is a portion of a facsimile received from the licensee: | | | | "On 05/30/99 at approximately 1210 PDT, a male green sea turtle was removed | | from the Diablo Canyon Power Plant intake structure. The sea turtle had | | entered the intake structure by swimming under the apron wall and surfacing | | outside of the bar racks. The sea turtle was transported by boat to a | | release point approximately 0.5 miles due west of the intake structure. It | | was observed to swim strongly away from the release point. The turtle's | | shell length was measured at 69 cm, and its weight was estimated to be 50-75 | | lbs. The turtle appeared to be in good health with no visible injuries with | | the exception of some scrapes on the rear of its shell." | | | | "The Diablo Canyon Power Plant Environmental Services Department has | | notified the National Marine Fisheries Service and the California Department | | of Fish and Game of the capture and subsequent release of the sea turtle, | | which is protected under the Endangered Species Act." | | | | The licensee plans to notify the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35781 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 06/01/1999| | UNIT: [1] [] [] STATE: TX |NOTIFICATION TIME: 07:57[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 06/01/1999| +------------------------------------------------+EVENT TIME: 06:08[CDT]| | NRC NOTIFIED BY: JANAK |LAST UPDATE DATE: 06/01/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GAIL GOOD R4 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOST/STOLEN/UNACCOUNTED/FALSIFIED KEY CARDS/I.D. CARDS/KEYS/OTHER ACCESS | | DEVICE. | | IMMEDIATE COMPENSATORY MEASURES TAKEN UPON DISCOVERY. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35782 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NUCLEAR LOGISTICS INC |NOTIFICATION DATE: 06/01/1999| |LICENSEE: NUCLEAR LOGISTICS INC |NOTIFICATION TIME: 11:07[EDT]| | CITY: FORT WORTH REGION: 4 |EVENT DATE: 04/19/1999| | COUNTY: STATE: TX |EVENT TIME: [CDT]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 06/01/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |VERN HODGE(FAX) NRR | | |RICHARD CONTE R1 | +------------------------------------------------+ | | NRC NOTIFIED BY: SEIKEN (FAX) | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PART 21 REPORT - DEVIATION IN A NUCLEAR LOGISTICS INC (NLI) DC POWER | | SUPPLY. | | | | A DEVIATION HAS BEEN IDENTIFIED IN A NLI DC POWER SUPPLY, P/N | | NLI-LGS-G-24-OV-R-8018 WHICH HAVE BEEN SUPPLIED AS A CLASS 1E COMPONENT, | | THAT ALLOWS A PREMATURE OVER VOLTAGE PROTECTION ACTUATION TO OCCUR IN A | | CIRCUIT SPECIFIC APPLICATION. THIS CONDITION OCCURRED DURING DIESEL | | GENERATOR STARTUP, SPECIFICALLY DURING DIESEL GENERATOR LOADING. THIS ISSUE | | WAS DETERMINED TO BE A DEVIATION ON 4/19/99, HOWEVER, TO DATE NLI HAS NOT | | BEEN ABLE TO DUPLICATE THIS CONDITION DURING LABORATORY TESTING. DATA | | COLLECTION AND ADDITIONAL TESTING IS BEING PERFORMED TO RESOLVE THE | | DEVIATION. IT THE PREMATURE OVER VOLTAGE PROTECTION ACTUATION IS DETERMINED | | TO BE THE RESULT OF THE POWER SUPPLY DESIGN, OTHER NLI-L SERIES POWER | | SUPPLIES WILL BE TESTED TO DETERMINE THEIR SUSCEPTIBILITY TO SIMILAR | | CONDITIONS. TESTING AND EVALUATION ACTIVITIES WILL BE COMPLETED ON 7/16/99. | | THESE COMPONENTS HAVE BEEN SUPPLIED AS SAFETY-RELATED COMPONENTS TO PUBLIC | | SERVICE ELECTRIC AND GAS COMPANY. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 35783 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MID MICHIGAN MEDICAL CENTER |NOTIFICATION DATE: 06/01/1999| |LICENSEE: MID MICHIGAN MEDICAL CENTER |NOTIFICATION TIME: 11:23[EDT]| | CITY: MIDLAND REGION: 3 |EVENT DATE: 05/24/1999| | COUNTY: STATE: MI |EVENT TIME: [EDT]| |LICENSE#: 21-01549-02 AGREEMENT: N |LAST UPDATE DATE: 06/01/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |DAVID HILLS R3 | | | | +------------------------------------------------+ | | NRC NOTIFIED BY: LANGRILL | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MEDICAL MISADMINISTRATION OCCURRED AT THE MID MICHIGAN MEDICAL CENTER DURING | | ADMINISTRATION OF A THERAPY DOSE OF I-131. | | | | A PATIENT WAS TO RECEIVE 150 MILLICURIES OF I-131 FOR A PRESCRIBED THERAPY | | DOSE, BUT ACTUALLY RECEIVED 100 MILLICURIES OF I-131. THE PRESCRIBING | | PHYSICIAN WAS NOTIFIED BUT IT IS NOT KNOWN WHETHER THE PATIENT HAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 35784 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: POWER RESOURCES |NOTIFICATION DATE: 06/01/1999| |LICENSEE: POWER RESOURCES |NOTIFICATION TIME: 14:39[EDT]| | CITY: GLENROCK REGION: 4 |EVENT DATE: 06/01/1999| | COUNTY: CONVERSE STATE: WY |EVENT TIME: 09:30[MDT]| |LICENSE#: SUA1511 AGREEMENT: N |LAST UPDATE DATE: 06/01/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |LINDA HOWELL R4 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: WILLIAM KEARNEY | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BYPRODUCT MATERIAL SPILLED IN A RESTRICTED AREA | | | | A backhoe accidentally broke a pipeline from the central plant to the waste | | disposal well causing a spill of about 4000 gallons of fluid. The fluid | | contained approximately 15-20 ppm U3O8. The pipeline was not in use at the | | time of the break so only the fluid in the pipe drained into the ditch that | | the backhoe was digging. The fluid has been pumped back into the process | | facility and any residual solids have been cleaned up. The accident | | occurred within the confines of the site. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35785 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 06/02/1999| | UNIT: [] [2] [] STATE: FL |NOTIFICATION TIME: 01:09[EDT]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 06/01/1999| +------------------------------------------------+EVENT TIME: 20:55[EDT]| | NRC NOTIFIED BY: JACK BREEN |LAST UPDATE DATE: 06/02/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KENNETH BARR R2 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |50 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - TS REQUIRED PLANT SHUTDOWN DUE TO DROPPED CONTROL ROD FOR UNKNOWN REASONS | | - | | | | AT 2055 ON 06/01/99, WITH UNIT 2 AT 100% POWER, CONTROL ELEMENT ASSEMBLY | | (CONTROL ROD) #40 OF SHUTDOWN GROUP 'B' DROPPED INTO THE REACTOR CORE FOR | | UNKNOWN REASONS. NO MAINTENANCE OR TESTING ACTIVITIES WERE BEING CONDUCTED | | AT THE TIME. | | | | THE LICENSEE DECLARED THE CONTROL ROD INOPERABLE AND REDUCED POWER TO | | INVESTIGATE THE CAUSE OF THE DROPPED CONTROL ROD. TECH SPEC 3.1.3.1 | | REQUIRES THE LICENSEE TO RESTORE THE CONTROL ROD TO OPERABLE STATUS WITHIN | | 6 HOURS OR PLACE UNIT 2 IN HOT SHUTDOWN MODE. | | | | THIS EVENT HAS NO EFFECT ON UNIT 1 WHICH IS AT 100% POWER. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | | | | * * * UPDATE AT 0210 ON 06/02/99 BY JOE MARTIN TO JOLLIFFE * * * | | | | AT 0210 ON 06/02/99, I & C TECHNICIANS REPLACED A FAILED HALL EFFECT | | TRANSDUCER (CURRENT SENSOR) WHICH CAUSED CONTROL ELEMENT ASSEMBLY #40 TO | | TRIP OPEN AND DROP INTO THE REACTOR CORE. PLANT OPERATORS WITHDREW THE | | CONTROL ROD, DECLARED IT OPERABLE, AND EXITED TECH SPEC 3.1.3.1. | | | | THE LICENSEE PLANS TO INFORM THE NRC RESIDENT INSPECTOR. | | | | THE NRC OPERATIONS OFFICER NOTIFIED THE R2DO KEN BARR. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021