U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/12/2009 - 11/13/2009 ** EVENT NUMBERS ** | General Information or Other | Event Number: 45485 | Rep Org: KENTUCKY DEPT OF RADIATION CONTROL Licensee: HARDIN MEMORIAL HOSPITAL Region: 1 City: ELIZABETHTOWN State: KY County: License #: KY-202-148-26 Agreement: Y Docket: NRC Notified By: ANGELA SHARYOCK HQ OPS Officer: CHARLES TEAL | Notification Date: 11/09/2009 Notification Time: 10:50 [ET] Event Date: 08/28/2009 Event Time: [CST] Last Update Date: 11/09/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): CHRISTOPHER CAHILL (R1DO) ANGELA MCINTOSH (FSME) | Event Text AGREEMENT STATE REPORT - BRACHYTHERAPY PATIENT RECEIVED MORE THAN PRESCRIBED DOSE The following information was received via NMED report #090706: "Hardin Memorial Hospital reported that a patient received 26.9% more dose than prescribed during prostate seed implant procedure on 8/28/09. The patient received I-125 brachytherapy seeds with a total activity of 1.26 GBq (34.054 mCi) instead of the prescribed 0.99 GBq (26.825 mCi). It is believed that the medical physicist calculated dose to the prostate using air kerma instead of milliCurie. All physicians and the patient have been notified of the mistake." A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient. | General Information or Other | Event Number: 45486 | Rep Org: NE DIV OF RADIOACTIVE MATERIALS Licensee: BECTON DICKINSON INFUSION THERAPY SYSTEMS INC Region: 4 City: BROKEN BOW State: NE County: License #: 04-01-01 Agreement: Y Docket: NRC Notified By: JIM DEFRAIN HQ OPS Officer: MARK ABRAMOVITZ | Notification Date: 11/09/2009 Notification Time: 16:54 [ET] Event Date: 11/07/2009 Event Time: [CST] Last Update Date: 11/09/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): JEFF CLARK (R4DO) ANDREA KOCK (FSME) | Event Text AGREEMENT STATE REPORT - IRRADIATOR SAFETY INTERLOCKS BYPASSED A fuse blew during operation of an irradiator facility in Broken Bow, NE. This affected: the source up or down indication, the roof plug switch, the high temperature sensor, and the source movement light. The system could not be reset manually with the key. To verify the source was in the shielded position, an operator was sent to the roof and verified that there was no slack in the cables and the position of the cables indicated the source was in the shielded position. The interlocks were bypassed and an operator entered the cell. It was determined that there was a blown fuse and faulty wiring which were replaced. Operators did not receive any radiation dose from this event. | Fuel Cycle Facility | Event Number: 45491 | Facility: GLOBAL NUCLEAR FUEL - AMERICAS RX Type: URANIUM FUEL FABRICATION Comments: LEU CONVERSION (UF6 TO UO2) LEU FABRICATION LWR COMMERICAL FUEL Region: 2 City: WILMINGTON State: NC County: NEW HANOVER License #: SNM-1097 Agreement: Y Docket: 07001113 NRC Notified By: SCOTT MURRAY HQ OPS Officer: JOE O'HARA | Notification Date: 11/12/2009 Notification Time: 11:47 [ET] Event Date: 11/11/2009 Event Time: 15:00 [EST] Last Update Date: 11/12/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: PART 70 APP A (b)(1) - UNANALYZED CONDITION | Person (Organization): MARK LESSER (R2DO) E. WILLIAM BRACH (NMSS) | Event Text INCOMPLETE DOCUMENTATION OF CRITICALITY SAFETY CONTROLS IN INTEGRATED SAFETY ANALYSIS SUMMARY "During a GNF-A ongoing review of the Fuel Manufacturing Operation (FMO) Integrated Safety Analysis (ISA), it was discovered at 3pm yesterday (11/11/09) that there may be an incomplete list of criticality safety controls associated with the Pellet and Rod Load Fabrication areas in the ISA Summary. "At 7pm, it was determined that the list of Items Relied On For Safety (IROFS) was incomplete and the affected equipment was shut down pending revision of the ISA to document IROFS for these processes. Notwithstanding the documentation deficiency, the controls associated with moderator intrusion and geometry remained in place, functional, and maintained with appropriate management controls. "While this discovery did not result in an unsafe condition, it is being reported on 11/12/09 pursuant to the reporting requirements of 10CFR70 Appendix A(b)(1) within 24 hours. "Safety Significance of Events: Low safety significance - All process criticality safety controls remained intact and functioning for this processes. "Safety Equipment Status: Pellet and Fuel Load fabrication areas are shutdown and will remain shutdown until the ISA review is completed. "Status of Corrective Actions: Pellet and Rod Load Fabrication areas will remain shutdown pending final investigation results and identification of additional IROFS." The licensee notified NRC Region 2 Inspector (Crespo) and will notify state and local authorities. | Fuel Cycle Facility | Event Number: 45492 | Facility: PADUCAH GASEOUS DIFFUSION PLANT RX Type: URANIUM ENRICHMENT FACILITY Comments: 2 DEMOCRACY CENTER 6903 ROCKLEDGE DRIVE BETHESDA, MD 20817 (301)564-3200 Region: 2 City: PADUCAH State: KY County: McCRACKEN License #: GDP-1 Agreement: Y Docket: 0707001 NRC Notified By: ROBERT MAGLASANG HQ OPS Officer: DONALD NORWOOD | Notification Date: 11/12/2009 Notification Time: 16:09 [ET] Event Date: 11/12/2009 Event Time: 11:15 [CST] Last Update Date: 11/12/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: RESPONSE-BULLETIN | Person (Organization): MARK LESSER (R2DO) E. WILLIAM BRACH (NMSS) | Event Text VIOLATION OF A NUCLEAR CRITICALITY SAFETY CONTROL "At 1115 CST on 11/12/09, abandoned cell piping was reported in C-331 and C-335 cell housings. The 16-inch abandoned piping is from the cell recycle line that was replaced in the mid 1970s. NCS [Nuclear Criticality Safety] controls require that equipment openings with unknown uranium deposits shall be covered with water-proof covers that are fire resistant. Since the piping contains an unknown uranium mass, and was discovered without water-proof covers, the NCS control was violated. "Since moderation is the primary criticality control, and where double contingency cannot be re-established within 4 hours, this is being reported to the NRC as a 4-hour Event Report in accordance with NRC BL 91-01 Supplement 1. "The NRC Resident Inspector has been notified of this event. "PGDP Problem Report No. ATRC-09-2781; PGDP Event Report No. PAD-2009-19. "Safety significance of events: Although the NCS control to cover the pipe openings was violated, it was not exposed to a liquid moderator. The geometry of the pipe is safe for a maximum enrichment that may be in the pipe. During the plant modifications that replaced the cell recycle lines, the maximum plant enrichment was 2.0 wt. % U235. There are no indications, based on quarterly NDA scans, that the piping contains greater than a safe mass of uranium. Therefore, the safety significance of the event is low. "Potential criticality pathways involved: The maximum plant enrichment at the time the piping was in operation was a maximum 2.0 wt. % U235. The piping is contained in housing without fire suppression. The single parameter pipe diameter for that enrichment is greater than 16 inches. In order for a criticality to be possible, the pipe would have to contain greater than a critical mass. A large amount of moderator would have to enter the horizontal pipe opening. Greater than a critical mass would then have to be washed from the pipe due to the unlikely moderator release at the pipe opening. The washed material would then have to accumulate in an unsafe geometry. "Controlled parameters: Moderation. "Estimated amount, enrichment, form of licensed material: The assay of any material is less than or equal to 2.00 wt. % U235. "Nuclear Criticality safety control(s) or control systems(s) and description of the failures or deficiencies: The first leg of double contingency relies on control of moderation. Moderator intrusion associated with sprinkler activation is controlled by limiting fire sprinkler head activation temperatures at the ceiling and bypass heights. The analysis also determined that significant moderator intrusion into open fissile piping due to inadvertent spills, RCW/oil line leaks, or other mechanism is unlikely. These controls were not violated and an unlikely moderator release event has not occurred at the pipe opening. The second leg of double contingency is also based on moderation. Piping exceeding 10.25 inches that contains an unknown or greater than safe mass deposit is required to have openings covered with fire resistant waterproof covers. Since the piping is nominal 16 inches in diameter, contains an unknown uranium mass, the NCS control was violated. Since the openings are not covered resulting in a loss of NCS control and there are two controls on one parameter, the process condition was not maintained. "Corrective actions to restore safety systems and when each was implemented: Control access to the area. Exempt the pipe from NCS controls based on enrichment determination, cover the pipe openings, or quantify the uranium mass in the pipe." | Power Reactor | Event Number: 45493 | Facility: SURRY Region: 2 State: VA Unit: [1] [2] [ ] RX Type: [1] W-3-LP,[2] W-3-LP NRC Notified By: DAN SCHOENSTER HQ OPS Officer: DONALD NORWOOD | Notification Date: 11/12/2009 Notification Time: 22:00 [ET] Event Date: 11/12/2009 Event Time: 19:00 [EST] Last Update Date: 11/12/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(xi) - OFFSITE NOTIFICATION | Person (Organization): MARK LESSER (R2DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | 2 | N | N | 0 | Refueling | 0 | Refueling | Event Text NOTIFICATION TO US COAST GUARD AND COMMONWEALTH OF VIRGINIA OF HAZARD TO NAVIGATION "Surry Power Station maintenance activities at the James River intake structure were supported with a barge from Crofton Industries using stop logs (referred to as caissons, each with dimensions of 24'x6'x3'and weighing 11,000 pounds empty) to seal water ingress into intake bays. On November 12, 2009, due to the potential for damage from high winds and tide, the barge and four of the caissons were towed by tug boat from the intake structure, across the James River, to Fort Eustis. At 1650 hours, mid-way across the river, one of the caissons broke free from the tug. The tug operator attempted to secure the partially submerged caisson, but was unsuccessful. The tug operator noted the location and completed the transfer of the barge and caissons to Fort Eustis. "At approximately 1900 hours, Crofton Industries informed Surry Power Station that in accordance with the Marine Safety Office Notification Procedure, they communicated with the US Coast Guard, notifying them of the incident and the approximate location of the caisson. In addition, at 2030 hours, Surry made a courtesy notification of the incident to the Virginia Department of Emergency Services. This report is being submitted due to the notification of other government agencies under 10CFR50.72(b)(2)(xi). In addition, the Site NRC Resident was also notified of this event." | Power Reactor | Event Number: 45494 | Facility: BROWNS FERRY Region: 2 State: AL Unit: [ ] [ ] [3] RX Type: [1] GE-4,[2] GE-4,[3] GE-4 NRC Notified By: JOE BENNETT HQ OPS Officer: DONALD NORWOOD | Notification Date: 11/12/2009 Notification Time: 22:36 [ET] Event Date: 11/12/2009 Event Time: 17:11 [CST] Last Update Date: 11/12/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(v)(D) - ACCIDENT MITIGATION | Person (Organization): MARK LESSER (R2DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 3 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text HPCI INOPERABLE DUE TO EXCESSIVE WATER IN STEAM DRAIN "The HPCI [High Pressure Coolant Injection] system was declared inoperable after completion of a scheduled surveillance due to an excessive amount of water in the turbine exhaust line. The line was being drained in response to the alarm 'HPCI TURB EXH DRAIN POT LEVEL HIGH', indicating that there was a high level in a drain pot attached to the turbine exhaust line. An investigation is in progress to determine the source of the water in the turbine exhaust line. "This event is reportable within 8 hours in accordance with 10CFR 50.72(b)(3)(v) as an event or condition that at the time of discovery could have prevented the fulfillment of a safety function. It also requires a 60 day written report in accordance with 10CFR 50.73(a)(2)(vii) "The NRC Resident Inspector has been notified. "SR number associated with this report: 91546." | |