Event Notification Report for May 10, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/07/1999 - 05/10/1999 ** EVENT NUMBERS ** 35612 35621 35634 35682 35688 35689 35690 35692 35693 35694 35695 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35612 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MA DEPT OF PUBLIC HEALTH RCP |NOTIFICATION DATE: 04/21/1999| |LICENSEE: AEA TECHNOLOGIES QSA, INC |NOTIFICATION TIME: 15:00[EDT]| | CITY: BURLINGTON REGION: 1 |EVENT DATE: 04/21/1999| | COUNTY: STATE: MA |EVENT TIME: 14:00[EDT]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 05/07/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MOHAMED SHANBAKY R1 | | |FREDERICK COMBS NMSS | +------------------------------------------------+JOSEPH GIITTER IRO | | NRC NOTIFIED BY: KEN TRAEGDE |DONNA MARIE PEREZ IP | | HQ OPS OFFICER: DICK JOLLIFFE |LEN WERT R2 | +------------------------------------------------+DALE POWERS R4 | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | |NOCM COMM ASST BRIEF | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - SHIPMENT OF 8 Ir-192 SOURCES (866 CURIES TOTAL) FROM BURLINGTON, MA, | | OVERDUE IN MEXICO - | | | | At 1500 EDT on 04/21/99, Ken Traegde of the Massachusetts Department of | | Public Health Radiation Control Program (RCP) located in Boston, | | Massachusetts, reported that on 04/16/99, AEA Technology QSA, Inc., located | | in Burlington, Massachusetts, shipped a Model-855 source changer loaded with | | eight Iridium-192 sources (totaling 866 curies) via Federal Express to | | Vicont S.A. De C.V. located in Toluca, Mexico. The undamaged package had a | | transport index of 1.4 (normal readings of 1.4 mR/hour at 1 meter and 55 | | mR/hour at the surface) at the time of shipment. | | | | The shipment was scheduled to arrive in Mexico on 04/17/99. As of 1400 EDT | | on 04/21/99, the recipient (Vicont S.A. De C.V.) had received the shipping | | papers but not the container. The shipper and Federal Express have launched | | a full search for the package. The Federal Express Hazardous Material | | Investigation Team has conducted a physical search of Express Depots in | | Boston, Memphis, Los Angeles, and Mexico. | | | | The license numbers are: SU-1485, 12-8361, 52-0243, 54-0237, and 58-0242. | | | | The NRC operations officer notified the Department of Transportation via the | | National Response Center (Gauthier); Report number 481132. | | | | (Contact the NRC operations officer for applicable telephone numbers.) | | | | *********************************** UPDATE AT 1345 ON 04/22/99 BY JONES | | *********************************** | | | | The NRC entered the Monitoring Phase of Normal Mode at 1345 on 04/22/99. | | The NRC operations officer notified the R1DO (Shanbaky), Region 1 (Miller), | | IRO (Congel and Giitter), NMSS (Paperiello), RCT (Weinstein), OPA (Gagner), | | EDO's office (Charleen Raddatz), and Chairman's office (Holian). The RCT | | notified the Federal Emergency Management Agency (Dan Rishe), Department of | | Energy (Thomas Yates), Department of Agriculture (Bob Conley), Department of | | Health and Human Services (James Raab), and Environmental Protection Agency | | and Department of Transportation via the National Response Center (Ms. | | Reddy). | | | | *********************************** UPDATE AT 1600 ON 04/22/99 BY JONES | | *********************************** | | | | A Commissioner's Assistants Briefing was conducted at 1600 on 04/22/99. The | | following notifications were made (* office did not participate): IRO (Joe | | Giitter and Eric Weinstein), Chairman Jackson (Dan Gillen), Commissioner | | Dicus (Joel Lubenau), Commissioner Diaz (Patrick Castleman), Commissioner | | McGaffigan (Janet Schlueter), Commissioner Merrifield (JohnThoma), EDO (*Dan | | Martin), DEDE (*Jocelyn Mitchell), NMSS (Don Cool and Carl Paperiello), NMSS | | EO (Fred Combs), R1DO (Mohamed Shanbaky), OPA (Joe Gilland), CAO (Thomas | | Madden), SECY (Andrew Bates), OSP (Paul Lohaus), OIP (Ron Hauber), Region 1 | | (Felicia Hinson and Jim Wiggins, etc), and Region 2 (Doug Collins, Chuck | | Hosey, and Dick Woodruff). The briefer was Fred Combs of NMSS. | | | | At 1610, the NRC operations officer played a tape of briefing for EDO (Dan | | Martin) and DEDE (Jocelyn Mitchell). | | | | ****************************** UPDATE AT 1230 ON 04/23/99 BY TROCINE AND | | JONES ****************************** | | | | A conference call was conducted at 1230 on 04/23/99 to update the status of | | this event. The following NRC offices participated (among others): IRO | | (Himes), NMSS (Brach, Combs, and Cook), Region 1 (Lloyd), Region 2 (Collins | | and Woodruff), Region 4 (Andrews), OPA (Hayden), OIP (Lieberman), OSP | | (Lohaus), and EDO (Raddatz). In addition, the following agencies | | participated: Department of Transportation (Rick Boyle), Massachusetts | | Department of Public Health RCP (Ken Traegde), Federal Express (Scott Mugno, | | Pat Oppenheimer, and Roy Parker), State of Tennessee (Alan Grewe), Tennessee | | Division of Radiation Health (Eddy Nanney), AEA Technology QSA, Inc. (Eric | | Okvist), and Environmental Protection Agency located in Atlanta (Paul | | Wagner). | | | | During this conference call, representatives of Federal Express reported | | that they are confident that the shipment of eight Iridium-192 sources left | | Boston. They issued an 'all-points' search order, faxed a description to | | all 'logical' locations, and conducted repeat physical searches in Memphis, | | Boston, and Mexico, all without locating the shipment to date. (The Los | | Angeles depot was not searched as had been reported on 04/21/99.) | | Massachusetts and Tennessee health authorities conducted radiological | | surveys in Boston and Memphis on 04/22/99 with negative results. | | | | Rick Boyle of the Department of Transportation notified the competent | | authority in Mexico, and Federal Express requested a detailed search of the | | Customs facilities in Mexico City. | | | | The next conference call is scheduled for 1230 EDT on Wednesday, 04/28/99. | | | | ************************* UPDATE AT 1333 ON 04/26/99 FROM TRAEGDE TO TROCINE | | ************************* | | | | At 0619 EDT on 04/26/99, Federal Express confirmed that the serial number on | | a Model-855, Type-B package found at the Stansted Airport (located outside | | of London, England) matched the serial number for the missing package | | containing the eight Iridium-192 sources. The Massachusetts Department of | | Public Health RCP was informed of this discovery by AEA Technology QSA, | | Inc., at 0933 EDT on 04/26/99. The package was reported to be intact and | | undisturbed. The carrier (Federal Express) contacted the shipper (AEA | | Technology QSA, Inc.), and the shipper requested that the package be | | forwarded to its intended destination. Accordingly, the package will be | | shipped from Stansted Airport to Toluca, Mexico, via Memphis, Tennessee. | | Federal Express informed the Massachusetts Department of Public Health RCP | | that the package is expected to arrive in Memphis, Tennessee, by tomorrow | | morning (04/27/99). | | | | The Massachusetts Department of Public Health RCP notified NRC Region 1 | | (Duncan White). The NRC Operations Officer notified the R1DO (Anderson); | | R2DO (Wert); R4DO (Graves); NMSS (Combs); IRO (Giitter, Miller, and Congel); | | RCT (Bailey). | | | | *********************************** UPDATE AT 1600 ON 04/26/99 BY TROCINE | | *********************************** | | | | A conference call was conducted at 1600 on 04/26/99 to update the status of | | this event. The following NRC offices participated (*office did not | | participate): IRO (Giitter), RCT (Bailey), NMSS (Brach and Cool), Region 1 | | (Kinneman), Region 2 (Hosey), Region 4 (*Graves), Region 1 Public Affairs | | (*Screnci and *Sheehan), HQ OPA (Beecher), OIP (Lieberman), OSP (Bolling and | | Lohaus), and EDO (Raddatz). In addition, the following agencies | | participated: Massachusetts Department of Public Health RCP (Ken Traegde), | | State of Tennessee (Alan Grewe and Mike Mobley), and Tennessee Division of | | Radiation Health (Eddy Nanney). | | | | Based upon the information discussed during this conference call (reference | | the 1333 04/26/99 update above), the NRC exited the Monitoring Phase of | | Normal Mode at 1615 on 04/26/99. | | | | The NRC operations officer notified the IRO (Giitter, Miller, and Congel); | | RCT (Bailey); NMSS EO (Cool); NMSS (Brach); Region 1 (Kinneman); Region 2 | | (Hosey); R1DO (Anderson); R2DO (Wert); R4DO (Graves); OPA (Beecher); OIP | | (Lieberman); OSP (Bolling and Lohaus); and EDO (Raddatz). The RCT notified | | the Federal Emergency Management Agency (Butch Steindurf), Department of | | Energy (Kevin Moore), Department of Agriculture (George Bickerton), | | Department of Health and Human Services (E.K. Gray), and Environmental | | Protection Agency and Department of Transportation via the National Response | | Center (Gauthier). | | | | **** UPDATE AT 1505 ON 04/29/99 FROM DAKUBU TAKEN BY WEAVER **** | | | | Dr. Dakubu of the Massachusetts Department of Public Health Radiation | | Control Program informed the NRC Operations Center that the sources arrived | | safely at their intended destination in Mexico on 04/28/98. The NRC | | Operations Officer informed the R1DO (Cliff Anderson) and NMSS EO (Larry | | Camper). | | | | **** UPDATE AT 0900 ON 04/30/99 BY JOLLIFFE **** | | | | The sources arrived in Mexico on 04/28/99 (not 04/28/98, as specified | | above). | | | | **** UPDATE AT 1209 ON 05/07/99 BY TROCINE **** | | | | This event has been updated to correct the notifications made to other | | agencies. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35621 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CRYSTAL RIVER REGION: 2 |NOTIFICATION DATE: 04/22/1999| | UNIT: [3] [] [] STATE: FL |NOTIFICATION TIME: 19:02[EDT]| | RXTYPE: [3] B&W-L-LP |EVENT DATE: 04/22/1999| +------------------------------------------------+EVENT TIME: 18:08[EDT]| | NRC NOTIFIED BY: BILL BANDHAUGER |LAST UPDATE DATE: 05/07/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LEN WERT R2 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBLE OVERLOAD OF ESF TRANSFORMER IN AN ABNORMAL OPERATING PROCEDURE | | FOUND | | | | While investigating a previous Licensee Event Report concerned with backfeed | | the following was discovered: | | "During a scenario involving a Loss of Off-Site Power resulting from a loss | | of the BEST and Startup transformers, the Crystal River Unit 3 abnormal | | operating procedures could have caused an overload of the safety-related | | Engineered Safeguards 4160V to 480V transformer. Assuming a single failure | | of the 'B' side diesel generator, power could have been unavailable to both | | trains of 480V Engineered safeguards loads. This condition is considered | | reportable per 10CFR50.72(b)(l)(ii)(B) and 10CFR50.73(a)(2)(ii)(B) as a | | condition outside of the design basis of the plant. Loads have been | | identified which can be administratively maintained off during this scenario | | to avoid the overload condition, and therefore, the transformer is | | operable." | | | | This condition is under investigation and further actions will be | | forthcoming. | | | | The licensee intends to notify the NRC Resident Inspector. | | | | **** UPDATE ON 05/07/99 AT 2311 BY RAWLS TO GOULD **** EVENT RETRACTION | | | | THE LICENSEE AND ABB POWER T&D CO, INC HAVE EVALUATED POSSIBLE OVERLOAD | | CONDITIONS OF THE "A" 4160/480V TRANSFORMER DURING A LOSS OF OFFSITE POWER | | WITH THE LOSS OF THE "B" BATTERY SCENARIO. THE RESULTS OF THE EVALUATIONS | | SHOW THAT THE CLASS 1E TRANSFORMER AND COMPONENTS WILL PERFORM THEIR | | DESIGNED FUNCTION FOR LONGER THAN 30 DAYS WITHOUT FAILURE. THE TRANSFORMER | | WILL SURVIVE LONGER THAN ONE YEAR UNDER THE IDENTIFIED LOAD CONDITIONS BASED | | ON A REVIEW OF ANSI/IEEE C57.96. IN ADDITION, THE NON-CLASS 1E CROSSTIES | | CIRCUITS TO THE RX AUX BUS 3A/3B ARE LICENSING BASIS REQUIREMENTS AND ARE | | NOT DESIGN BASIS REQUIREMENTS. THE LICENSEE IS THEREFORE RETRACTING THIS | | EVENT. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. THE NRC OPERATIONS | | OFFICER NOTIFIED THE R2DO CHRIS CHRISTENSEN. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35634 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SURRY REGION: 2 |NOTIFICATION DATE: 04/26/1999| | UNIT: [] [2] [] STATE: VA |NOTIFICATION TIME: 11:13[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 04/26/1999| +------------------------------------------------+EVENT TIME: 08:37[EDT]| | NRC NOTIFIED BY: HILBERT-SEMMES |LAST UPDATE DATE: 05/07/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LEN WERT R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT RECEIVED A TRAIN "B" HIGH CONSEQUENCE-LIMITING SAFEGUARDS (CLS) | | SIGNAL. | | | | THIS OCCURRED WHEN AN ELECTRICIAN LIFTED A LEAD WHILE REPLACING RELAY | | "2-CLS-RLY-1B1" IN THE "B" TRAIN HIGH CLS SYSTEM. ONE CONTAINMENT TRIP | | VALVE FOR THE CONTAINMENT PARTICULATE AND GAS RADIATION MONITORS | | REPOSITIONED (CLOSED), AND THE PARTICULATE AND GAS RADIATION MONITOR PUMP | | DE-ENERGIZED. A SAFETY INJECTION SIGNAL WAS NOT RECEIVED AS IT WAS | | PROPERLY DEFEATED IN ACCORDANCE WITH STATION PROCEDURES. THE ELECTRICIANS | | VERIFIED THAT THE HIGH CLS SYSTEM WAS DE-ENERGIZED AS THEY WOULD EXPECT | | PRIOR TO PERFORMING WORK TO PREVENT A SPURIOUS ACTUATION. THE LICENSEE IS | | INVESTIGATING THE CAUSE AND THE REQUIRED CORRECTIVE ACTIONS. THE HIGH CLS | | SIGNAL WAS RESET SINCE THE 2/4 CONTAINMENT PRESSURE < 14.2 PSIA MATRIX WAS | | MET DUE TO THE ACCURACY OF THE GAUGES. THE TRIP VALVE WAS PLACED IN THE | | PRE-EVENT CONDITION (OPEN), AND THE RADIATION MONITOR PUMP WAS RE-ENERGIZED | | AND RESTARTED. CORE OFF LOAD WAS NOT IN PROGRESS AT THE TIME OF THIS | | EVENT. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED BY THE LICENSEE. | | | | ***************** UPDATE AT 1102 ON 05/07/99 FROM LISA HILLBERT-SEMMES TO | | TROCINE ****************** | | | | The licensee is retracting this event notification. | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At 1113 on April 26, 1999, a 4-hour Non-Emergency Notification was made in | | accordance with 10CFR50.72(b)(2)(ii) due to an ESF actuation. An | | inadvertent Unit 2 High Consequence Limiting Safeguards (CLS) signal for | | Train 'B' was caused by maintenance activities when replacing a High CLS | | relay (#2-CLS-RLY-1B1) with Unit 2 in Refueling Shutdown. The High CLS | | signal only initiated the closure of containment trip valve #2-RM-TV-200B, | | which caused the sample pump, #2-RM-P-200, for the containment particulate | | and gaseous radiation monitors to de-energize." | | | | "NUREG-1022, Event Reporting Guidelines 10CFR50.72 and 50.73, states that | | 'The Commission is interested both in events where an ESF was needed to | | mitigate the consequences (whether or not the equipment performed properly) | | and events where an ESF actuated unnecessarily.... Usually, the staff would | | not consider this to include single component actuations because single | | components of complex systems, by themselves, usually do not mitigate the | | consequences of significant events.'" | | | | "Based on further review of this event and guidance provided in NUREG-1022, | | it was determined that this event was not reportable as the High CLS signal | | was invalid and resulted in the actuation of only one component which did | | not mitigate the consequences of the event." | | | | "This notification is made to retract the report made on April 26, 1999, | | based on the above discussion." | | | | The licensee notified the NRC Resident Inspector. The NRC Operations | | Officer notified the R2DO Chris Christensen. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35682 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUMMER REGION: 2 |NOTIFICATION DATE: 05/06/1999| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 07:34[EDT]| | RXTYPE: [1] W-3-LP |EVENT DATE: 05/06/1999| +------------------------------------------------+EVENT TIME: 06:45[EDT]| | NRC NOTIFIED BY: JIM PROPER |LAST UPDATE DATE: 05/07/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHRIS CHRISTENSEN R2 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ATTEMPTED INTRODUCTION OF CONTRABAND INTO THE PROTECTED AREA (1-hour report | | in accordance with 10CFR73.71, Appendix G) | | | | The licensee reported an attempted introduction of contraband into the | | protected area. Immediate compensatory measurements were taken upon | | discovery. (Contact the NRC Operations Officer for additional details and | | for a site contact telephone number.) | | | | The licensee notified the NRC Resident Inspector. | | | | **** UPDATE AT 1314 ON 05/07/99 FROM RICE TO GOULD **** EVENT RETRACTION | | | | THE LICENSEE HAS INVESTIGATED THIS EVENT FURTHER AND HAS DETERMINED THAT THE | | EVENT IS NOT REPORTABLE SINCE THERE WAS NO DELIBERATE INTENT TO INTRODUCE | | CONTRABAND INTO THE PROTECTED AREA. A BACKGROUND CHECK CONFIRMED NO | | CRIMINAL HISTORY FOR THE INDIVIDUAL. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | | | | THE NRC OPERATIONS OFFICER NOTIFIED THE R2DO CHRIS CHRISTENSEN. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 35688 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: USAF RADIOISOTOPE COMMITTEE |NOTIFICATION DATE: 05/07/1999| |LICENSEE: USAF RADIOISOTOPE COMMITTEE |NOTIFICATION TIME: 10:45[EDT]| | CITY: Sumptor REGION: 2 |EVENT DATE: 05/07/1999| | COUNTY: STATE: SC |EVENT TIME: 09:38[EDT]| |LICENSE#: 42-23539-01AF AGREEMENT: Y |LAST UPDATE DATE: 05/07/1999| | DOCKET: 03028641 |+----------------------------+ | |PERSON ORGANIZATION | | |CHRIS CHRISTENSEN R2 | | |BILL JONES R4 | +------------------------------------------------+DON COOL NMSS | | NRC NOTIFIED BY: MAJOR JAMES HICKS |FRANK CONGEL IRO | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF A MISSING CHEMICAL AGENT MONITOR CONTAINING 15 mCi OF NICKEL-63 | | FROM SHAW AIR FORCE BASE LOCATED IN SUMPTOR, SOUTH CAROLINA | | | | At 0938 on 05/07/99, Shaw Air Force Base (AFB) located in Sumptor, South | | Carolina, notified the U.S. Air Force Radioisotope Committee located at | | Bolling AFB located in Washington D.C. of a missing chemical agent monitor | | (CAM) containing a 15-mCi nickel-63 source. | | | | On 04/27/99, the base radiation safety officer (RSO) at Shaw AFB conducted | | an inventory of CAMs located in building #1981. The correct number of CAMs | | were there, but one had the wrong serial number. Examination of previous | | inventories shows one CAM with a different serial number. The building had | | been searched with no success. The 20CES/CEX RSO has no explanation for the | | different serial number on one CAM or where the correct CAM may be located. | | | | | | It is suspected that the CAM may have been exchanged with another Air Force | | Unit or may have been sent off for calibration. At this time, the U.S. Air | | Force Radioisotope Committee believes that the CAM is still in Air Force | | possession. Past shipping records will be researched, and calibration labs | | that serve Shaw AFB will be notified. The completion time for these actions | | is currently estimated to be 06/07/99. | | | | Call the NRC Operations Officer for a licensee contact telephone number. | | | | The licensee plans to notify the NRC Region 4 office and plans to issue a | | 30-day written report. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35689 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 05/07/1999| | UNIT: [1] [] [] STATE: GA |NOTIFICATION TIME: 11:09[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 05/07/1999| +------------------------------------------------+EVENT TIME: 08:21[EDT]| | NRC NOTIFIED BY: EDWEN URQUHART |LAST UPDATE DATE: 05/07/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHRIS CHRISTENSEN R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 53 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR SCRAM DUE TO LOSS OF EHC PRESSURE | | | | An automatic reactor scram occurred due to high reactor vessel pressure | | (1080 psig) after the main turbine stop and control valves drifted closed. | | All control rods inserted following the scram, and all systems functioned as | | expected. Neither the HPCI nor RCIC systems started, as reactor vessel | | water level did not decrease to the automatic actuation setpoint. The | | licensee reported that an operator inadvertently isolated the main turbine | | electrohydraulic control (EHC) system oil supply while tagging out the | | standby EHC oil pump, causing the turbine stop and control valves to drift | | closed. | | | | The NRC Resident Inspector has been informed of this notification by the | | licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35690 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 05/07/1999| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 12:41[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 05/07/1999| +------------------------------------------------+EVENT TIME: 09:50[EDT]| | NRC NOTIFIED BY: LANGE |LAST UPDATE DATE: 05/07/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES LINVILLE R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 59 Power Operation |59 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE DECLARED THE HIGH PRESSURE CORE SPRAY (HPCS) SYSTEM INOPERABLE | | AND ENTERED A 14 DAY LCO ACTION STATEMENT. | | | | THE HPCS SYSTEM FAILED TO MEET THE CHANNEL CHECK CRITERIA AND WAS DECLARED | | INOPERABLE, BUT FUNCTIONAL. TWO TRIP UNITS WERE FOUND NOT TO BE WITHIN THE | | 13 INCHES LIMIT FOR LEVEL INITIATION INSTRUMENTATION (THEY MEASURED 15 | | INCHES). A WORK ORDER HAS BEEN GENERATED TO CORRECT THE PROBLEM BEFORE THE | | TIME CLOCK EXPIRES FOR THE LCO ACTION STATEMENT. THE REACTOR IS CURRENTLY | | IN SINGLE LOOP OPERATION AT 59% POWER. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35692 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/07/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 23:00[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/07/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 13:45[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/07/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |MONTE PHILLIPS R3 | | DOCKET: 0707001 |JOHN GREEVES NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: BEASLEY | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PRIMARY CONDENSATE ALARM RECEIVED AT THE C-337-A FACILITY. | | | | A PRIMARY CONDENSATE ALARM WAS RECEIVED ON THE C-337-A #1 EAST AUTOCLAVE | | WATER INVENTORY CONTROL (WIC) SYSTEM. THE WIC SYSTEM IS REQUIRED TO BE | | OPERABLE WHILE HEATING IN MODE 5 ACCORDING TO TECHNICAL SAFETY REQUIREMENT | | #2.2.4.2. THE AUTOCLAVE WAS CHECKED ACCORDING TO THE ALARM RESPONSE | | PROCEDURE, AND SUBSEQUENTLY REMOVED FROM SERVICE AND DECLARED INOPERABLE. | | TROUBLESHOOTING WAS INITIATED AND IS CONTINUING IN ORDER TO DETERMINE THE | | REASON FOR THE ALARM. | | | | THE NRC RESIDENT INSPECTOR WAS INFORMED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35693 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: COGEMA MINING, INC |NOTIFICATION DATE: 05/08/1999| |LICENSEE: COGEMA MINING, INC |NOTIFICATION TIME: 11:32[EDT]| | CITY: REGION: 4 |EVENT DATE: 05/08/1999| | COUNTY: CAMPBELL STATE: WY |EVENT TIME: 01:30[MDT]| |LICENSE#: SUA-1341 AGREEMENT: N |LAST UPDATE DATE: 05/08/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BILL JONES R4 | | |JOHN GREEVES NMSS | +------------------------------------------------+MORRIS DOE | | NRC NOTIFIED BY: JOHN VASELIN, RSO |ALLRED HHS | | HQ OPS OFFICER: DICK JOLLIFFE |CANUPP FEMA | +------------------------------------------------+MASON EPA | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NONR OTHER UNSPEC REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - 15,000 GALLON MINING INJECTION SOLUTION SPILL - | | | | A WELLFIELD MINING INJECTION SOLUTION ("BARREN LIXIVIANT") SPILL OCCURRED AT | | THE IN-SITU LEACH INJECTION MINE UNIT 5 (#5BD47-1) AT THE CHRISTENSEN MINE | | IN CAMPBELL COUNTY, WY. | | | | THE SPILL, WHICH IS ESTIMATED TO BE 15,000 GALLONS WITH A URANIUM | | CONCENTRATION OF | | 1.0 mg/I OF U3O8, IS THE RESULT OF A PLUMBING FAILURE AT THE INJECTION WELL | | HEAD. THE SPILL WAS REPORTED TO THE NRC SINCE IT IS GREATER THAN 10,000 | | GALLONS, WHICH IS CONSIDERED SIGNIFICANT FROM AN OPERATIONS STANDPOINT. | | | | THE SOLUTION SPILLED ONTO THE NEARBY SOIL AND IT IS ANTICIPATED THAT THE | | SPILL DOES NOT POSE A HEALTH OR ENVIRONMENTAL HAZARD DUE TO ITS LOW | | CONCENTRATION OF URANIUM. THERE ARE NO RESIDENTS WITHIN ONE MILE OF THE | | SPILL AND THE NEAREST TOWN IS FURTHER THAN 15 MILES AWAY. | | | | THE INJECTION WELL WAS SHUT DOWN AND THE SPILL WAS STOPPED. THE WELL WILL | | NOT BE USED UNTIL THE PLUMBING IS REPAIRED. A SOIL SAMPLE HAS BEEN | | COLLECTED AT THE SPILL LOCATION AND WILL BE ANALYZED FOR THE PRESENCE OF | | Ra-226 TO DETERMINE IF SOIL CLEAN-UP IS NECESSARY. | | | | THE RADIATION SAFETY OFFICER (RSO) PLANS TO NOTIFY THE WYOMING STATE | | DEPARTMENT OF ENVIRONMENTAL QUALITY AND PLANS TO SUBMIT A WRITTEN REPORT TO | | THE NRC WITHIN 7 DAYS. | | | | HOO NOTE: SEE SIMILAR EVENTS #35524, #35542 AND #35593. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35694 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 05/08/1999| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 14:58[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 05/08/1999| +------------------------------------------------+EVENT TIME: 13:35[CDT]| | NRC NOTIFIED BY: CHRISTIAN |LAST UPDATE DATE: 05/09/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MONTE PHILLIPS R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR SCRAM FROM 100% POWER DUE TO SJAE HIGH PRESSURE ISOLATION. | | | | CONTROL ROOM OPERATORS MANUALLY SCRAMMED THE REACTOR FROM 100% POWER DUE TO | | A STEAM JET AIR EJECTOR (SJAE) HIGH PRESSURE ISOLATION. THE CAUSE OF THE | | ISOLATION IS UNKNOWN AND BEING INVESTIGATED. ALL CONTROL RODS FULLY | | INSERTED AND NO ECCS INJECTIONS OCCURRED. THE PLANT ALSO RECEIVED A | | PRIMARY CONTAINMENT ISOLATION (PCI) SYSTEM GROUP 1 (MSIVs CLOSED), GROUP 2 | | (TORUS AND DRYWELL VENTS) AND GROUP 3 (RWCU SYSTEM) ISOLATIONS. ONE SRV | | CYCLED OPEN AND CLOSED PROPERLY. HOWEVER, A SECOND SRV INDICATED HIGH TAIL | | PIPE TEMPERATURE. THE LICENSEE IS INVESTIGATING THIS CONDITION. | | | | THE LICENSEE PLANS TO INFORM THE NRC RESIDENT INSPECTOR. | | | | * * * UPDATE AT 1035 ON 05/09/99 BY PAT DECKER TO JOLLIFFE * * * | | | | DURING THE SRV OPENING AND CLOSING, THE PLANT RECEIVED A PCI SYSTEM GROUP 3 | | (RWCU SYSTEM) ISOLATION SIGNAL FROM THE REACTOR VESSEL WATER LEVEL DROPPING | | BELOW 9 INCHES. | | | | THE LICENSEE PLANS TO INFORM THE NRC RESIDENT INSPECTOR. | | | | THE NRC OPERATIONS OFFICER NOTIFIED THE R3DO MONTE PHILLIPS. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35695 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/09/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 20:22[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/09/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 16:45[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/09/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MONTE PHILLIPS R3 | | DOCKET: 0707002 |JOHN GREEVES NMSS | +------------------------------------------------+FRANK CONGEL IRO | | NRC NOTIFIED BY: LARSON | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NRC BULLETIN 91-01, 4 HOUR REPORT | | | | AT 1645 ON 05/09/99, DURING A PRESSURE DECAY TEST OF THE #1 AUTOCLAVE IN THE | | X-342 BUILDING, A LIGHT DUSTING OF UO2F2 WAS OBSERVED INSIDE THE AUTOCLAVE | | AND A HEAVIER ACCUMULATION OF UO2F2 WAS OBSERVED ON THE PRESSURE DECAY | | FILTER USED TO PREVENT URANIUM FROM ENTERING THE AUTOCLAVE DURING THIS TEST. | | THE AUTOCLAVE WAS PLACED IN A CONTAINMENT MODE ISOLATING IT FROM ALL SUPPORT | | SYSTEMS. HEALTH PHYSICS TECHNICIANS PERFORMED CONTAMINATION AND AIRBORNE | | SAMPLING AND ALL SAMPLES WERE LESS THAN DETECTABLE LIMITS. HAVING URANIUM | | INSIDE THE SHELL OF THE AUTOCLAVE IS A LOSS OF ONE CONTROL OF THE DOUBLE | | CONTINGENCY PRINCIPLE CONTAINED IN NCSA_342A002. THE ACCUMULATION OF UO2F2 | | ON THE OUTSIDE OF THE PRESSURE DECAY FILTER IS NOT EXPECTED. ADDITIONAL | | EVALUATIONS ARE BEING CONDUCTED AT THIS TIME. | | | | THERE IS NO LOSS OF HAZARDOUS/RADIOACTIVE MATERIAL OR | | RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF THIS EVENT. | | THIS EVENT DOES NOT PRESENT ANY IMMINENT DANGER OF A CRITICALITY. | | | | THE AUTOCLAVE HAS BEEN ISOLATED FROM ALL POTENTIAL MODERATOR SOURCES, SO | | CRITICALITY IS NOT POSSIBLE. MODERATION, ENRICHMENT AND GEOMETRY PARAMETERS | | WERE MAINTAINED THROUGHOUT THIS EVENT. THE UNLIKELIHOOD OF URANIUM INSIDE | | THE AUTOCLAVE SHELL AND OUTSIDE OF THE UF6 CYLINDER WAS A LOST PARAMETER. | | THE AUTOCLAVE WAS TAGGED TO PREVENT ANY OPERATION UNTIL RECOVERY PLANS ARE | | DEVELOPED. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021