Information Notice No. 82-19:Loss of High Head Safety Injection Emergency Boration and Reactor Coolant Makeup Capability
SSINS No.: 6835 IN 82-19 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C. 20555 June 18, 1982 Information Notice No. 82-19: LOSS OF HIGH HEAD SAFETY INJECTION EMERGENCY BORATION AND REACTOR COOLANT MAKEUP CAPABILITY Addressees: All nuclear power reactor facilities holding an operating license (OL) or construction permit (CP). Purpose: This information notice is provided as a notification of an incident that may have safety significance. It is expected that recipients will review the information for applicability to their facilities. No specific action or response is required at this time. Description of Circumstances: On February 12, 1982, Duke Power Company's McGuire Unit 1 experienced a loss of high head safety injection emergency boration and reactor coolant makeup capability. Hydrogen from the positive displacement pump (PDP) suction dampener entered the common suction of the charging system, causing both centrifugal charging pumps (CCPs) and the PDP to be inoperable. The system was restored within 30 minutes. The unit was in Mode 1, at 50% of full power at the time of the event. While CCP 1A was operating, the licensee was preparing to return the PDP to service following maintenance. Upon opening of the suction isolation valve to the PDP, air and hydrogen in the PDP suction piping entered the common suction of the charging system. Control room personnel observed oscillation of the CCP 1A motor current and charging flow. They immediately shifted to CCP 1B and tripped CCP 1A. Approximately 30 seconds later, similar indications were received from CCP 1B. It was tripped, and letdown was isolated. When the nuclear equipment operator who had opened the isolation valve heard a page announcement that charging had been terminated, he immediately called the control room. As a result of his call, the control room operators suspected that gas from the PDP suction dampener was entering the common suction line. The operator was instructed to reclose the isolation valve. The suction piping and the CCPs were vented, CCP 1B was restarted, and charging and letdown were reestablished. The licensee does not intend to return the PDP to service until a change is made to preclude recurrence of this event. . IN 82-19 June 18, 1982 Page 2 of 2 The suction dampener installed at McGuire (see Attachment 1) consists of a vertical section of 12-inch pipe with hydrogen gas overpressure. Water level in the suction dampener is controlled automatically by two solenoid valves. Based on comparison of water levels in the suction dampener and its reference leg, one valve supplies gas when the suction dampener level is too high, and one valve vents gas when the level is too low. Prior to the event, the reference leg had been inadvertently drained, erron- eously indicating that the water level in the suction dampener was too high. Therefore, hydrogen was continuously supplied to the suction damper causing the gas to enter the suction piping common to the CCPs and the PDP. Failure to properly vent the PDP and its associated piping prior to opening the valve that isolates the equipment from the common suction of the CCP may have contributed to the event. During review of this event by the NRC staff, it became apparent that a single failure in the non-safety-related portion of the system resulted in loss of centrifugal and positive displacement safety injection charging pumps. There is a concern that the potential of a single component malfunction, personnel error, or maintenance error in the safety or non-safety related portion of the system could lead to the same consequences even though the system may be of a different design than that used at the McGuire Station. If you have any questions regarding this matter, please contact the Regional Administrator of the appropriate NRC Regional Office, or this office. Edward L. Jordan, Director Division of Engineering and Quality Assurance Office of Inspection and Enforcement Technical Contact: W. Marinelli 301-492-8073 Attachments: 1. Charging Pump Flow Diagram 2. List of Recently Issued IE Information Notices
Page Last Reviewed/Updated Tuesday, March 09, 2021
Page Last Reviewed/Updated Tuesday, March 09, 2021