The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for March 15, 2001

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           03/14/2001 - 03/15/2001

                              ** EVENT NUMBERS **

37831  37835  37836  37837  37838  37839  37840  37841  

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   37831       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 03/13/2001|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 08:24[EST]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        03/12/2001|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        17:45[EST]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  03/14/2001|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |GEOFFREY WRIGHT      R3      |
|  DOCKET:  0707002                              |JOHN HICKEY          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  JOE HALCOMB                  |                             |
|  HQ OPS OFFICER:  FANGIE JONES                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NBNL                     RESPONSE-BULLETIN      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| NRC BULLETIN 91-01 - 24 HOUR REPORT                                          |
|                                                                              |
| The following is taken from the faxed report:                                |
|                                                                              |
| ON 3/12/01 AT 1745 HOURS X-705 OPERATIONS PERSONNEL WERE CONDUCTING ROUTINE  |
| INSPECTIONS OF THE TUNNEL BASEMENT AREA WHEN THEY IDENTIFIED THAT THE        |
| SCAVENGER SYSTEM WOULD NOT OPERATE IN THE 'AUTOMATIC' OR THE  'MANUAL' MODE. |
| NCSA-0705_035.A05 REQUIREMENT 5d STATES  "THE SCAVENGER PUMP SWITCH VERIFIED |
| NOT TO BE IN THE 'MANUAL' MODE WHILE UNATTENDED." THE STATUS OF THE          |
| SCAVENGER PUMP SWITCH WAS IN  'AUTOMATIC' MODE BUT IT WAS IDENTIFIED WHEN    |
| TESTED THAT THE PUMP WOULD NOT OPERATE IN THE  'AUTOMATIC' OR THE 'MANUAL'   |
| MODE BUT WOULD OPERATE IN THE  'MANUAL BY-PASS'  MODE. THIS VIOLATES THE     |
| INTENT OF THE NCSA REQUIREMENT WHEREBY THE PUMP WOULD NOT START              |
| AUTOMATICALLY  NOR WAS THE PUMP MANNED IN THE 'MANUAL'  MODE. THE FACT THAT  |
| A TIME FRAME EXISTED WHEN THE PUMP WOULD NOT START IN THE 'AUTOMATIC'  MODE  |
| AND DURING THIS SAME TIME FRAME THE PUMP WAS NOT MANNED IN THE 'MANUAL'      |
| MODE CONSTITUTES A LOSS OF ONE CONTROL WHICH IS RELIED ON TO MEET THE DOUBLE |
| CONTINGENCY PRINCIPAL,                                                       |
|                                                                              |
| SAFETY SIGNIFICANCE OF EVENTS:                                               |
|                                                                              |
| LOW = The failure of the Scavenger Pump to operate In the automatic mode     |
| represents the loss of one control (5d) relied upon for double contingency.  |
| The failure of the Scavenger Pump to operate in the automatic mode would     |
| allow the Scavenger System Storage Tank to overflow and solution to collect  |
| on the floor of the basement The size of the floor area and the remaining    |
| control on the amount of solution transferred make a criticality nearly      |
| non-credible.                                                                |
|                                                                              |
| POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO(S) OF HOW            |
| CRITICALITY COULD OCCUR):                                                    |
|                                                                              |
| Six of eight Fissile Solution Storage Banks fail in such a way that all of   |
| the Fissile Solution collects in the tunnel basement floor. This is          |
| sufficient Fissile Solution to exceed the safe depth of 1.5 inches for       |
| solutions containing greater than 100 wt.% U-235.                            |
|                                                                              |
| CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.):     |
|                                                                              |
| Volume Control was lost when the Scavenger Pump failed. Geometry Control was |
| maintained throughout this event.                                            |
|                                                                              |
| ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS     |
| LIMIT AND % WORST CASE OP CRITICAL MASS):                                    |
|                                                                              |
| The Tunnel Storage System receives Fissile Solution for various operations   |
| in the X-705 Facility. The most likely form is UO2F2 in solution with a      |
| maximum enrichment of 100 wt.% U-235.                                        |
|                                                                              |
| NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION   |
| OF THE FAILURES OR DEFICIENCIES:                                             |
|                                                                              |
| Automatic Mode of Scavenger Pump failed. Pump not manned in Manual Mode, 5d  |
| Control lost. Note: Pump would operate in the Manual By-Pass Mode but the    |
| pump was unmanned. Since no Fissile Solution leaked and allowed >1.5 inches  |
| of solution to collect on the floor the second control was maintained.       |
|                                                                              |
| CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED:   |
|                                                                              |
| Entered Anomalous Condition. Assigned Operator to man the system until       |
| facility status was verified. Immediately verified no evolutions in progress |
| that could challenge the Scavenger System. Tagged out the power supplies to  |
| all facility equipment that could challenge the Scavenger System. Emergent   |
| Work authorized by Plant Shift Superintendent for repairs to Scavenger       |
| System. Called in off-duty Nuclear Criticality Safety Staff to assess        |
| compliance, create Anomalous Condition Report and oversee the efforts to     |
| establish the lost control. Control established at 2038 hours by manning the |
| pump controls.                                                               |
|                                                                              |
| The licensee notified the NRC Resident Inspector as well as the DOE          |
| representative.                                                              |
|                                                                              |
| * * * UPDATE 1808EST ON 3/14/01 FROM JOE HALCOMB TO S. SANDIN * * *          |
|                                                                              |
| The following update was submitted to clarify the above report:              |
|                                                                              |
| "03/14/01 - Update #1 - The Nuclear Criticality Safety (NCS) Group performed |
| a follow up assessment of the above event. A revision to the NCS Anomalous   |
| Condition Report was issued and it determined that the malfunction of the    |
| scavenger system did not constitute a loss of an NCS control and that double |
| contingency was maintained. The previous issue would not have been reported  |
| based on the revised NCS Anomalous Condition Report."                        |
|                                                                              |
| The licensee informed the NRC resident inspector and DOE site                |
| representative.  Notified R3DO(Wright) and NMSS(Hickey).                     |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   37835       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  SAINT VINCENT MEDICAL CENTER         |NOTIFICATION DATE: 03/14/2001|
|LICENSEE:  BEST INDUSTRIES                      |NOTIFICATION TIME: 09:17[EST]|
|    CITY:  BRIDGEPORT               REGION:  1  |EVENT DATE:        03/12/2001|
|  COUNTY:                            STATE:  CT |EVENT TIME:        17:00[EST]|
|LICENSE#:                        AGREEMENT:  N  |LAST UPDATE DATE:  03/14/2001|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |PETE ESELGROTH       R1      |
|                                                |KEVIN RAMSEY         NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  J. MELI                      |                             |
|  HQ OPS OFFICER:  JOHN MacKINNON               |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|CCCC 21.21               UNSPECIFIED PARAGRAPH  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| DEFECTIVE IODINE-125 SEEDS.                                                  |
|                                                                              |
| One hundred thirty-three (133) I-125 sources each with an activity of        |
| approximately 0.3 millicuries were received by the Saint Vincent Medical     |
| Center located in Bridgeport, CT.  The I-125 seeds are used for prostate     |
| implants.  Upon receiving the sources they were counted and the seeds'       |
| activity was checked.  They were then placed in a sterilization tray which   |
| has 10 wells (the seeds were distributed among the 10 wells).    The tray    |
| has a cover which allows for steam circulation.  The same day or the         |
| following morning the trays were sent forth to be sterilized.  After         |
| sterilization the seeds are taken out of the sterilizer and the sterilizer   |
| surveyed.  Nothing detectable was noted.  Later that day the seeds were      |
| removed from the wells and loaded into needles.  At the conclusion of this   |
| process the licensee did a survey of the area.  It was then when the         |
| licensee found a rather high level of radiation, not high enough to be a     |
| seed.  After further investigation the licensee concluded that the           |
| sterilization tray was contaminated and highly contaminated in the area of   |
| at least 5 of the 10 wells. The licensee's assumption is that one or more    |
| the seeds opened up during sterilization. The seeds were fine prior to       |
| sterilization.  Total estimated removable contamination found on the tray    |
| was 4 microcuries.    A more through survey was performed on everything that |
| had came in contact with the tray.  It was found that the inner wrapping     |
| that goes around the tray before it is placed in the sterilizer was          |
| contaminated.   Nothing else that had come in contact with the tray was      |
| found to be contaminated. Personnel do not seem to be contaminated.  The two |
| people who were involved in the loading process are scheduled to have        |
| thyroid uptake exams today.  This incident was reported to the seed          |
| manufacturer, Best Industries, and the seeds will be shipped back to them.   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37836       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SEABROOK                 REGION:  1  |NOTIFICATION DATE: 03/14/2001|
|    UNIT:  [1] [] []                 STATE:  NH |NOTIFICATION TIME: 13:11[EST]|
|   RXTYPE: [1] W-4-LP                           |EVENT DATE:        03/14/2001|
+------------------------------------------------+EVENT TIME:        10:30[EST]|
| NRC NOTIFIED BY:  HUGH HAWKINS                 |LAST UPDATE DATE:  03/14/2001|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |PETE ESELGROTH       R1      |
|10 CFR SECTION:                                 |                             |
|*PRE 50.72(b)(2)(xi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Hot Standby      |0        Hot Standby      |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION TO VARIOUS AGENCIES CONCERNING AN OIL SPILL ONSITE      |
|                                                                              |
| "At 10:30 AM on 3/14/2001 the following agencies were notified of an oil     |
| leak on site.                                                                |
|                                                                              |
| New Hampshire DES                                                            |
| National Response Center                                                     |
| US Coast Guard                                                               |
| Environmental Protection Agency (EPA)                                        |
|                                                                              |
| "About 1 gallon of oil was observed on top of a concrete pad near the        |
| vehicle maintenance shop. The oil came through the pad via cracks in the     |
| concrete. There is an oil line that runs under this pad from a 6000 gallon   |
| above ground tank. The tank has been isolated, local storm drains have been  |
| protected and a contractor is on site to excavate the area and determine the |
| extent of the problem. The notifications were made as a precautionary        |
| measure since the quantity of oil under the concrete pad is unknown.  The    |
| oil was first observed on 3/13/01 at approximately 1600."                    |
|                                                                              |
| The licensee informed the NRC resident inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Hospital                                         |Event Number:   37837       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  CHRISTIANA CARE HEALTH SERVICE       |NOTIFICATION DATE: 03/14/2001|
|LICENSEE:  CHRISTIANA CARE HEALTH SERVICE       |NOTIFICATION TIME: 13:15[EST]|
|    CITY:  WILMINGTON               REGION:  1  |EVENT DATE:        03/14/2001|
|  COUNTY:                            STATE:  DE |EVENT TIME:        07:10[EST]|
|LICENSE#:  07-12153-02           AGREEMENT:  N  |LAST UPDATE DATE:  03/14/2001|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |PETE ESELGROTH       R1      |
|                                                |FRITZ STURZ          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  EDWARD TORVIK                |                             |
|  HQ OPS OFFICER:  STEVE SANDIN                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|BAE1 20.2202(b)(1)       PERS OVEREXPOSURE      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 24-HOUR REPORT INVOLVING POTENTIAL PERSONNEL OVEREXPOSURE                    |
|                                                                              |
| At approximately 0710EST a technician at the Christiana Care Health Services |
| spilled a tube in the corner of the hot lab containing between 30-50 ml of   |
| Technetium-99m milked from the generator.  The activity was measured as 650  |
| millicuries immediately prior to the spill.  The hot lab was promptly        |
| evacuated. There was no personnel contamination involved.  Initial rad       |
| surveys of the affected area showed between 80 and 200 mr/hr prior to        |
| decontamination.  Following final decontamination measured rad levels taken  |
| at 1000EST were approximately 10 to 40 mr/hr.  Access to the lab has been    |
| restored, however, the corner area is taped off and covered by plastic to    |
| minimize the spread of contamination and allow for decay.                    |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37838       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: HATCH                    REGION:  2  |NOTIFICATION DATE: 03/14/2001|
|    UNIT:  [1] [] []                 STATE:  GA |NOTIFICATION TIME: 16:37[EST]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        03/09/2001|
+------------------------------------------------+EVENT TIME:        06:45[EST]|
| NRC NOTIFIED BY:  HARRY RUSSELL                |LAST UPDATE DATE:  03/14/2001|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |ROBERT HAAG          R2      |
|10 CFR SECTION:                                 |                             |
|*IND 50.72(b)(3)(v)(D)   ACCIDENT MITIGATION    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| HIGH PRESSURE COOLING INJECTION (HPCI) RENDERED INOPERABLE DUE TO FAULTY     |
| BATTERY CHARGER                                                              |
|                                                                              |
| "Investigation of the failure of battery charger 1R42-S031 on 3/9/2001       |
| (reference Condition Report 2001001827) has determined that the Unit 1 HPCI  |
| system was inoperable from the time of receipt of the first 'HPCI System     |
| Inverter Circuit Failure' annunciator until the time charger 1R42-S031 was   |
| removed from service. During this time (approximately 15 to 20 minutes), the |
| HPCI system inverter was tripping on high voltage and resetting              |
| automatically when voltage levels returned to normal. The voltage            |
| fluctuations causing the inverter to trip and reset were caused by an        |
| internal fault in charger 1R42-S031: a bad fuse was making intermittent      |
| connection resulting in intermittent firing of the charger's                 |
| silicon-controlled rectifiers (SCRs) and rapidly changing current and        |
| voltage outputs. These fluctuations and the random tripping of the HPCI      |
| system inverter rendered the HPCI system unreliable, and hence inoperable,   |
| until the cause of the fluctuations was corrected, that is, until the        |
| charger was removed from service. Determined to be reportable 3-14-2001 @    |
| 1338 EST."                                                                   |
|                                                                              |
| The licensee informed the NRC resident inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37839       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SUSQUEHANNA              REGION:  1  |NOTIFICATION DATE: 03/14/2001|
|    UNIT:  [] [2] []                 STATE:  PA |NOTIFICATION TIME: 18:02[EST]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        03/14/2001|
+------------------------------------------------+EVENT TIME:        15:08[EST]|
| NRC NOTIFIED BY:  ROBERT R. BOESCH             |LAST UPDATE DATE:  03/14/2001|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:                                |PETE ESELGROTH       R1      |
|10 CFR SECTION:                                 |                             |
|*ESF 50.72(b)(3)(iv)(A)  VALID SPECIF SYS ACTUAT|                             |
|*INB 50.72(b)(3)(v)(B)   POT RHR INOP           |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNIT 2 EXPERIENCED AN UNEXPECTED LOSS OF SHUTDOWN COOLING DUE TO TRIPPING OF |
| VARIOUS POWER SUPPLY BREAKERS                                                |
|                                                                              |
| "Unit 2 was in Mode 5 on the fifth day of its 10th Refuel and Inspection     |
| Outage. At 1508 hours, the unit experienced an unexpected loss of Division 1 |
| RPS Power supply. The loss of power was a result of the Electrical           |
| Protection Assembly (EPA) A & C breakers and motor generator output breaker  |
| tripping. The cause is under investigation.                                  |
|                                                                              |
| "The loss of power caused the RHR Shutdown Cooling suction valve HV251F009   |
| to close. This is a common suction valve to both divisions of RHR and        |
| resulted in the complete loss of RHR Shutdown Cooling. The reactor currently |
| has its head removed with the reactor cavity flooded up with the gates to    |
| the spent fuel pool removed. A Supplemental Decay Heat Removal system was in |
| service at the time, but was not considered fully capable of decay heat      |
| removal. Reactor coolant temperature increased less than 2 degrees during    |
| the 37 minutes SDC was out of service. The RPS power supply was switched to  |
| its alternate supply and SDC was restored at 1545 hours. In accordance with  |
| 10CFR50.72(b)(3)(v) this represents a loss of a safety system which removes  |
| residual heat and requires an 8 hour ENS call. In addition to the isolation  |
| of RHR SDC, RWCU isolated due to containment valve HV244F001 closing, and    |
| Unit 2 HVAC Zone 3 (refuel floor) isolated. These isolations constitute an   |
| actuation of a Containment Isolation signal that affected multiple systems,  |
| and is reportable per                                                        |
| 10CFR50.72(b)(3)(iv)(A)."                                                    |
|                                                                              |
| Peak temperature after losing SDC was 105 degrees. The licensee informed the |
| NRC resident inspector.                                                      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37840       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PEACH BOTTOM             REGION:  1  |NOTIFICATION DATE: 03/14/2001|
|    UNIT:  [2] [] []                 STATE:  PA |NOTIFICATION TIME: 20:13[EST]|
|   RXTYPE: [2] GE-4,[3] GE-4                    |EVENT DATE:        03/14/2001|
+------------------------------------------------+EVENT TIME:        14:10[EST]|
| NRC NOTIFIED BY:  ROSS MOONITZ                 |LAST UPDATE DATE:  03/14/2001|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |PETE ESELGROTH       R1      |
|10 CFR SECTION:                                 |                             |
|*IND 50.72(b)(3)(v)(D)   ACCIDENT MITIGATION    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| HPCI DECLARED INOPERABLE DUE TO FAILURE OF EXHAUST LINE VACUUM RELIEF VALVES |
| TO FUNCTION DURING IST TESTING                                               |
|                                                                              |
| "During routine testing of the Unit 2 High Pressure Coolant Injection system |
| (HPCI) exhaust line vacuum relief valves (VRV), it was discovered that both  |
| VRVs failed to open at their In Service Test (IST) required differential     |
| pressure value. The Unit 2 HPCI system has been declared inoperable and      |
| repairs are in progress.                                                     |
|                                                                              |
| "This event is being reported in accordance with 10CFR50.72(b)(3)(v)(D) due  |
| to a failure of a single train system which prevents fulfillment of a safety |
| function."                                                                   |
|                                                                              |
| With HPCI inoperable this places Unit 2 in a 14-day Limiting Condition of    |
| Operation.  All other ECCS systems have been verified operable.              |
|                                                                              |
| The licensee informed the NRC resident inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37841       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SAINT LUCIE              REGION:  2  |NOTIFICATION DATE: 03/14/2001|
|    UNIT:  [] [2] []                 STATE:  FL |NOTIFICATION TIME: 20:20[EST]|
|   RXTYPE: [1] CE,[2] CE                        |EVENT DATE:        03/14/2001|
+------------------------------------------------+EVENT TIME:        17:52[EST]|
| NRC NOTIFIED BY:  DAVE WILLIAMS                |LAST UPDATE DATE:  03/14/2001|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |ROBERT HAAG          R2      |
|10 CFR SECTION:                                 |                             |
|*RPS 50.72(b)(2)(iv)(B)  RPS ACTUATION - CRITICA|                             |
|*ESF 50.72(b)(3)(iv)(A)  VALID SPECIF SYS ACTUAT|                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     A/R        Y       100      Power Operation  |0        Hot Standby      |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNIT 2 EXPERIENCED A TURBINE TRIP - REACTOR TRIP ON LOSS OF LOAD             |
|                                                                              |
| "At 1752 hours on 3/14/01, the St. Lucie Unit 2 reactor automatically        |
| tripped on a turbine loss of load signal. Prior to the trip, the output      |
| breaker on the 2A Control Element Drive motor generator set opened for an    |
| unknown reason. Shortly thereafter, various Control Rod trouble alarms       |
| annunciated and the Control Rods dropped into the core due to loss of power  |
| on the Control Rod busses. The loss of power to the Control Rod busses       |
| initiated a turbine trip, which in turn generated a Reactor Protective       |
| System trip signal on loss of load. All Control Rods inserted fully.         |
| Standard Post Trip actions were completed satisfactorily with all safety     |
| functions met.                                                               |
|                                                                              |
| "Following the trip, it was noticed that the 2A1 non-safety related 6.9KV    |
| electric busses did not automatically transfer to the Startup Transformers.  |
| This resulted in the loss of power to the 2A1 and 2B2 Reactor Coolant Pumps  |
| and the 2A Main Feedwater pump. The cause for the failure to transfer is     |
| being investigated. Due to the loss of the Reactor Coolant Pumps, the        |
| Reactor Coolant System was manually depressurized to 1850 psia per plant     |
| procedures.                                                                  |
|                                                                              |
| "The Auxiliary Feedwater Actuation System automatically actuated on low      |
| Steam Generator level as expected for reactor trips from high power level.   |
| Steam Generator level is currently being maintained by the 2B Main Feedwater |
| pump.                                                                        |
|                                                                              |
| "The reactor is currently stable in Mode 3 and the cause of the trip is      |
| under investigation."                                                        |
|                                                                              |
| No primary safety or reliefs lifted during the transient.  Decay heat is     |
| being removed via the bypass valves to the main condenser.  The AFW pumps    |
| are operating but not supplying feed to the Steam Generators.  The licensee  |
| had not verified whether any atmospheric dumps cycled.  There is no known    |
| Steam Generator tube leakage at this time.  Normal offsite power remains     |
| available and there was no impact on Unit 1 which is operating at 100%       |
| power. Unit 2 will remain in Hot Standby pending development and completion  |
| of corrective actions. The licensee informed the NRC resident inspector.     |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Thursday, March 25, 2021