Event Notification Report for March 1, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 02/26/1999 - 03/01/1999 ** EVENT NUMBERS ** 35407 35409 35410 35411 35412 35413 35415 35416 35417 35418 35419 35420 35421 35422 35423 35424 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35407 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATERFORD REGION: 4 |NOTIFICATION DATE: 02/25/1999| | UNIT: [3] [] [] STATE: LA |NOTIFICATION TIME: 18:41[EST]| | RXTYPE: [3] CE |EVENT DATE: 02/25/1999| +------------------------------------------------+EVENT TIME: 14:18[CST]| | NRC NOTIFIED BY: BILL MCKINNEY |LAST UPDATE DATE: 02/27/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ELMO COLLINS R4 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PRESSURIZER NOZZLE LEAKAGE DISCOVERED DURING REFUELING OUTAGE | | | | During a visual inspection, evidence of reactor coolant system leakage was | | found on two inconel instrument nozzles located on the top head of the | | pressurizer. The leakage was in the annulus area where the nozzle | | penetrates the pressurizer head. The nozzles are welded on the inner | | diameter of the pressurizer and are joined to instrument valves RC-310 and | | RC-311. | | | | The NRC resident inspector has been informed of this notification by the | | licensee. | | | | * * * UPDATE AT 2251 ON 02/27/99 FROM DAVID LITOLFF TAKEN BY STRANSKY * * * | | | | "On 02/25/99 a 4-hour report to the NRC was made per 10CFR50 72(b)(2)(i) for | | evidence of Reactor Coolant System Leakage on two pressurizer instrument | | nozzles. The purpose of this report is to update the 02/25/99 report for | | additional Reactor Coolant System instrument nozzles which have been | | identified as having evidence of RCS leakage. On 02/27/99, evidence of | | boric acid leakage was found on one Hot Leg 1 Inconel Alloy 600 instrument | | nozzle. Potential leakage was also found for one steam generator instrument | | nozzle and the pressurizer side shell nozzle. Any further evidence of | | leakage found in subsequent inspections will be included in the 30-day | | Licensee Event Report." | | | | The NRC resident inspector will be informed of this report by the licensee. | | The NRC Operations Officer notified the R4DO (Chuck Cain). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35409 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 02/26/1999| | UNIT: [1] [] [] STATE: NH |NOTIFICATION TIME: 09:28[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 02/26/1999| +------------------------------------------------+EVENT TIME: 01:22[EST]| | NRC NOTIFIED BY: STEVE MORRISSEY |LAST UPDATE DATE: 02/26/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF A DEAD SEAL IN THE CIRCULATING WATER FOREBAY | | | | The following text is a portion of a facsimile received from the licensee: | | | | "A dead seal was observed in the Seabrook Station's CW (circulating) water | | forebay on February 26, 1999, at about 0122. It is not known whether the | | seal was alive or dead upon entering the offshore intake structure. This | | 24-hour notification is [being] made in accordance with Section 4.1 of the | | Environmental Protection Plan, Appendix 'B' of the Operating License." | | | | The licensee plans to notify the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35410 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 02/26/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 14:09[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 02/26/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 08:45[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 02/26/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |BRUCE JORGENSEN R3 | | DOCKET: 0707001 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: M. UNDERWOOD | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PROCESS GAS LEAK DETECTION SYSTEM INOPERABLE (24-HOUR REPORT) | | | | The following text is a portion of a facsimile received from Paducah: | | | | "On 02/26/99 at 0845 [CST], while performing TSR surveillances on C-333 unit | | 4 cell 10 Process Gas Leak Detection (PGLD), it was discovered that the | | detector heads would not test fire. In the process of evaluating and | | troubleshooting, the PGLD system was placed in a condition (override mode) | | which would have detected a release, but was then placed back in a condition | | (normal mode) in which the PGLD system was inoperable. After approximately | | 90 minutes, the system was returned to an operable condition (override | | mode). The PGLD system is required to be operable when operating above | | atmospheric pressure. C-333 unit 4 cell 10 was operating above atmospheric | | pressure at the time of the failure." | | | | The NRC Resident Inspector has been informed of this notification by Paducah | | personnel. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35411 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OCONEE REGION: 2 |NOTIFICATION DATE: 02/26/1999| | UNIT: [1] [2] [3] STATE: SC |NOTIFICATION TIME: 15:20[EST]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP,[3] B&W-L-L|EVENT DATE: 02/26/1999| +------------------------------------------------+EVENT TIME: 13:00[EST]| | NRC NOTIFIED BY: LARRY NICHOLSON |LAST UPDATE DATE: 02/26/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROBERT HAAG R2 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N N 0 Hot Shutdown |0 Hot Shutdown | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EFW SYSTEM DECLARED OUTSIDE OF DESIGN BASIS | | | | "On February 8, 1999, Duke Energy Corporation (Duke) met with the NRC staff | | at NRC Headquarters to discuss a concern involving the differences in the | | Oconee Emergency Feedwater (EFW) system design and post-TMI licensing basis | | associated with the mitigation of certain Main Feedwater break scenarios. | | The plant design utilizes the availability of EFW from any unit should the | | affected unit's EFW system be lost during a Main Feedwater line break. In | | response, an NRC letter, dated February 24, 1999, agreed that the issue did | | not constitute a significant safety concern and provided an NRC | | interpretation that the reliance of alternate EFW sources, except for | | certain approved exceptions, was not consistent with the current licensing | | basis. | | | | "The specific concern involves the failure to close of the upper surge tank | | to hotwell makeup valve (C-187) following a main feedwater line rupture, | | resulting in the depletion of the upper surge tank and subsequent loss of | | EFW on the affected unit. Should this occur, operators would restore | | feedwater by either cross-connecting EFW to one of the other units or | | starting the Standby Shutdown Facility Auxiliary Service Water pump. These | | alternate sources are designed and capable of supplying feedwater to the | | affected unit. Operators are trained and procedures are established to | | accomplish these tasks. | | | | "On February 26, 1999, following review of the NRC letter, it was determined | | that the differences in the Oconee Emergency Feedwater (EFW) system design | | and post-TMI licensing basis regarding mitigation of certain Main Feedwater | | break scenarios, concurrent with a single active failure, constituted a | | condition outside the licensing basis of the plant. This condition does not | | constitute a safety concern due to the availability of multiple, diverse | | sources of feedwater. The EFW system is considered operable but in | | non-conformance with the licensing basis as stated in the UFSAR. Duke is | | evaluating options to resolve the subject UFSAR discrepancy." | | | | The NRC resident inspector has been informed of this notification. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 35412 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MAYO CLINIC |NOTIFICATION DATE: 02/26/1999| |LICENSEE: MAYO FOUNDATION |NOTIFICATION TIME: 16:22[EST]| | CITY: ROCHESTER REGION: 3 |EVENT DATE: 02/18/1999| | COUNTY: STATE: MN |EVENT TIME: 12:00[CST]| |LICENSE#: 22-00519-03 AGREEMENT: N |LAST UPDATE DATE: 02/26/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BRUCE JORGENSEN R3 | | |JOHN HICKEY NMSS | +------------------------------------------------+KEVIN RAMSEY (fax) NMSS | | NRC NOTIFIED BY: RICHARD VETTER |RICHARD BARKLEY R1 | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 10 CFR PART 21 REPORT - TREATMENT SOFTWARE ERROR CAUSED MEDICAL | | MISADMINISTRATION | | | | The licensee reported that a medical misadministration occurred on 2/18/1999 | | due to a problem with treatment planning software (TCP Version 1.20 upgrade) | | provided by Nucletron of Columbia, Maryland. The misadministration was | | identified on 2/25/1999 and verified on 2/26/1999. Specifically, a patient | | was prescribed a dose of 4500 rads by external beam; however, due to a | | problem with the treatment software, the patient was also given a dose of | | 200 rads to the area from a high dose rate brachytherapy unit. The patient | | and the referring physician have both been informed of the | | misadministration. | | | | The licensee submitted the following information in accordance with 10 CFR | | Part 21: | | | | "Identification of the facility, the activity, or the basic component: | | High dose rate afterloader treatment (Ir-192 microselectron HDR V2) | | Device software (TCS Version 1.20 upgrade) | | | | "Identification of the firm supplying the basic component which failed to | | comply: | | Nucletron, Columbia, MD | | | | "Nature of the failure and safety hazard that could be created: | | The software allows more than one active cell on a treatment planning | | sheet. | | | | "This allows parameters within another cell to be modified while not working | | in that cell. In this case, dwell time and step size were simultaneously | | active. While purposely intending to change dwell time, step size can change | | without alerting the user. This could result in a possible therapy | | misadministration under 10CFR35. | | | | "Date on which information of defect was obtained: | | February 25, 1999 | | | | "Number and location of all such components: | | Mayo Foundation has only one such device. It is located in the Charlton | | Building, Room CHS-209. Nucletron can supply information regarding other | | facilities using the device. | | | | "Corrective action: | | Mayo Foundation modified its procedures to require a pretreatment check that | | includes step size; this action has been completed. All individuals who | | manually enter treatment data will be made aware of the defect and told to | | visually confirm their entries prior to printing the pretreatment report; | | this action will be completed by Tuesday, March 2, 1999. | | | | "On Friday, February 26, Mayo Foundation notified Nucletron of the anomaly | | suggesting they correct their computer software." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35413 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 02/26/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 16:38[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 02/25/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 16:15[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 02/26/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |BRUCE JORGENSEN R3 | | DOCKET: 0707001 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: J. M. UNDERWOOD | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR NRC BULLETIN 91-01 REPORT | | | | "Potentially fissile trap media was discovered in an approximately 30 gallon | | trash can in violation of NCSA GEN-15. NCSA GEN-15 requires that | | fissile/potentially fissile waste be accumulated in a maximum 5.5-gallon | | waste drum. The only exception is if the waste is exempted from NCS controls | | in accordance with requirement 2 of NCSA GEN-15. However, the trap media was | | not exempted prior to disposal. | | | | "The waste was generated prior to implementation of NCSA GEN-1 5 and is | | therefore a legacy issue; however, NCSA GEN-15 is the currently approved | | NCSA for the generation and handling of potentially fissile waste. | | | | "This event is being categorized as a 24-hour event in accordance with | | Safety Analysis Report Table 6.9-1 Criteria A.4.a and NRC Bulletin 91-01, | | Supplement 1 report. | | | | "SAFETY SIGNIFICANCE OF EVENTS: | | | | "This violation resulted in the loss of one leg of double contingency. | | Although double contingency was not maintained, there was not enough | | material present to result in a critical configuration. | | | | "POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO[S] OF HOW | | CRITICALITY COULD OCCUR): | | | | The trash can contained approximately 15 gallons of contaminated alumina. | | Based upon data from KY/S-208, Subcritical Dimensions For Water Reflected | | UO2F2 and Water Systems at Two Weight Percent Enrichment, at 2.0 wt % U-235, | | the safe volume of UO2F2 solution is 23 gallons. Additionally, KY/S-208 | | modeled optimal concentration UO2F2 solution in a spherical geometry | | reflected with 30 cm of water. The trash can contains trap material | | intermixed with the UO2F2, and the material is not in the optimum | | configuration modeled in KY/S-208, therefore, in reality it would take much | | more than 23 gallons to achieve a critical configuration. Based upon this | | information, a criticality is not possible. | | | | "In order for a criticality to be possible much more than 23 gallons of the | | trap material would have to be present In the trash can. | | | | "CONTROLLED PARAMETERS (MASS, MODERATION. GEOMETRY, CONCENTRATION, ETC.): | | | | "Controlled parameters are geometry and spacing. | | | | "ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE OF CRITICAL MASS): | | | | "The trash can contained approximately 15 gallons of contaminated alumina at | | a maximum assay of 1.04 wt % U235. | | | | "In order for a criticality to be possible, much more than 23 gallons of the | | trap material would have to be present in the trash can. | | | | "The determination that the material in the drum was fissile is based on | | conservative sample results. Two independent smears and two independent bulk | | samples were taken and analyzed. One of the bulk sample results indicated an | | assay of .944% U-235. All of the remaining sample results were below 9%. A | | .1% error is conservatively applied to lab sample results as a general rule | | to account for uncertainties. Much lower uncertainties are routinely | | achieved but have not been established far these samples at this time. This | | Incident Report conservatively assumes the material in the drum is fissile | | based on the .1% error applied to the one sample result above .9% U-235. | | | | "NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES: | | | | "Loss of spacing control. Double contingency control leg was lost since | | geometry process condition was not maintained. | | | | "CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED: | | | | "The trap media will be disposed of in a minimum 5.5 gallon drum in | | accordance with plant procedure CP2-EW-WM1036. | | | | "A minimum 6 ft. spacing is being maintained between the cold trap and the | | container of contaminated trap media. A minimum 2 ft. spacing will be | | maintained between the maximum 5.5 gallon waste drum containing the trap | | media and all other fissile/potentially fissile material." | | | | The NRC resident inspector has been informed of this notification. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 35415 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SAN DIEGO MEDICAL CENTER |NOTIFICATION DATE: 02/26/1999| |LICENSEE: VA MEDICAL SYSTEM |NOTIFICATION TIME: 17:31[EST]| | CITY: SAN DIEGO REGION: 4 |EVENT DATE: 02/26/1999| | COUNTY: STATE: CA |EVENT TIME: 08:10[PST]| |LICENSE#: 04-15030-01 AGREEMENT: Y |LAST UPDATE DATE: 02/26/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ELMO COLLINS R4 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MIKE ZORN | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAAA 20.1906(d) SURFACE CONTAMINATION E| | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PACKAGE RECEIVED WITH SURFACE CONTAMINATION ABOVE LIMITS | | | | At 0810 PST, a courier delivered a shipment of radiopharmaceuticals from the | | SYNCOR pharmacy in San Diego, CA. Upon receipt, the licensee performed a | | routine wipe sample of the external surfaces of the outer container (ammo | | box), and discovered contamination in excess of the reporting requirements | | of 10 CFR 20.1906. Initial wipes indicated up to 30,000 CPM of gross | | activity for a swab that had been run over all surfaces of the container. | | The package contained two vials of radiopharmaceuticals; 10 mCi of Tc-99m | | META solution, and 10 mCi of Ga-67 (not NRC regulated). The licensee did | | not report any damage to the vials, and they were administered to patients. | | No contamination occurred at the medical center as a result of this | | shipment. | | | | A more detailed survey of the container revealed up to 50,000 cpm/300cm2. | | The licensee did not determine the isotope of the contaminant. A | | representative of SYNCOR visited the medical center, and took several wipe | | samples for isotopic identification. The licensee plans to investigate this | | event with SYNCOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35416 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 02/27/1999| | UNIT: [] [2] [] STATE: MI |NOTIFICATION TIME: 00:31[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 02/26/1999| +------------------------------------------------+EVENT TIME: 21:30[EST]| | NRC NOTIFIED BY: BRIAN MUTZ |LAST UPDATE DATE: 02/27/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE JORGENSEN R3 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - Potentially excessive thermal stress on two containment penetrations due | | to blocked cooling flow - | | | | At 2130 on 02/26/99, with Unit 2 in cold shutdown mode in a refueling | | outage, the Licensee determined that on 08/02/96, with Unit 2 at 100% power, | | a temporary plant modification was implemented on Unit 2 which allowed for | | continued power operation with component cooling water (CCW) to containment | | penetrations #CPN-3 and #CPN-4 isolated. These penetrations contain the | | steam generator #2 and #3 main steam headers. This condition is reportable | | under 10CFR50.72(b)(2)(i) as an event found while the reactor is shutdown, | | that, had it been found while the reactor was in operation, would have | | resulted in the nuclear power plant, including its principal safety | | barriers, being in a seriously degraded condition that significantly | | compromised plant safety. The component cooling water return header | | upstream of the containment isolation valve, #2-CCR-441, (containment | | penetrations #CPN-3 and #CPN-4 inner cooling coils CCW outlet containment | | isolation valve) was discovered to contain blockage during a post | | maintenance activity associated with the repair of valve #2-CCR-441. The | | blocked line eliminated cooling flow to the penetration inner coolers, which | | is designed to assure integrity of the penetration sleeve. The result of | | operating with the CCW isolated to penetrations #CPN-3 and #CPN-4 was the | | creation of potentially excessive thermal stress on the penetration sleeves. | | Design basis information indicates that the penetration sleeve may be | | exposed to temperatures of as high as 150�F without experiencing | | degradation. It is estimated that the penetration sleeves on penetrations | | #CPN-3 and #CPN-4 were operated at a temperature approximating main steam | | temperature of approximately 600�F. | | | | This condition was identified during an expanded system readiness review. | | No immediate corrective action is planned since the main steam system is | | currently out of service and containment integrity is not required in the | | current operational mode. Further analysis and corrective action will be | | considered during ongoing investigation under the corrective action | | program. | | | | The Licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35417 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CRYSTAL RIVER REGION: 2 |NOTIFICATION DATE: 02/27/1999| | UNIT: [3] [] [] STATE: FL |NOTIFICATION TIME: 09:07[EST]| | RXTYPE: [3] B&W-L-LP |EVENT DATE: 02/27/1999| +------------------------------------------------+EVENT TIME: 08:10[EST]| | NRC NOTIFIED BY: LARRY MOFFATT |LAST UPDATE DATE: 02/27/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROBERT HAAG R2 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - STATE NOTIFIED OF A KEMP'S RIDLEY SEA TURTLE RETRIEVED FROM THE PLANT | | INTAKE WATER - | | | | At 2232 on 02/26/99, a young Kemp's Ridley sea turtle was taken from the | | water at the intake of Crystal River Unit 3. The turtle was found pinned | | against the bar rack and was retrieved by site personnel in accordance with | | the Florida Power Corporation Turtle Protection Guidelines. Crystal River | | Mariculture Center personnel took custody of the sea turtle and will return | | it to the Gulf of Mexico In the afternoon of 02/27/99. At 0810 on 02/27/99, | | the Florida Department of Environmental Protection was notified of the | | retrieval of the sea turtle. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35418 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 02/27/1999| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 13:37[EST]| | RXTYPE: [1] W-2-LP |EVENT DATE: 02/27/1999| +------------------------------------------------+EVENT TIME: 11:39[EST]| | NRC NOTIFIED BY: DOUGLAS GOMEZ |LAST UPDATE DATE: 02/27/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 70 Power Operation |70 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONTAINMENT VENTILATION ISOLATION DURING I&C WORK ON RADIATION MONITOR | | | | "During Instrument and Control (I/C) activities on radiation channel R-12, | | an unexpected Containment Ventilation Isolation (CVI) occurred. The planning | | activities for this maintenance recognized the potential of generating a CVI | | signal and directed the technicians to install a jumper to prevent the | | actuation. Even with the jumper installed an unexpected CVI occurred when | | the R-12 drawer was deenergized. The CVI was therefore due to maintenance | | activities and was not the result of an actual high radiation condition. | | | | "No plant system other than the containment ventilation monitoring system | | was affected by this event. The plant is stable at approximately 70% power | | with a plant coastdown in progress. | | | | "This event is reportable under lOCFR50.72(b)(2)(ii), 'Any condition that | | results in a manual or automatic actuation an Engineered Safety Feature.'" | | | | The NRC resident inspector has been informed of this notification. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35419 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 02/27/1999| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 22:39[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 02/27/1999| +------------------------------------------------+EVENT TIME: 21:56[EST]| | NRC NOTIFIED BY: STEVE CAROLIN |LAST UPDATE DATE: 02/27/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |AINT 50.72(b)(1)(vi) INTERNAL THREAT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |65 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FIRE ONSITE LASTING LESS THAN 10 MINUTES | | | | At 2156, the 'A' circulating water pump tripped, and the control room | | received indication of a fire in the pump motor. The onsite fire brigade | | responded, and the fire was extinguished at 2204. The licensee reported | | that the pump motor does not appear to be extensively damaged, and that no | | other equipment was involved in the fire. Reactor power was reduced to 65% | | of rated due to the unavailability of the circulating water pump. No | | personnel injuries were reported. | | | | The licensee will inform the NRC resident inspector of this event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35420 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SALEM REGION: 1 |NOTIFICATION DATE: 02/28/1999| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 02:55[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 02/28/1999| +------------------------------------------------+EVENT TIME: 01:38[EST]| | NRC NOTIFIED BY: JACK GRANT |LAST UPDATE DATE: 02/28/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 60 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - AUTO Rx TRIP FROM 60% DUE TO MAIN TURBINE TRIP DUE TO LOW AUTO STOP OIL | | PRESSURE - | | | | AT 0130 ON 02/28/99, THE UNIT 1 REACTOR AUTO TRIPPED FROM 60% POWER DUE TO A | | MAIN TURBINE TRIP (WITH REACTOR POWER ABOVE THE P-9 SETPOINT OF 50% POWER) | | DUE TO LOW AUTO STOP OIL PRESSURE. ALL CONTROL RODS INSERTED COMPLETELY. | | THE AUXILIARY FEEDWATER SYSTEM AUTO STARTED TO MAINTAIN STEAM GENERATORS AT | | NORMAL WATER LEVELS. NO SAFETY OR RELIEF VALVES LIFTED AND STEAM IS BEING | | DUMPED TO THE MAIN CONDENSER. UNIT 1 IS STABLE IN MODE 3 (HOT STANDBY). | | THE LICENSEE IS INVESTIGATING THE CAUSE OF THE LOW AUTO STOP OIL PRESSURE. | | | | THE LICENSEE PLANS TO INFORM THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35421 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: VOGTLE REGION: 2 |NOTIFICATION DATE: 02/28/1999| | UNIT: [1] [] [] STATE: GA |NOTIFICATION TIME: 03:14[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 02/27/1999| +------------------------------------------------+EVENT TIME: 23:40[EST]| | NRC NOTIFIED BY: CHUCK MEYER |LAST UPDATE DATE: 02/28/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROBERT HAAG R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 18 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | -MAN Rx TRIP FROM 18% DUE TO NUCLEAR INSTRUMENTS ANOMALY DURING PLANT | | SHUTDOWN- | | | | WHILE SHUTTING UNIT 1 DOWN FOR A PLANNED REFUELING OUTAGE, CONTROL ROOM | | OPERATORS MANUALLY TRIPPED UNIT 1 FROM 18% POWER DUE TO A CONCERN THAT THE | | NUCLEAR INSTRUMENTS INTERMEDIATE RANGE FLUX TRIP WOULD NOT RESET BEFORE THE | | POWER RANGE (P-10) AUTO UNBLOCK OCCURRED. ALL CONTROL RODS INSERTED | | COMPLETELY. NO SAFETY OR RELIEF VALVES LIFTED. CONTROL ROOM OPERATORS | | MANUALLY ACTUATED THE AUXILIARY FEEDWATER SYSTEM TO MAINTAIN STEAM | | GENERATORS AT THEIR NORMAL WATER LEVELS. UNIT 1 IS STABLE IN MODE 3 (HOT | | STANDBY). THE LICENSEE PLANS TO INVESTIGATE THE CAUSE OF THE NUCLEAR | | INSTRUMENTS ANOMALY AND PROCEED WITH THE PLANNED REFUELING OUTAGE. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35422 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: KEWAUNEE REGION: 3 |NOTIFICATION DATE: 02/28/1999| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 18:41[EST]| | RXTYPE: [1] W-2-LP |EVENT DATE: 02/28/1999| +------------------------------------------------+EVENT TIME: 16:50[CST]| | NRC NOTIFIED BY: CRAIG BYALL |LAST UPDATE DATE: 02/28/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE JORGENSEN R3 | |10 CFR SECTION: | | |AUNA 50.72(b)(1)(ii)(A) UNANALYZED COND OP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 97 Power Operation |97 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT PLACED IN UNANALYZED CONDITION DUE TO CLOSURE OF CONTAINMENT ISOLATION | | VALVE | | | | At 0400 CST on 02/28/99, the plant was incorrectly placed in an unanalyzed | | condition when a manual valve between the reactor coolant drain tank and the | | chemical volume control holdup tank was closed. This manual valve was | | located downstream of two containment isolation valves that had failed | | timing tests, and the manual valve was being relied upon to maintain | | containment integrity in accordance with NRC Generic Letter 96-06. However, | | when the manual valve was closed, overpressure protection for that line was | | lost. The valve subsequently was reopened, restoring the penetration at | | 0800 CST on 02/28/99. The reportability of this condition was identified at | | 1650 CST. The NRC resident inspector has been informed of this | | notification. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35423 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 02/28/1999| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 22:54[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 02/28/1999| +------------------------------------------------+EVENT TIME: 22:00[EST]| | NRC NOTIFIED BY: DAVID WALSH |LAST UPDATE DATE: 02/28/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | |AINB 50.72(b)(2)(iii)(B) POT RHR INOP | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT OUTSIDE OF DESIGN BASIS DUE TO SHEARED VALVE STEM IN RHR SYSTEM | | | | "On 2/11/99 the Unit 1 'B' RHR Loop was removed from service for a scheduled | | maintenance work window. During the system restoration at 2330 Hrs, it was | | identified that the keepfill system did not respond as expected. An | | investigation into the degraded keepfill condition was initiated. An | | Operability Determination was performed and it was determined that the RHR | | system was operable with the degraded keepfill system. | | | | "On 2/16/99 at 0400 hrs, the Unit 1 'A' RHR Loop was removed from service to | | perform a scheduled maintenance work window. The 'A' RHR Loop was returned | | to service at 2115 hrs on 2/16/99 and is currently operable. | | | | "On 2/26/99, after further trouble shooting of the degraded keepfill | | condition on the 'B' RHR Loop it was determined that the most likely cause | | was the RHR Loop 'B' Injection Flow Control Valve, HVI51F017B, being failed | | closed. The 'B' RHR Loop was declared inoperable at 1600 Hrs on 2/26/99. The | | valve was inspected and found to have the stem sheared from the disk. | | Following a review of the time line of the events, it was identified that | | both the 'A' and 'B' RHR Loops were inoperable from 0400 hrs to 2115 hrs on | | 2/16/99 during the scheduled maintenance work windows for the 'A' RHR Loop. | | | | "This report is being made due to the Plant being Outside of the Design | | Basis requiring a 1 Hr ENS Notification under 10CFR50.72(b)(1)(ii)(B) and a | | Loss of a Safety System requiring a 4 Hr ENS notification under | | 1OCFR50.72(b)(2)(iii)(B)." | | | | The NRC resident inspector has been informed of this notification. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35424 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OCONEE REGION: 2 |NOTIFICATION DATE: 03/01/1999| | UNIT: [] [2] [] STATE: SC |NOTIFICATION TIME: 00:17[EST]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP,[3] B&W-L-L|EVENT DATE: 02/28/1999| +------------------------------------------------+EVENT TIME: 20:40[EST]| | NRC NOTIFIED BY: MIKE HILL |LAST UPDATE DATE: 03/01/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROBERT HAAG R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 98.5 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | -AUTO Rx TRIP ON HIGH RCS PRESSURE DUE TO MAIN TURBINE CONTROL VALVES | | FAILING CLOSED- | | | | At 1609 on 02/28/99, the Unit 2 electro-hydraulic control system lost | | various power supplies. Main steam pressure increased from a normal 900 psig | | to 942 psig and reactor power increased from 100% to 100.4%. The main | | turbine control valves had throttled closed for unknown reasons causing the | | main steam pressure to increase. Main feedwater was throttled to reduce | | main steam header pressure since the turbine header pressure control station | | had no effect. Unit 2 was stabilized at 98.5% power with the main steam | | pressure at 938 psig and the main feedwater master control stations and the | | reactor control station in manual. | | | | At 2040 on 02/28/99, Unit 2 automatically tripped from 98.5% power due to a | | reactor protection system actuation (reactor coolant system high pressure | | trip). All control rods inserted completely. The main steam code safety | | valves lifted to dump steam to the atmosphere for approximately 10 minutes. | | Plant operators verified that the valves reseated properly. Steam is being | | dumped to the main condenser. The main feedwater system remained | | operational throughout the event. The reactor control station was in | | automatic at the time of the trip. Unit 2 is stable in hot shutdown mode. | | | | The licensee is investigating the cause of the main turbine control valves | | failing closed and plans to make necessary repairs. | | | | Units 1 and 3 remain at 100% power and were unaffected by this event. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021