U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/21/2006 - 11/22/2006 ** EVENT NUMBERS ** | Power Reactor | Event Number: 43002 | Facility: WATTS BAR Region: 2 State: TN Unit: [1] [ ] [ ] RX Type: [1] W-4-LP,[2] W-4-LP NRC Notified By: BEN HUNT HQ OPS Officer: JEFF ROTTON | Notification Date: 11/21/2006 Notification Time: 06:31 [ET] Event Date: 11/21/2006 Event Time: 06:15 [EST] Last Update Date: 11/21/2006 | Emergency Class: UNUSUAL EVENT 10 CFR Section: 50.72(a) (1) (i) - EMERGENCY DECLARED 50.72(b)(2)(xi) - OFFSITE NOTIFICATION | Person (Organization): ROBERT HAAG (R2) JARED WERMIEL (NRR) MELVYN LEACH (IRD) CONSTANTOPOULOS (DHS) MIKE LAFORTY (FEMA) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | N | 0 | Cold Shutdown | 0 | Cold Shutdown | Event Text UNUSUAL EVENT DECLARED DUE TO UNIDENTIFIED LEAKAGE Licensee reported 20 GPM of unidentified leakage from indication of VCT lowering level. RCS pressure is 50 psig. Source of the leak has not been identified and it is not known at this time where the RCS leakage is going. All air and liquid releases are within specifications and no protective action recommendations are needed at this time. The licensee has notified the State and Local emergency agencies. The licensee will notify the NRC Resident Inspector. * * * UPDATE PROVIDED BY BEN HUNT TO JEFF ROTTON AT 0714 ON 11/21/06 * * * Unidentified leakage is now calculated to be 2 GPM based on inventory balance using charging and letdown flow and VCT level. It is believed that the indication of a leak may be from an incomplete vacuum fill of the S/G after the S/G replacement modification and when the RCS was pressurized, the remaining voids in the S/Gs were filled. There has been no visible leakage found outside of the RCS. Notified NRREO (Wermiel), R2DO (Haag), IRD Manager (Wilson / Leach). * * * UPDATE AT 0756 ON 11/21/2006 FROM BEN HUNT TO MARK ABRAMOVITZ * * * The licensee terminated the Unusual Event (UE) at 0737 due to indicated RCS leakage being less than 2 GPM. The site's emergency action criteria for a UE is 10 GPM unidentified leakage. No water has been found to have leaked outside the RCS. The licensee notified the NRC Resident Inspector. Notified NRREO (Wermiel, Ross-Lee), R2DO (Haag), IRD Manager (Wilson, Leach), DHS SWO (Gray), FEMA (LaForty) * * * UPDATE PROVIDED BY DOUG HOLT TO JEFF ROTTON AT 0959 ON 11/21/06 * * * "The cause of the apparent leakage is under investigation by plant and TVA personnel. No actual leakage is believed to have transpired. Current plant conditions are stable." The licensee notified the NRC Resident Inspector. Notified R2DO (Haag), NRREO (Ross-Lee), IRD Manager (Wilson) * * * UPDATE AT 1215 EST ON 11/21/06 FROM DOUG HOLT TO S. SANDIN * * * "As a result of the declaration of a Notification of Unusual Event earlier today relative to a suspected RCS leak, a News Release is being made. The purpose of the release is to clarify to local officials and residents the nature of the suspected leak and the actions taken by school officials. The cause of the suspected leak remains under investigation." The licensee notified the NRC Resident Inspector. Notified R2DO (Haag). | |