Information Notice No. 84-81: Inadvertent Reduction in Primary Coolant Inventory in Boiling Water Reactors During Shutdown and Startup
SSINS No.: 6835 IN 84-81 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C. 20555 November 16, 1984 Information Notice No. 84-81: INADVERTENT REDUCTION IN PRIMARY COOLANT INVENTORY IN BOILING WATER REACTORS DURING SHUTDOWN AND STARTUP Addressees: All boiling water reactor (BWR) facilities holding an operating license (OL) or construction permit (CP). Purpose: This information notice is being provided to inform licensees of a potentially significant problem pertaining to the inadvertent reduction of reactor pressure vessel (RPV) coolant inventory at BWRs. It is expected that recipients will review this notice for applicability to their facilities and consider actions, if appropriate, to preclude a similar problem from occurring at their facilities. However, suggestions contained in this information notice do not constitute NRC requirements; therefore, no specific action or written response is required. Description of Circumstances: There have been five relatively recent events at BWR facilities involving reductions of RPV inventory while the reactor was shut down or starting up. Washington Nuclear Power Unit 2 On August 23, 1984, Washington Nuclear Power Unit 2 (WNP-2) experienced a loss of 25 inches of RPV coolant inventory through the residual heat removal (RHR) system to the radwaste system. The reactor was going to cold shutdown from low power (~l%). While warming the B loop of the RHR system for shutdown cooling, the shutdown cooling isolation valve closed because of a shutdown line high-flow signal. Because it was not alarmed in the control room, this condition was not noticed for about 15 minutes while the isolated line continued to drain to the radwaste system. When the valve was reopened, 25 inches of RPV inventory drained into the evacuated RHR line. The drop in RPV level was noticed by the operator, who reclosed the suction valve. The reactor protective system (RPS) initiated a scram and the primary containment isolation system (PCIS) isolated the RHR system with the vessel level at +12.5 inches. This is approximately 174 inches above the top of the core. The loop was refilled and warmup was continued. A plant modification was made to provide audible annunciation in the control room of the closure of the isolation valves. . IN 84-81 November 16, 1984 Page 2 of 4 On August 7, 1984, WNP-2 was starting up with the RPV at 400 psig and feedwater flow not yet established with a condensate booster pump. The main steam line drains were opened to the main condenser and RPV level decreased to +13 inches in about 15 minutes. RPS and PCIS initiated to terminate the event. The drain lines were closed and RPV level was restored. A caution statement was added to the minimum startup checklist to prevent opening a steam line flow path before establishing feedwater flow via the condensate system. LaSalle Unit 1 On June 11, 1982, LaSalle 1 experienced a loss of approximately 3,000 gallons of RPV inventory to RHR piping. LaSalle 1 had an unirradiated core and was in initial startup. The B loop of the RHR system was aligned in the shutdown cooling mode and the A loop was in the standby mode. While performing a local leak rate test on the A loop drywell spray outboard isolation valve, a portion of RHR piping was drained. When the test was completed and the RHR A loop was returned to the standby mode, water from the RPV drained into the RHR piping. The RPS initiated a scram at a vessel level of +12.5 inches, and the PCIS isolated the RHR system. Makeup water was then supplied to the A loop from condensate and the B loop was verified filled and vented. The scram and isolations were reset. The procedures for the initiation of shutdown cooling were rewritten to include cautions for the operator concerning level fluctuations. On September 14, 1983, while LaSalle 1 was in cold shutdown and performing an RHR system relay logic test on the B loop, 50 inches of RPV inventory was drained to the suppression pool. To align the RHR system for the test, several valves were open: both drywell spray valves, the suppression pool spray valve, the test return to suppression pool valve, and the C loop injection valve. When the B loop injection valve was opened to perform the test, the only remaining valve available to isolate the RPV was a testable check valve. This valve was held open because its actuator was misassembled and, furthermore, its shaft packing gland was too tight to have permitted closure. The RPS and PCIS initiated at +12.5 inches to terminate the event, but the vessel level went from +50 inches to O inch (161.5 inches above the top of the active fuel). Several corrective actions were taken by the licensee. The inoperable testable check valve was repaired and other testable check valves in the RHR, low pressure core spray, high pressure core spray, and reactor core isolation cooling systems were checked. Post maintenance local leak rate testing was performed as needed. The test procedures were modified to require the manual stop valve to be closed for the loop in test. . IN 84-81 November 16, 1984 Page 3 of 4 Brunswick Unit 2 On September 24, 1984, an integrated containment leak rate test was being performed on Brunswick 2. Some RPV inventory was lost during an attempt to lower torus water level. The RHR system was aligned in the shutdown cooling mode with the RPV refueled and reassembled following a 5-month refueling and maintenance outage. An operator opened a drain path from the RHR system to the radwaste system thinking that RHR was in the torus cooling mode. Instead of draining water from the torus as intended, the RPV was partially drained. The RPS and PCIS initiated to terminate the event. The licensee altered the procedures for the integrated containment leak rate test to require additional operator monitoring during a containment test. Discussion: This information notice details five events in which RPV inventory was partially drained through various systems--primarily because the procedures focused on the system being tested without proper consideration for the plant as a whole.* The RPS and PCIS functioned, as designed, to terminate the events. However, the events were unnecessary challenges to safety systems. In addition, General Electric Company's SIL No. 388, "RHR Valve Misalignment During Shutdown Cooling Operation for BWRs 3/4/5 and 6," February 1983, addresses possible misalignments of the RHR system that could lead to a reduction in RPV coolant inventory. The potential for partially draining the RPV exists with all water systems connected directly or indirectly to the RPV. Barriers exist to prevent a loss of RPV inventory to systems not designed or intended to receive it. In most cases, the system functions automatically to prevent a breach of these barriers, but a system that is largely manually operated, such as RHR, depends heavily on accurate procedures and appropriate operator actions. Licensees may wish to review their procedures and training programs in view of the events and corrective actions discussed above and the information provided in the General Electric SIL. * One of these events also involved an improperly maintained testable check valve actuator. Several other instances of improperly maintained testable check valve actuators have recently occurred at BWRs. Information Notice 84-74, dated September 28, 1984, describes some of these events in light of the concern with overpressurizing low-pressure systems connected to the primary coolant system. . IN 84-81 November 16, 1984 Page 4 of 4 No specific action or written response is required by this information notice. If there are any questions regarding this matter, please contact the Regional Administrator of the appropriate NRC regional office or this office. Edward L. Jordan, Director Division of Emergency Preparedness and Engineering Response Office of Inspection and Enforcement Technical Contact: M. S. Wegner, IE (301) 492-4511 Attachment: List of Recently Issued IE Information Notices
Page Last Reviewed/Updated Tuesday, March 09, 2021
Page Last Reviewed/Updated Tuesday, March 09, 2021