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Event Notification Report for January 23, 1999

U.S. Nuclear Regulatory Commission
Operations Center

EVENT REPORTS FOR
01/22/1999 - 01/23/1999

EVENT NUMBERS
3531035311
Power Reactor
Event Number: 35310
Facility: BRUNSWICK
Region: 2     State: NC
Unit: [1] [] []
RX Type: [1] GE-4,[2] GE-4
NRC Notified By: DAVE JENKINS
HQ OPS Officer: LEIGH TROCINE
Notification Date: 01/23/1999
Notification Time: 09:50 [ET]
Event Date: 01/23/1999
Event Time: 06:38 [EST]
Last Update Date: 01/23/1999
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(ii) - ESF ACTUATION
Person (Organization):
CHRIS CHRISTENSEN (R2)
BRIAN BONSER (R2)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 M/R Y 25 Power Operation 0 Hot Shutdown
Event Text
PRIMARY CONTAINMENT ISOLATIONS FOLLOWING A MANUAL REACTOR SCRAM FROM 25% POWER DUE TO LOWERING TEMPERATURE IN THE BOTTOM HEAD REGION OF THE REACTOR PRESSURE VESSEL DURING SINGLE REACTOR RECIRCULATION LOOP OPERATION

The following text is a portion of a facsimile received from the licensee:

"EVENT: On January 23, 1999, at 06:38, primary containment groups 2, 6, and 8 isolations were received following a manual reactor scram. The reactor scram was inserted on Unit 1 due to lowering temperature in the bottom head region of the reactor pressure vessel during single reactor recirculation loop operation. The cooldown was augmented by recirculation pump runback to 28% demand (expected action at low power due to total feedwater flow) which reduced circulation through the vessel. A technical specification shutdown was not required due to bottom head temperature at the time of the reactor scram. Following the manual reactor scram, reactor water level lowered to 160 inches. This is below the Reactor Water Level Low Level One setpoint of 166 inches. This is a normal level transient following a reactor scram and was anticipated by the operating crew. Although these isolations were anticipated by the operating crew, they were not explicitly discussed prior to the reactor scram; therefore, this report is being made in accordance with 10 CFR 50.72(b)(2)(ii). All required isolations occurred as a result of the Reactor Water Level Low Level One initiation signal. Reactor water level immediately swelled above the Low Level One setpoint. Group 2 isolation valves include drywell equipment and floor drains, traversing incore probe, residual heat removal (RHR) discharge isolation to radwaste, and RHR process sampling valves. Group 6 isolation valves include containment atmosphere control system and post-accident monitoring valves. Group 8 isolation valves include RHR system shutdown cooling isolation valves; these valves were closed prior to the isolation signal."

"INITIAL SAFETY SIGNIFICANCE EVALUATION: Minimal. All systems responded as designed from the Reactor Water Level Low Level One initiation signal."

"CORRECTIVE ACTION(S): Isolations occurred as designed; no corrective actions [are] required."

The licensee stated that Technical Specification 3.4.9, Reactor Coolant System Pressure and Temperature Limits - Normal Operation With the Core Critical, specifies minimum temperatures while critical. If parameters go outside these references limits, this technical specification requires the parameters to be restored within 30 minutes. With temperature lowering in the bottom head region, the licensee chose to manually scram the reactor to restore the parameter before expiration of the 30-minute limiting condition for operation.

All rods fully inserted following the manual reactor scram. There were no emergency core cooling actuations or safety injections, and none were expected. None of the relief valves lifted.

The unit is currently stable in Mode 3 (Hot Shutdown). Normal feedwater is being used to supply water to the reactor vessel. The main steam isolation valves are open, the turbine stop and control valves are closed, and the condenser is available as a heat sink. All containment parameters appear to be normal. Offsite power is available, and the emergency diesel generators are operable if needed.

NOTE: Prior to this event, the unit was operating at reduced power to facilitate the performance of a recirculation
pump motor-generator set brush replacement.

The licensee notified the NRC resident inspector.


Power Reactor
Event Number: 35311
Facility: BEAVER VALLEY
Region: 1     State: PA
Unit: [1] [] []
RX Type: [1] W-3-LP,[2] W-3-LP
NRC Notified By: TOM COTTER
HQ OPS Officer: JOHN MacKINNON
Notification Date: 01/23/1999
Notification Time: 12:43 [ET]
Event Date: 01/23/1999
Event Time: 10:24 [EST]
Last Update Date: 01/23/1999
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(ii) - ESF ACTUATION
Person (Organization):
FRANK COSTELLO (R1)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 M/R Y 73 Power Operation 0 Hot Standby
Event Text
DURING POWER REDUCTION, THE REACTOR WAS MANUALLY TRIPPED DUE TO LOW CONDENSER VACUUM.

Prior to this event, one of four condenser waterbox sections was removed from service for tube cleaning, and reactor power was increased from 90% to approximately 92% power. At 0916 EST, a low condenser vacuum alarm was received at which time the licensee commenced a power reduction. During power reduction, condenser parameters continued to degrade due to circulating water system air intrusion from a leaking isolation valve. The reactor was manually tripped from approximately 73% power due to the degradation of the condenser system. All rods fully inserted into the reactor core, and all systems operated as expected. Both the motor-driven and turbine-driven auxiliary feedwater pumps automatically started on low-low steam generator water level. None of the power-operated relief valves on the primary or secondary side of the plant opened. Decay heat from the primary system of the plant is being dumped to the main condenser. (The main condenser can handle the decay heat loads.) Both the motor-driven and turbine-driven feedwater pumps were secured after main feedwater was restored to service. The electrical grid is stable, and all the emergency core cooling systems are fully operable is needed.

The NRC resident inspector was notified of this event by the licensee.