U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/16/2009 - 12/17/2009 ** EVENT NUMBERS ** | General Information or Other | Event Number: 45563 | Rep Org: PA BUREAU OF RADIATION PROTECTION Licensee: GRAND VIEW HOSPITAL Region: 1 City: SELLERSVILLE State: PA County: BUCKS License #: PA-0220 Agreement: Y Docket: NRC Notified By: DAVID ALLARD HQ OPS Officer: HOWIE CROUCH | Notification Date: 12/11/2009 Notification Time: 18:40 [ET] Event Date: 12/11/2009 Event Time: [EST] Last Update Date: 12/11/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): DANIEL HOLODY (R1DO) CHRISTIAN EINBERG (FSME) | Event Text AGREEMENT STATE REPORT - MEDICAL EVENT The following information was obtained from the Commonwealth of Pennsylvania via facsimile: "Medi-Physics [PA license PA-0515] prepared a 30 ml kit of Myoview at approximately 2:30 a.m. on December 11, 2009. The radiochemical purity was determined to be 91%. They consider 90% on the center as passing. "On December 11, 2009, Grand View Hospital reported a problem with a nuclear medicine scan. Medi-Physics confirmed with BRP [Pennsylvania Bureau of Radiation Protection] that they dispensed 50 doses from the vial of Myoview in question. They believed 13 of these doses were administered to patients in PA and NJ. They thought the doses that were administered were resting doses of 8 to 10 mCi each. They assured BRP that they have a system in place to track their doses and contacted all the recipients once they were notified of the problem. "Initially, Grand View, one of the hospitals that received a Myoview dose, called Medi-Physics to advise them they saw thyroid and no cardiac uptake in a patient they injected with Myoview. This suggests free 99mTC04. Therefore, at approximately 8:30 a.m., they repeated [the quality check] on the Myoview left in the vial and determined the tag was less than 1%. Medi-Physics is still investigating the problem and will send the vial to the United Kingdom for chemical analysis once it is no longer radioactive. BRP feels this is an [abnormal occurrence] because there was (fundamentally) the wrong radiopharmaceutical given to a patient. "BRP has been in contact with all parties, will continue to investigate and enter in NMED." PA Report ID No.: PA090035 A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient. | General Information or Other | Event Number: 45566 | Rep Org: SC DIV OF HEALTH & ENV CONTROL Licensee: MCLEOD REGIONAL MEDICAL CENTER Region: 1 City: FLORENCE State: SC County: License #: 139 Agreement: Y Docket: NRC Notified By: JIM PETERSON HQ OPS Officer: DONALD NORWOOD | Notification Date: 12/14/2009 Notification Time: 01:40 [ET] Event Date: 12/09/2009 Event Time: [EST] Last Update Date: 12/14/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): DANIEL HOLODY (R1DO) REBECCA NEASE (R2DO) CHRISTIAN EINBERG (FSME) SAM COLLINS (R1) DONNA JANDA (R1) JOHN KINNEMAN (R1) DIANE SCRENCI (R1PA) ROBERT LEWIS (FSME) CHARLES MILLER (FSME) JOE DECICCO (FSME) | Event Text AGREEMENT STATE REPORT - Cs-137 BRACHYTHERAPY SOURCE LEAKING The following information was communicated to the NRC via a telephone notification on December 14, 2009: On Wednesday, December 9, 2009, Bionomics personnel were at McLeod Regional Medical Center in Florence, SC to package several old sources for disposal. These packages remained at McLeod until the following day when Bionomics personnel picked them up for transport to the Bionomics facility in Oak Ridge, TN. On Friday, December 11, 2009, a Bionomics worker reported that he had radioactive contamination on his clothing. On Sunday, December 13, 2009 it was ascertained that this radioactive contamination had come from the sources picked up at McLeod. A brachytherapy source containing 38 mCi of Cs-137 was found to be leaking. Bionomics contacted an HP consultant from the University of SC to have him perform radiation surveys at the McLeod facility. Radiation surveys found contamination in treatment areas, supply rooms, offices, and hallways. Highest contact readings were localized and were approximately 100 mR/hr. At this time it is believed that no radioactive contamination had been tracked outside of the McLeod facility. The McLeod Radiation Safety Officer has surveyed all staff personnel - except for two individuals - that had been in the contaminated areas. No radioactive contamination was found on any of these individuals. The other two individuals will be surveyed today, Monday, December 14, 2009. Bionomics personnel are presently on-site at the McLeod Medical Center performing decontamination. The Medical Center has closed the area to personnel and patients until decontamination is completed. | General Information or Other | Event Number: 45570 | Rep Org: NE DIV OF RADIOACTIVE MATERIALS Licensee: BECTON DICKINSON INFUSION THERAPY SYS Region: 4 City: BROKEN ARROW State: NE County: License #: 04-01-01 Agreement: Y Docket: NRC Notified By: JIM DEFRAIN HQ OPS Officer: VINCE KLCO | Notification Date: 12/15/2009 Notification Time: 16:45 [ET] Event Date: 12/14/2009 Event Time: 19:00 [CST] Last Update Date: 12/16/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): JACK WHITTEN (R4DO) REBECCA TADESSE (FSME) | Event Text AGREEMENT STATE REPORT - IRRADIATOR SAFETY INTERLOCKS BYPASSED While engaged in production, the irradiator source was brought down due to an electrical fault. To verify the source was in the shielded position, an operator was sent to the roof and verified that there was no slack in the cables and the position of the cables indicated the source as in the shielded position. The interlocks were bypassed and an operator entered the cell. A damaged wire was discovered and repaired. Operators did not receive any radiation dose from this event. Previously, a flex conduit was discovered with damaged insulation that had caused a short (Ref: EN # 45486). * * * UPDATE ON 12/16/09 AT 1724 FROM TRUDY HILL TO MARK ABRAMOVITZ * * * The Nebraska item number for this event is NE090018. Notified the R4DO (Whitten). | General Information or Other | Event Number: 45574 | Rep Org: HYDROAIRE Licensee: HYDROAIRE Region: 3 City: CHICAGO State: IL County: License #: Agreement: Y Docket: NRC Notified By: SESHA GIRI HQ OPS Officer: VINCE KLCO | Notification Date: 12/16/2009 Notification Time: 17:11 [ET] Event Date: 09/29/2009 Event Time: 09:02 [CST] Last Update Date: 12/16/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: 21.21 - UNSPECIFIED PARAGRAPH | Person (Organization): TAMARA BLOOMER (R3DO) PART 21 COORDINATOR (NRR) RICHARD BARKLEY (R1DO) | Event Text PART 21 INVOLVING A PUMP SHAFT COUPLING FAILURE A service water pump failed during operation on 9/29/2009. Upon disassembly it was detected that a shaft coupling installed on a repaired service water pump failed while in service. The failed coupling was replaced with a new coupling of a different heat code. According to the manufacturer, the threaded coupling design was only supplied for Palisades. | Power Reactor | Event Number: 45575 | Facility: PALO VERDE Region: 4 State: AZ Unit: [1] [2] [3] RX Type: [1] CE,[2] CE,[3] CE NRC Notified By: FARA ORESHACK HQ OPS Officer: MARK ABRAMOVITZ | Notification Date: 12/16/2009 Notification Time: 17:30 [ET] Event Date: 12/16/2009 Event Time: 06:11 [MST] Last Update Date: 12/16/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: 26.719 - FITNESS FOR DUTY | Person (Organization): JACK WHITTEN (R4DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | 2 | N | Y | 100 | Power Operation | 100 | Power Operation | 3 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text FITNESS FOR DUTY - NON-LICENSED SUPERVISOR A non-licensed supervisor had a confirmed positive for alcohol during a "for cause" fitness-for-duty test. The employee's access to the plant has been terminated. Contact the Headquarters Operations Officer for additional details. The licensee notified the NRC Resident Inspector. | Power Reactor | Event Number: 45576 | Facility: PALO VERDE Region: 4 State: AZ Unit: [1] [2] [3] RX Type: [1] CE,[2] CE,[3] CE NRC Notified By: FARA ORESHACK HQ OPS Officer: MARK ABRAMOVITZ | Notification Date: 12/16/2009 Notification Time: 17:30 [ET] Event Date: 12/16/2009 Event Time: 10:39 [MST] Last Update Date: 12/16/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: 26.719 - FITNESS FOR DUTY | Person (Organization): JACK WHITTEN (R4DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | 2 | N | Y | 100 | Power Operation | 100 | Power Operation | 3 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text FITNESS FOR DUTY - LICENSED OPERATOR A licensed operator supervisor had a confirmed positive for alcohol during a "for cause" test. The employee's access to the plant has been terminated. Contact the Headquarters Operations Officer for additional details. The licensee notified the NRC Resident Inspector. | Power Reactor | Event Number: 45577 | Facility: SUMMER Region: 2 State: SC Unit: [1] [ ] [ ] RX Type: [1] W-3-LP NRC Notified By: JASON WEATHERSBY HQ OPS Officer: KARL DIEDERICH | Notification Date: 12/16/2009 Notification Time: 17:30 [ET] Event Date: 12/16/2009 Event Time: 14:15 [EST] Last Update Date: 12/16/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): CHARLIE PAYNE (R2DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | M/R | Y | 45 | Power Operation | 0 | Hot Standby | Event Text MANUAL REACTOR TRIP FOLLOWING A FAILURE OF THE STEAM DUMP SYSTEM "VC Summer Nuclear Station (VCSNS) was performing a preplanned turbine shutdown in order to perform maintenance on a faulty turbine control valve. After the manual turbine trip, the steam dump system failed to operate and the crew manually tripped the reactor. The cause of the failure of the steam dump system is unknown, and is currently being investigated. Both motor driven Emergency Feedwater pumps were manually started at 40% Steam Generator Level. Preliminary review indicates all other primary and secondary systems responded as required. The plant is in mode 3 at normal RCS [Reactor Coolant System] pressure and temperature. Decay heat is being removed by dumping steam via the secondary [steam generator] power operated relief valves. The station will remain in mode 3 until repairs are complete. Estimated restart date has not been determined." All rods fully inserted. There is no known primary to secondary leakage. Off site power supply configuration is normal. The turbine trip was performed at 45% power due to a stuck open turbine control valve. The licensee has notified the NRC Resident Inspector and will notify state and local contacts. | |