Event Notification Report for April 12, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/09/1999 - 04/12/1999 ** EVENT NUMBERS ** 35562 35563 35564 35565 35566 35567 35568 35569 35570 35571 35572 35573 35574 35575 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35562 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BROWNS FERRY REGION: 2 |NOTIFICATION DATE: 04/09/1999| | UNIT: [] [] [3] STATE: AL |NOTIFICATION TIME: 00:51[EDT]| | RXTYPE: [1] GE-4,[2] GE-4,[3] GE-4 |EVENT DATE: 04/08/1999| +------------------------------------------------+EVENT TIME: 20:45[CDT]| | NRC NOTIFIED BY: TIM GOLDEN |LAST UPDATE DATE: 04/09/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WALTER RODGERS R2 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HPCI TEMPORARILY INOPERABLE | | | | System Affected: During the performance of a regularly scheduled | | Instrumentation surveillance on the Unit 3 HPCI Steam Line Space High | | Temperature switches (in accordance with plant procedure 3-SR-3.3.6.1(3D)) | | personnel noticed that a relay not tested by procedure was chattering. The | | affected relay 3-RLY-073-23A-K16 was adjacent to a relay 3-RLY-073-23A-K8 | | which was being tested by the surveillance. While troubleshooting the cause | | of the chattering relay, a loose wire was found in the power supply pathway | | for the HPCI logic circuit. This loose wire had the potential to prevent | | adequate voltage being supplied to the initiation and isolation logic for | | the Unit 3 HPCI system. | | | | Actions: The loose wire was retightened. | | | | Reportability: The potential for inadequate voltage being available for the | | HPCI logic circuit resulted in a conservative decision to declare the HPCI | | system inoperable. In accordance with plant procedure SPP 3.5, code of | | Federal Regulations 10CFR50.72/73 and NUREG 1022 Rev 1 this is reportable as | | a 4 Hour Non-Emergency report due to any event or condition that alone could | | have prevented the Fulfillment of the safety function of structures or | | systems that are needed to (d) Mitigate the consequences of an accident. | | This criteria is specified in 10CFR50.72.b.2.iii as a 4 hour report and in | | 10CFR50.73.a.2.v as a 30 day written report. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35563 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 04/09/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 02:50[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 04/08/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 23:00[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 04/09/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |BRUCE BURGESS R3 | | DOCKET: 0707002 |ROSEMARY HOGAN IRO | +------------------------------------------------+SUSAN SHANKMAN NMSS | | NRC NOTIFIED BY: KEITH VANDERPOOL | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BULLETIN 91-01 REPORT - VIOLATION OF NCSA | | | | "ON 4/8/99, AT 2300 IT WAS DISCOVERED THAT REQUIREMENT #14 OF NCSA-0333_ | | 015.E03 WAS NOT BEING MAINTAINED ON CELL 33-3-8 WITHIN THE X-333 PROCESS | | BUILDING. REQUIREMENT #14 STATES IN PART 'IF THE MOTORS ARE OFF, EITHER | | THE RCW CONTROL VALVE OR THE RCW SUPPLY BLOCK VALVE SHALL BE CLOSED WITHIN 4 | | HOURS.' THE MOTORS WERE IN FACT OFF AND THE RCW CONTROL VALVE FAILED IN | | THE OPEN POSITION AND THE RCW SUPPLY VALVE WAS NOT CLOSED WITHIN 4 HOURS, | | THUS VIOLATING REQUIREMENT #14. VIOLATION OF THIS REQUIREMENT CONSTITUTES | | A LOSS OF CONTROL "B" (MODERATION) IN THE DOUBLE CONTINGENCY MATRIX FOR | | CONTINGENCY EVENT B.6.b.1. CONTROL 'A' WHICH IS THE PASSIVE BARRIER | | PROVIDED BY THE | | CONDENSER AND COOLER TUBES REMAINED IN PLACE THROUGHOUT THIS EVENT. | | CONTROL WAS NOT ESTABLISHED WITHIN THE 4 HOUR SPECIFIED TIME FRAME THUS | | MAKING THIS A 4 HOUR NRC EVENT. CONTROL HAS BEEN ESTABLISHED AND CELL | | 33-3-8 IS NOW ONSTREAM. (MOTORS ON)" | | | | THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35564 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CATAWBA REGION: 2 |NOTIFICATION DATE: 04/09/1999| | UNIT: [1] [2] [] STATE: SC |NOTIFICATION TIME: 05:15[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/09/1999| +------------------------------------------------+EVENT TIME: 04:28[EDT]| | NRC NOTIFIED BY: HOLLAND |LAST UPDATE DATE: 04/09/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WALTER RODGERS R2 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT ENTERED 3.0.3 DUE TO BOTH TRAINS OF CONTROL ROOM VENTILATION BEING | | INOPERABLE. | | | | A SPURIOUS SIGNAL ON THE CHLORINE DETECTOR ON UNIT 1 "B" TRAIN CONTROL ROOM | | VENTILATION INTAKE WAS RECEIVED WHILE UNIT 2 VENTILATION INTAKE WAS CLOSED. | | UNIT 2 CONTROL ROOM INTAKE HAD PREVIOUSLY CLOSED ON A SPURIOUS SIGNAL( SEE | | EVENT 35561) AND IT WAS STILL CLOSED FOR TROUBLESHOOTING. BOTH UNITS | | CONTROL ROOM VENT SYSTEMS BEING CLOSED RESULTS IN THE INOPERABILITY OF BOTH | | TRAINS OF CONTROL ROOM VENTILATION, PLACING BOTH UNITS IN TS 3.0.3. | | | | THE RESIDENT INSPECTOR WILL BE NOTIFIED. | | | | *** UPDATE AT 0530 BY HOLLAND TO GOULD *** | | | | THEY EXITED 3.0.3 AT 0526 WHEN THE "B" TRAIN WAS RESTORED TO OPERABLE | | CONDITION. | | | | THE RESIDENT INSPECTOR WILL BE NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35565 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BEAVER VALLEY REGION: 1 |NOTIFICATION DATE: 04/09/1999| | UNIT: [1] [2] [] STATE: PA |NOTIFICATION TIME: 09:14[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 04/09/1999| +------------------------------------------------+EVENT TIME: 08:37[EDT]| | NRC NOTIFIED BY: DANIEL MURRAY |LAST UPDATE DATE: 04/09/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN KINNEMAN R1 | |10 CFR SECTION: | | |AENS 50.72(b)(1)(v) ENS INOPERABLE | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Standby |0 Hot Standby | |2 N Y 98 Power Operation |98 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EMERGENCY SIRENS INOPERABLE | | | | At 0837, the control room received a report from the Beaver County Emergency | | Management Agency (BCEMA 911 center) that the emergency notification | | sirens for Beaver County were inoperable. The computer that activates the | | sirens was damaged by a lightning strike. This constitutes a major loss of | | emergency communications capability as listed in 10CFR50.72.(b)1.v. Crews | | are working to repair the main (damaged) computer and are also working to | | place the backup computer in service. They expect to have the emergency | | sirens returned to service within 1 hour. | | | | The licensee notified the NRC resident inspector. | | | | *** UPDATE ON 4/9/99 @ 1431 BY SHIPE TO GOULD *** | | | | ALL SIRENS WERE RETURNED TO SERVICE AT 1401. | | | | THE RESIDENT INSPECTOR WILL BE INFORMED. R1DO (KINNEMAN) WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 35566 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MATERIALS TESTING CONSULTANTS |NOTIFICATION DATE: 04/09/1999| |LICENSEE: MATERIALS TESTING CONSULTANTS |NOTIFICATION TIME: 12:14[EDT]| | CITY: GRAND RAPIDS REGION: 3 |EVENT DATE: 04/09/1999| | COUNTY: STATE: MI |EVENT TIME: 09:00[EDT]| |LICENSE#: 21-15281-02 AGREEMENT: N |LAST UPDATE DATE: 04/09/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BRUCE BURGESS R3 | | |SCOTT MOORE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: PETE GASEWICZ | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOST TROXLER MOISTURE/DENSITY GAUGE | | | | A technician, en route to a project site, encountered problems with his | | pickup truck approximately one mile from the company offices. The | | technician was transporting a Troxler model 3430 gauge, containing one 8 mCi | | Cs-137 source and one 40 mCi Am-241/Be source. A second truck was sent to | | retrieve the technician and his equipment. However, when the gauge was | | moved to the second truck, it was not properly secured to the bed of the | | truck, nor was the tailgate raised. Upon arrival at the office, the | | technician discovered that the gauge had fallen from the truck. The | | technician immediately retraced the route of travel, but did not find the | | gauge. The licensee believes that a passing motorist may have picked it up. | | The gauge was locked inside of its storage case at the time of the loss. | | The local police department has been contacted by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35567 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ROCHESTER GAS AND ELECTRIC CORP |NOTIFICATION DATE: 04/09/1999| |LICENSEE: COLTEC INDUSTRIES |NOTIFICATION TIME: 13:50[EDT]| | CITY: ROCHESTER REGION: 1 |EVENT DATE: 04/09/1999| | COUNTY: STATE: NY |EVENT TIME: [EDT]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 04/09/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN KINNEMAN R1 | | |VERN HODGE (FAX) NRR | +------------------------------------------------+ | | NRC NOTIFIED BY: WIDAY (FAX) | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE REPORTED A PART 21 DEFECT ON A REPLACEMENT TURBOCHARGER | | SUPPLIED BY COLTEC INDUSTRIES. | | | | THE LICENSEE REPLACED A TURBOCHARGER(MODEL 730), SUPPLIED BY COLTEC | | INDUSTRIES, ON THEIR "B" EMERGENCY DIESEL GENERATOR (ALCO MODEL 16-251F) AT | | GINNA STATION. IT WAS DETERMINED THAT THERE WAS A MANUFACTURING DEFICIENCY | | IN THE REPLACEMENT TURBOCHARGER WHICH CONSISTED OF A MISSING DRAIN PORT IN | | THE INTERMEDIATE CASING ON THE TURBINE END WHICH WOULD PREVENT ENGINE | | LUBRICATING OIL FROM BEING ABLE TO DRAIN BACK TO THE ENGINE SUMP FROM THE | | TURBOCHARGER SHAFT AND BEARINGS. THIS DEFICIENCY CREATED A CONDITION WHERE | | ENGINE LUBE OIL WAS BEING DIRECTED INTO THE CYLINDERS THROUGH THE EXHAUST | | MANIFOLD PIPING, WHICH COULD HAVE RESULTED IN SERIOUS ENGINE DAMAGE. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35568 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 04/09/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 18:07[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 04/08/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 18:55[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 04/09/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |BRUCE BURGESS R3 | | DOCKET: 0707002 |SUSAN SHANKMAN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: RICK LARSON | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR NRC BULLETIN 91-01 REPORT | | | | "At 1855 on 4/8/99, a Nuclear Criticality Safety Analysis (NCSA) | | PLANT033.A01 control was lost. This loss was of one control (concentration), | | which is one contingency of a double contingency design of this NCSA. | | Moderation was maintained. The concentration control was lost when a surge | | of UF6 material at less than 1% U-235 sublimed from a cell being returned to | | service, causing the pressure in an intermediate drum (a type of surge drum) | | to exceed the NCSA limit of 17 psia. The highest pressure reached was 19.6 | | psia in the drum. Actions were immediately taken to reduce the drum pressure | | and it was returned to allowable limits within 45 minutes. The drum | | temperature was maintained above 220�F during this excursion. | | | | "This is reportable under NRC Bulletin 91-01 24-hour criticality control. | | There was no loss of hazardous/radioactive material or | | radioactive/radiological exposure as a result of this event." | | | | The NRC resident inspector has been informed of this notification. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 35569 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SYNCOR INTERNATIONAL CORPORATION |NOTIFICATION DATE: 04/09/1999| |LICENSEE: SYNCOR INTERNATIONAL CORPORATION |NOTIFICATION TIME: 18:31[EDT]| | CITY: COLUMBUS REGION: 3 |EVENT DATE: 04/08/1999| | COUNTY: STATE: OH |EVENT TIME: 03:30[EDT]| |LICENSE#: 04-26507-01MD AGREEMENT: N |LAST UPDATE DATE: 04/09/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BRUCE BURGESS R3 | | |SUSAN SHANKMAN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: SCOTT LANGFORD | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAE2 20.2202(b)(2) EXCESSIVE RELEASE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF 185 mCi OF Tc-99m | | | | The licensee reported that 185 mCi of Tc-99m (5 unit doses) was lost from | | the Syncor radiopharmacy facility in Columbus, OH. The missing unit doses | | were contained in an ammo can which was one of eight cans in this particular | | shipment. The driver for the shipment stated that only seven cans were | | located on the shelf when he arrived to pick them up; however, another | | driver who had picked his shipment up several minutes before stated that | | there were eight cans located on the shelf when he left the area. | | | | This is an access controlled facility, and the licensee believes that the | | can was either misplaced within the facility, inadvertently delivered to the | | wrong customer, or disposed of as an undeliverable shipment. The licensee | | will submit a written report to the NRC regarding this event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35570 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BEAVER VALLEY REGION: 1 |NOTIFICATION DATE: 04/09/1999| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 18:46[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 04/09/1999| +------------------------------------------------+EVENT TIME: 18:38[EDT]| | NRC NOTIFIED BY: DANIEL MURRAY |LAST UPDATE DATE: 04/09/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN KINNEMAN R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 98 Power Operation |98 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCREPANCIES DISCOVERED IN APPENDIX R PROCEDURES | | | | "A review associated with an Engineering fire protection self-assessment has | | identified discrepancies in manual actions specified in select Unit 1 | | post-fire safe shutdown procedures. Steps in these procedures require | | certain manual actions to be taken that have been determined to be | | inappropriate. Performing these actions could place Unit 1 in a condition | | which is outside the design basis of the Fire Protection Program involving | | Appendix R Safe Shutdown capability. These actions involve manually | | de-energizing non-essential class 1E power circuits. The intent of these | | actions is to turn off circuits that are not required for safe shutdown in | | order to eliminate the potential for circuit faults due to a postulated fire | | that could trip out an entire AC distribution panel. However, performing | | these actions would result in de-energizing the power to the diesel building | | exhaust dampers. It has been determined that the dampers revert to the | | closed position when their power supply is de-energized. This could have | | resulted in the emergency diesel generator operating with insufficient | | ventilation for diesel room cooling. This condition could have prevented the | | fulfillment of the safety function of the emergency diesel generators needed | | to satisfy the Appendix R Safe Shutdown requirements. As a result of these | | procedural deficiencies, the ability to mitigate the consequences of a fire | | event and to place the plant in a safe shutdown condition cannot be | | assured. | | | | "A condition report has been written to document these procedural | | discrepancies. The root cause and corrective actions are being addressed | | through the corrective action program." | | | | The licensee will inform the NRC resident inspector of this notification. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35571 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: YANKEE ROWE REGION: 1 |NOTIFICATION DATE: 04/09/1999| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 19:13[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 04/09/1999| +------------------------------------------------+EVENT TIME: 18:50[EDT]| | NRC NOTIFIED BY: MARK GILMORE |LAST UPDATE DATE: 04/09/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN KINNEMAN R1 | |10 CFR SECTION: | | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Decommissioned |0 Decommissioned | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NUCLEAR ALERT TELEPHONE SYSTEM INOPERABLE | | | | The licensee reported that the Nuclear Alert telephone, which links the | | plant to local police departments, is inoperable. FTS2000 and commercial | | telephone service is unaffected. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35572 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: RIVER BEND REGION: 4 |NOTIFICATION DATE: 04/10/1999| | UNIT: [1] [] [] STATE: LA |NOTIFICATION TIME: 07:46[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 04/10/1999| +------------------------------------------------+EVENT TIME: 03:10[CDT]| | NRC NOTIFIED BY: HUSTON |LAST UPDATE DATE: 04/10/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LAWRENCE YANDELL R4 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ESF SIGNAL INITIATED CAUSING SOME CONTAINMENT ISOLATION VALVES TO CLOSE | | | | "While performing preparations for an ENS-SWG1A bus outage the alternate | | supply breaker ENS-ACB04 tripped. The bus was being supplied by this source | | and the resultant loss of power and invalid actuation signal caused several | | containment isolation AOVs to close. The containment purge system was in | | operation and isolated as designed. Two drain system valves (DFR-AOV102 and | | DER AOV127) and one sample system valve (B33-FO20) also isolated." | | | | The trip took place during a clearance procedure when an individual, in the | | field, opened a fuse cabinet. The incident is being investigated. A | | limited restoration of systems has been done. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35573 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATTS BAR REGION: 2 |NOTIFICATION DATE: 04/11/1999| | UNIT: [1] [] [] STATE: TN |NOTIFICATION TIME: 02:46[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/11/1999| +------------------------------------------------+EVENT TIME: 00:42[EDT]| | NRC NOTIFIED BY: RICK O'REAR |LAST UPDATE DATE: 04/11/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WALTER RODGERS R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R N 0 Hot Standby |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO CONTROL ROD DRIVE MALFUNCTION | | | | "Watts Bar Unit 1 experienced a Manual Reactor Trip during Control Rod | | Testing while in Mode 3 (with Reactor shutdown for Refueling Outage). At | | 0042 on 04/11/1999, the Main Control Room Crew manually opened the | | Reactor Trip Breakers when the Control Rod Drive system continued to | | withdraw Shutdown Bank A following a Manual withdrawal to 10 steps. The | | rods should have stopped at 10 steps withdrawn. This was the first in a | | sequence of rod withdrawals per Surveillance instruction 1-S I-85-2. | | | | "All other rods were fully inserted at the time of testing Shutdown Bank A | | with RCS Boron concentration at 2184 PPM. When Shutdown Bank A continued to | | withdraw, the SRO directed the Reactor Trip breakers to be | | opened and verified all rods fully inserted. All systems responded as | | expected. The Unit remains stable in Mode 3. | | | | "In addition, this generated a Main Feedwater Isolation Signal. At the time | | of the event, all feedwater lines were isolated for outage work. | | | | "At present, an investigation is in progress to determine cause of event and | | Control Rod Testing has been suspended pending outcome of that | | investigation." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35574 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SALEM REGION: 1 |NOTIFICATION DATE: 04/11/1999| | UNIT: [] [2] [] STATE: NJ |NOTIFICATION TIME: 17:52[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/11/1999| +------------------------------------------------+EVENT TIME: 15:54[EDT]| | NRC NOTIFIED BY: PETE JONES |LAST UPDATE DATE: 04/11/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN KINNEMAN R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONTAINMENT VENTILATION ISOLATION | | | | During the process of lifting the reactor vessel head, the containment noble | | gas monitor (2R12A) alarmed, causing a containment ventilation isolation. | | The containment purge isolation valves closed as a result of the isolation. | | Nonessential personnel were immediately evacuated from containment, and all | | remaining personnel (except the crane operator) were evacuated after the | | reactor vessel head was placed onto its stand. The crane operator is | | required to be on station in accordance with station procedures. The | | licensee is analyzing samples taken from the containment atmosphere. The | | NRC resident inspector will be informed of this notification by the | | licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35575 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CATAWBA REGION: 2 |NOTIFICATION DATE: 04/11/1999| | UNIT: [1] [2] [] STATE: SC |NOTIFICATION TIME: 21:13[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/11/1999| +------------------------------------------------+EVENT TIME: 20:21[EDT]| | NRC NOTIFIED BY: GARY HAMILTON |LAST UPDATE DATE: 04/11/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WALTER RODGERS R2 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONTROL ROOM CHILLERS DECLARED INOPERABLE | | | | Both control room ventilation chillers were declared inoperable due to high | | temperature in the Standby Nuclear Service Water pond. The system had been | | operating in an "operable but degraded" condition due to fouling of tubes in | | the chiller condensers. The engineering analysis in support of continued | | system operation specified a maximum Standby Nuclear Service Water pond | | temperature of 70�F (the normal temperature limit for the pond is 91.5�F). | | The licensee is currently attempting to cool the pond, but stated that | | preparations are also being made to commence a dual unit shutdown. The NRC | | resident inspector will be informed of this notification by the licensee. | | | | * * * UPDATE 2148 4/11/1999 FROM HAMILTON TAKEN BY STRANSKY * * * | | | | The licensee commenced shutdowns of both units at 2120. At 2133, the "B" | | control room chiller was restored to operable, and the shutdowns were | | terminated. Reactor power had been decreased to 98%, and is being returned | | to rated. The NRC resident inspector will be informed of this notification | | by the licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021