Event Notification Report for May 22, 2003
U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
05/21/2003 - 05/22/2003
** EVENT NUMBERS **
39754 39853 39869 39870 39871 39872 39873 39874 39875
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 39754 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 04/13/2003|
| UNIT: [1] [] [] STATE: TX |NOTIFICATION TIME: 19:06[EDT]|
| RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/13/2003|
+------------------------------------------------+EVENT TIME: 16:56[CDT]|
| NRC NOTIFIED BY: RON GIBBS |LAST UPDATE DATE: 05/21/2003|
| HQ OPS OFFICER: STEVE SANDIN +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |DAVID LOVELESS R4 |
|10 CFR SECTION: | |
|ADEG 50.72(b)(3)(ii)(A) DEGRADED CONDITION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N N 0 Cold Shutdown |0 Cold Shutdown |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| REACTOR VESSEL BOTTOM HEAD DEGRADED CONDITION |
| |
| "On 4/12/2003, during the Unit 1 11th (1RE11) refueling outage, an |
| inspection was performed of the vessel bottom head. This bare metal |
| inspection identified a potential leak indication at the head to penetration |
| interface for Bottom Mounted Instrumentation (BMI) penetrations 1 and 46. |
| There was a small amount of residue around the outer circumference of the |
| BMI penetrations. No wastage was observed. Samples of the residue were taken |
| and the area was cleaned with demineralized water. Chemical sample results |
| available as of 1300 on 4/13/2003 are not conclusive; however, they have |
| confirmed that the residue found at the Penetration 46 contains boron, |
| indicating that this could be an RCS leak. The residue removed from |
| Penetration 1 was characterized as 'gummy' and its composition is still |
| under investigation. Additional exams are planned to confirm the likely |
| origin of the residue and to determine the scope of any repairs. There has |
| been no indication of RCS leakage observed at the BMI penetrations during |
| previous operational cycles. This notification is being made in accordance |
| with 10 CFR 50.72(b)(3)(ii)(A)." |
| |
| Unit 1 will remain in mode 5 until appropriate corrective actions are |
| identified. The licensee informed the NRC resident inspector. |
| |
| * * * * UPDATE 1151 EDT 04/18/03 FROM WAYNE HARRISON TO MIKE RIPLEY * * * |
| |
| "STP Nuclear Operating Co. will be making a press release [at 12:00 pm |
| 04/18/03] concerning the indications found on the Bottom Mounted |
| Instrumentation penetrations on Unit 1. The release is being coordinated |
| with NRC Region IV. |
| |
| "STP has notified or will be notifying various federal, state and local |
| agencies, including FEMA, the governors office, Matagorda County, Bay City. |
| City of Palacios, state representatives and state senators, US |
| representatives and US Senators." |
| |
| The licensee notified the NRC Resident Inspector. |
| |
| Notified R4DO (C. Johnson), HQ PAO (W. Beecher) |
| |
| *** UPDATE AT 1745 EDT ON 05/21/03 FROM WAYNE HARRISON TO ARLON COSTA *** |
| |
| "STP Nuclear Operating Co. expects to make a press release on 5/22/2003 |
| concerning the indications found on the Bottom Mounted Instrumentation |
| penetrations on Unit 1. NRC Region IV has been advised of the planned press |
| release. STPNOC will also be sharing the press release with various local |
| and state government agencies. |
| |
| "The draft release is attached. |
| |
| "NRC was notified of the leakage per 10CFR50.72 on 4/13/2003 (EN# 39754). |
| |
| "NRC was notified of a press release describing the leakage on 4/18/2003 |
| (EN#39754 update)." |
| |
| The licensee notified the NRC Resident Inspector. |
| |
| Notified HQ PAO (W. Beecher) and R4DO(T. Pruett). |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Fuel Cycle Facility |Event Number: 39853 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/16/2003|
| RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 10:04[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/15/2003|
| 6903 ROCKLEDGE DRIVE |EVENT TIME: 14:00[EDT]|
| BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/21/2003|
| CITY: PIKETON REGION: 3 +-----------------------------+
| COUNTY: PIKE STATE: OH |PERSON ORGANIZATION |
|LICENSE#: GDP-2 AGREEMENT: N |SONIA BURGESS R3 |
| DOCKET: 0707002 |TOM ESSIG NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: MCCLEERY | |
| HQ OPS OFFICER: CHAUNCEY GOULD | |
+------------------------------------------------+ |
|EMERGENCY CLASS: NON EMERGENCY | |
|10 CFR SECTION: | |
|QSAF 72.75(c)(2) SAFETY EQUIP DISABLED/F| |
|NONR OTHER UNSPEC REQMNT | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| SAFETY SYSTEM ACTUATION |
| |
| On 5/15/03 @1400 during pigtail disconnect, a small amount of particulate |
| fell from the pigtail. This particulate began to smoke resulting in a see |
| and flee. During the see and flee the gas release alarm was activated. The |
| alarm resulted in the actuation of a "Q" Safety system while in applicable |
| mode (mode III). The PSS Responded to the see and flee. The affected |
| cylinder was made inoperable. No spread of contamination outside already |
| posted area. Air sampling results are less than MDA. |
| |
| The NRC Resident Inspector was notified. |
| |
| * * * UPDATE AT 23:46 EDT ON 5/20/03 FROM McCLEERY TO CROUCH * * * |
| |
| The following update was received from the regulatee via facsimile: |
| |
| "5/20/05: As requested, this is additional information to clarify some |
| questions in the initial report of PTS-2003-011. Mode III (Cylinder/Pigtail |
| Operations) includes but is not limited to pigtail |
| connection/disconnections, roll/tilt and valve clarity checks; steam valves |
| closed, cylinder valve or safety valve may or may not be closed. MDA is |
| minimum detectable activity. The initial report should have been marked as |
| Other Non-CFR Requirements in place of (c)(2) safety equipment failure. |
| |
| Additionally, during the investigation of the event it was determined the |
| cylinder safety valve air supply was removed prior to the see and flee. |
| This condition is reportable under 76.120 (c)(2)(ii) [and] 76.120 (d)(2). |
| The equipment is required by Technical Safety Requirements (TSR) to be |
| available and operable to perform the required safety function, while the |
| autoclave is operating in mode III (cylinder/ pigtail operations). |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Fuel Cycle Facility |Event Number: 39869 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/20/2003|
| RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 23:46[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/20/2003|
| 6903 ROCKLEDGE DRIVE |EVENT TIME: 09:30[EDT]|
| BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/21/2003|
| CITY: PIKETON REGION: 3 +-----------------------------+
| COUNTY: PIKE STATE: OH |PERSON ORGANIZATION |
|LICENSE#: GDP-2 AGREEMENT: N |ANNE MARIE STONE R3 |
| DOCKET: 0707002 |JOHN HICKEY NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: JIM McCLEERY | |
| HQ OPS OFFICER: HOWIE CROUCH | |
+------------------------------------------------+ |
|EMERGENCY CLASS: NON EMERGENCY | |
|10 CFR SECTION: | |
|OSAF 76.120(c)(2) SAFETY EQUIPMENT FAILUR| |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| SAFETY EQUIPMENT FAILURE |
| |
| The following information was obtained from the regulatee via facsimile: |
| |
| "05/20/03 at 0930 hrs. following the investigation into circumstances |
| surrounding NRC Event #39853 (PTS-2003-011 update #1), the Plant Shift |
| Superintendent's (PSS) office was notified that the air supply line to the |
| parent cylinder safety valves had been disconnected during applicable TSR |
| mode III (Cylinder/Pigtail Operations) on multiple occasions in both the |
| X-343 and X-344 facilities. Discussions with facility management and |
| operating personnel indicate the air supply line was disconnected in |
| preparation for sampling operations. This condition is reportable under |
| 76.120 (c)(2)(ii) and 76.120 (d)(2). The equipment is required by Technical |
| Safety Requirements (TSR) to be available and operable and either should |
| have been operating or have operated on demand. |
| |
| "The PSS directed an extent of condition be performed for cylinder |
| operations in X-342, X-343, X-344 and X-326 withdrawal station. The result |
| of the extent of condition placed the X-343 sample autoclaves in mode VII |
| (shutdown) and removed from service until affected procedures can be |
| changed, the X-344 autoclaves remain operable, the X-342 autoclaves remains |
| inoperable, and the X-326 withdrawal station remains operable." |
| |
| The regulatee has notified the NRC Resident Inspector. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Fuel Cycle Facility |Event Number: 39870 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/21/2003|
| RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 00:08[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/20/2003|
| 6903 ROCKLEDGE DRIVE |EVENT TIME: 19:15[CDT]|
| BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/21/2003|
| CITY: PADUCAH REGION: 3 +-----------------------------+
| COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION |
|LICENSE#: GDP-1 AGREEMENT: Y |ANNE MARIE STONE R3 |
| DOCKET: 0707001 |JOHN HICKEY NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: C. PITTMAN | |
| HQ OPS OFFICER: HOWIE CROUCH | |
+------------------------------------------------+ |
|EMERGENCY CLASS: NON EMERGENCY | |
|10 CFR SECTION: | |
|NBNL RESPONSE-BULLETIN | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| CRITICALITY CONTROL 24-HOUR REPORT (BULLETIN 91-01) |
| |
| The following information was received from the regulatee via facsimile : |
| |
| "At 1915 on 5/20/03, the Plant Shift Superintendent (PSS) was notified that |
| some removed process gas equipment item groups in C-720 have not received |
| proper independent mass verification in violation of NCSA GEN-010. The |
| group mass is required to be independently verified to be within always safe |
| mass limits. This is done by independently verifying the equipment item |
| mass is correctly copied onto the grouping sheet. An entry was discovered |
| on the grouping sheet in which the mass on the equipment was 0 [zero] |
| pounds, however the GEN-010 tag on the equipment item indicated a mass of |
| 284 pounds of uranium at 1.38% enrichment. Additionally, several equipment |
| items were tagged with GEN-010 tags that had information lined out and |
| corrected, appearing to violate the independent verification of the |
| equipment item mass, on the tag. This information was then subsequently |
| used for grouping purposes on the equipment grouping sheet. This is a legacy |
| issue, as the dates on the tags are from the 97-98 timeframe. |
| |
| "SAFETY SIGNIFICANCE OF EVENTS: |
| |
| "Double contingency was not maintained because the independent verification |
| of mass has not been performed. However, the policy for the shop is to only |
| allow items which have been fully decontaminated into the shop, which gives |
| high confidence that less than a safe mass is present. |
| |
| "POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO(S) OF HOW |
| CRITICALITY COULD OCCUR): |
| |
| "In order for a criticality to be possible, greater than a critical mass of |
| uranium must be accumulated [and] then become moderated. |
| |
| "CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.): |
| |
| "Double contingency is maintained by implementing two controls on mass. |
| |
| "ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS |
| LIMIT AND % WORST CASE CRITICAL MASS): |
| |
| "Less than an always safe mass of uranium. |
| |
| "NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION |
| OF THE FAILURES OR DEFICIENCIES: |
| |
| "The first leg of double contingency is based on mass. NCSA GEN-010 |
| requires that the total uranium mass of grouped items be verified less than |
| the UH [Uncomplicated Handling] mass limit and documented. The mass of an |
| equipment item was incorrectly copied onto the grouping sheet. However, the |
| listed mass for the item is UH at the listed enrichment. In addition, other |
| items in the group have tags, which indicate no visible contamination but |
| have been updated and only have one signature. This mass was then used in |
| the grouping. The control was violated, however the parameter has been |
| maintained. |
| |
| "The second leg of double contingency is based on mass. NCSA GEN-010 |
| requires that the total uranium mass of grouped items be independently |
| verified less than the UH mass limit and documented in accordance with |
| CP2-PO-FO1031 [a facility procedure]. The independent verification was |
| incorrectly performed; therefore, this control was violated. Since there |
| are two controls on one parameter, double contingency was not maintained. |
| |
| "Since double contingency is based on two controls on one parameter, and a |
| control was violated, double contingency was not maintained. |
| |
| "CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEMS AND WHEN EACH WAS |
| IMPLEMENTED: |
| |
| "Ensure each item in the group is properly tagged according to CP2-CO-CN2030 |
| [a facility procedure]. Properly group and document each equipment item |
| according to CP2-CO-CN2030. Upon completion of the above corrective |
| actions, the exclusion zone and postings may be removed." |
| |
| The regulatee has notified the NRC Resident Inspector. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 39871 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PALO VERDE REGION: 4 |NOTIFICATION DATE: 05/21/2003|
| UNIT: [1] [2] [3] STATE: AZ |NOTIFICATION TIME: 09:15[EDT]|
| RXTYPE: [1] CE,[2] CE,[3] CE |EVENT DATE: 05/21/2003|
+------------------------------------------------+EVENT TIME: 02:20[MST]|
| NRC NOTIFIED BY: COSENZA |LAST UPDATE DATE: 05/21/2003|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |TROY PRUETT R4 |
|10 CFR SECTION: | |
|NINF INFORMATION ONLY | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 98 Power Operation |98 Power Operation |
|2 N Y 98 Power Operation |98 Power Operation |
|3 N Y 98 Power Operation |98 Power Operation |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| FAILURE OF THE SECURITY FORCES HAND HELD RADIOS |
| |
| Security at the site had a partial loss of their radio system. Their Bay |
| station and telephone communications systems were up, but the hand held |
| radios could not transmit out. These radios, however could receive. This |
| problem has occurred in the past. Their communications people were able to |
| reboot the system and go back to the secondary and returned the radios back |
| to service. There was no evidence that equipment had been tampered with. |
| |
| The NRC Resident will be notified. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 39872 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DRESDEN REGION: 3 |NOTIFICATION DATE: 05/21/2003|
| UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 11:31[EDT]|
| RXTYPE: [1] GE-1,[2] GE-3,[3] GE-3 |EVENT DATE: 05/21/2003|
+------------------------------------------------+EVENT TIME: 04:18[CDT]|
| NRC NOTIFIED BY: DENNIS FRANCIS |LAST UPDATE DATE: 05/21/2003|
| HQ OPS OFFICER: HOWIE CROUCH +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |ANNE MARIE STONE R3 |
|10 CFR SECTION: | |
|AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
| | |
|2 N Y 85 Power Operation |85 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| ACCIDENT MITIGATION DEGRADED DUE TO PRESSURE SWITCHES OUTSIDE TECHNICAL |
| SPECIFICATION ALLOWANCES |
| |
| "During calibration of Dresden Unit 2 Electromatic Relief Valve/Target Rock |
| Valve Pressure Switches, two of the five pressure switches were found |
| outside the Technical Specification (TS) Allowable Range and outside the |
| Analytical Limit (1.5 psig above the TS Allowable). Setpoints for the B and |
| C Electromatic Relief Valves (ERVs) were found at 3.1 and 2.4 psig above the |
| TS allowable respectively. The TS Bases state that four ERVs are required |
| to accomplish the safety function for pressure mitigation. This event is |
| reportable because two of five ERV pressure switches were outside TS |
| allowables, which could have prevented fulfillment of the safety function |
| for pressure mitigation (10 CFR 50.73(a)(2)(v)]. The pressure switch |
| setpoints have been subsequently calibrated and returned to within TS |
| allowable values." |
| |
| The licensee notified NRC Resident Inspector. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Other Nuclear Material |Event Number: 39873 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG: S.K. GEOTECHNICAL CORPORATION |NOTIFICATION DATE: 05/21/2003|
|LICENSEE: S.K. GEOTECHNICAL CORPORATION |NOTIFICATION TIME: 13:06[EDT]|
| CITY: HELENA REGION: 4 |EVENT DATE: 05/21/2003|
| COUNTY: STATE: MT |EVENT TIME: 07:00[MDT]|
|LICENSE#: 25-27594-01 AGREEMENT: N |LAST UPDATE DATE: 05/21/2003|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |TROY PRUETT R4 |
| |JIM WHITNEY TAS |
+------------------------------------------------+LARRY CAMPER NMSS |
| NRC NOTIFIED BY: LOWELL KLOCKE | |
| HQ OPS OFFICER: ARLON COSTA | |
+------------------------------------------------+ |
|EMERGENCY CLASS: NON EMERGENCY | |
|10 CFR SECTION: | |
|BLO1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| STOLEN MOISTURE DENSITY GAUGE |
| |
| A Campbell Pacific Nuclear portable moisture density gauge Model MC-3, |
| Serial Number MC 39058846 was stolen from the licensee's storage trailer. |
| The gauge contains a cesium-americium-beryllium radioactive source (10 |
| millicuries Cs-137 and 50 millicuries Am-241/Be). The licensee's trailer |
| containing the stolen gauge was located at a Home Depot construction site, |
| 1801 Custer Ave, Helena, MT 59601. Helena City police is investigating this |
| and other thefts that occurred overnight at several trailers located at this |
| same site. |
| |
| The licensee contacted Region IV (M. Shaffer) and will contact the Montana |
| Department of Health. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 39874 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 05/21/2003|
| UNIT: [2] [3] [] STATE: NY |NOTIFICATION TIME: 17:32[EDT]|
| RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 05/21/2003|
+------------------------------------------------+EVENT TIME: 13:55[EDT]|
| NRC NOTIFIED BY: RICHARD ALEXANDER |LAST UPDATE DATE: 05/21/2003|
| HQ OPS OFFICER: ARLON COSTA +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |ANTHONY DIMITRIADIS R1 |
|10 CFR SECTION: | |
|ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|2 N Y 100 Power Operation |100 Power Operation |
|3 N Y 100 Power Operation |100 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| LOSS COMMUNICATION DUE TO MORE THAN 10% AVAILABILITY OF SIRENS |
| |
| "On May 21, 2003 at 1355 hours, during on site monitoring of the offsite |
| emergency notification system, three (3) sirens out of a total of 10 in |
| Putnam County indicated a communications failure. The cause for the failure |
| was subsequently determined, based on information obtained by the crew, to |
| have been attributed to communication failure due to fuse failure at the |
| sirens. Communication was fully restored to the affected sirens at |
| approximately 1549 hours on May 21, 2003. Route alerting was available |
| during the loss of sirens. |
| |
| "The NRC resident inspectors, State and Putnam county were notified of this |
| event." |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Other Nuclear Material |Event Number: 39875 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG: TERRACON CORPORATION |NOTIFICATION DATE: 05/21/2003|
|LICENSEE: TERRACON CORPORATION |NOTIFICATION TIME: 18:08[EDT]|
| CITY: Raymore REGION: 3 |EVENT DATE: 05/21/2003|
| COUNTY: STATE: MO |EVENT TIME: [CDT]|
|LICENSE#: 15-27070-01 AGREEMENT: N |LAST UPDATE DATE: 05/21/2003|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |TROY PRUETT R4 |
| |MARK SHAFFER R4 |
+------------------------------------------------+LARRY CAMPER NMSS |
| NRC NOTIFIED BY: Bob Weber |ANNE MARIE STONE R3 |
| HQ OPS OFFICER: MIKE RIPLEY | |
+------------------------------------------------+ |
|EMERGENCY CLASS: NON EMERGENCY | |
|10 CFR SECTION: | |
|NONR OTHER UNSPEC REQMNT | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| DAMAGED MOISTURE DENSITY GUAGE |
| |
| A moisture density gauge owned by the licensee was damaged when it was run |
| over at a construction site in Raymore, Missouri (Hwy. 58 at Lauris Dr.). |
| The gauge is a Campbell Pacific model CPN1DR containing a 10 millicurie |
| Cs-137 source and a 50 millicurie Am-241:Be source. The gauge has been |
| isolated and it has been determined that the sources appear intact. The |
| licensee is the process of retrieving the gauge for return to the |
| manufacturer. |
| |
| Notified R3DO (A. Stone), R4DO (T. Pruett), R4 (Mark Shaffer), NMSS EO (L. |
| Camper) |
+------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021