Event Notification Report for June 16, 2000
U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
06/15/2000 - 06/16/2000
** EVENT NUMBERS **
37084 37085 37086 37087 37088
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 37084 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 06/15/2000|
| UNIT: [1] [2] [] STATE: NC |NOTIFICATION TIME: 07:51[EDT]|
| RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 06/15/2000|
+------------------------------------------------+EVENT TIME: 06:57[EDT]|
| NRC NOTIFIED BY: JOE COSTA |LAST UPDATE DATE: 06/15/2000|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |RUDOLPH BERNHARD R2 |
|10 CFR SECTION: | |
|AESS 50.72(b)(1)(v) EMERGENCY SIREN INOP | |
|APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N Y 100 Power Operation |100 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| LOSS OF NINE EMERGENCY OFFSITE SIRENS DUE TO LOSS OF LOCAL POWER |
| |
| The licensee was notified that at 0657 EDT that nine of the offsite |
| emergency warning sirens were deenergized at 0408 EDT due to local power |
| outage and were inoperable for greater than one hour. Six were restored in |
| 1 hour and 16 minutes and the other three were restored in 2 hours and 16 |
| minutes. All sirens are now operable. |
| |
| The licensee notified the NRC Resident Inspector and the State authorities. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|General Information or Other |Event Number: 37085 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG: FLORIDA BUREAU OF RADIATION CONTROL |NOTIFICATION DATE: 06/15/2000|
|LICENSEE: PROFESSIONAL SERVICE INDUSTRIES INC |NOTIFICATION TIME: 10:25[EDT]|
| CITY: TAMPA REGION: 2 |EVENT DATE: 06/14/2000|
| COUNTY: STATE: FL |EVENT TIME: 09:00[EDT]|
|LICENSE#: 22-12 AGREEMENT: Y |LAST UPDATE DATE: 06/15/2000|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |RUDOLPH BERNHARD R2 |
| | |
+------------------------------------------------+ |
| NRC NOTIFIED BY: CHARLES ADAMS (FACSIMILE) | |
| HQ OPS OFFICER: BOB STRANSKY | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|NAGR AGREEMENT STATE | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT |
| |
| The State of Florida Bureau of Radiation Control reported that a Troxler |
| soil moisture/density gauge (Model 3430, Serial #30059), containing 8 mCi of |
| Cs-137 and 40 mCi of Am-241/Be, had been stolen from a state licensee. The |
| licensee reported that the gauge was stolen from a temporary job site |
| between the hours of 6 p.m. on 6/13/00 and 9 a.m. on 6/14/00. The chain link |
| fence surrounding the site was not damaged, but the door to the shed had |
| been pried open. The lock on the storage locker containing the container and |
| gauge had been cut. The gauge and container were the only items taken. The |
| Hillsborough Sheriff's Office and the Florida Bureau of Radiation Control |
| are investigating. The Sheriff's Office is planning to issue a press |
| release. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Hospital |Event Number: 37086 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG: SIOUX VALLEY HOSPITAL |NOTIFICATION DATE: 06/15/2000|
|LICENSEE: SIOUX VALLEY HOSPITAL |NOTIFICATION TIME: 13:52[EDT]|
| CITY: SIOUX FALLS REGION: 4 |EVENT DATE: 04/04/2000|
| COUNTY: STATE: SD |EVENT TIME: 12:30[MDT]|
|LICENSE#: 40-12378-01 AGREEMENT: N |LAST UPDATE DATE: 06/15/2000|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |LINDA SMITH R4 |
| |DON COOL NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: DOUG WARNER | |
| HQ OPS OFFICER: STEVE SANDIN | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|LADM 35.33(a) MED MISADMINISTRATION | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| PATIENT DID NOT RECEIVE THERAPEUTIC DOSE OF I-131 AS PRESCRIBED |
| |
| On 4/4/2000 at 1230 hours a patient undergoing treatment for thyroid cancer |
| did not receive the 100 mCi of I-131 as stated in the written instructions. |
| The Patient Appointment Center misinterpreted the instruction "100mCi I-131 |
| followed by a whole body scan" to mean "I-131 whole body scan." A |
| diagnostic administration of 4.26 mCi I-131 was given for the whole body |
| scan. The whole body scan results were reviewed and the prescribing |
| physician concluded that the therapeutic dose was not required. The patient |
| was informed. The Heath Physicist consultant to the hospital reviewed the |
| incident and advised the hospital that the error was recordable but not |
| reportable. This report is being made following an inspection by NRC Region |
| 4 (J. Cruz). |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 37087 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 06/15/2000|
| UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 21:54[EDT]|
| RXTYPE: [1] GE-6 |EVENT DATE: 06/15/2000|
+------------------------------------------------+EVENT TIME: 19:15[CDT]|
| NRC NOTIFIED BY: MARSHALL FUNKHOUSER |LAST UPDATE DATE: 06/15/2000|
| HQ OPS OFFICER: STEVE SANDIN +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |DAVID HILLS R3 |
|10 CFR SECTION: | |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| HIGH PRESSURE CORE SPRAY (HPCS) DECLARED INOPERABLE DUE TO INCOMPLETE POST |
| MODIFICATION TESTING OF IT'S ASSOCIATED DIESEL GENERATOR |
| |
| "At 1915 on 6/15/00 a Engineering review of a plant modification to the |
| Division 3 Diesel Generator (DG) determined that the Post Modification |
| Testing did not verify proper operation of the Loss of Off-Site Power (LOOP) |
| circuitry. This modification had only been performed to Division 3 DG and |
| therefore Division 1 and 2 DG's are not affected. Division 3 DG provides |
| power to the High Pressure Core Spray (HPCS) pump. The failure of Division 3 |
| DG to operate during a LOOP would have prevented HPCS from operating. The |
| loss of a single train safety system such as HPCS is reportable under |
| 10CFR50.72(b)(2)(iii)(D)." |
| |
| The plant modification involved rewiring the electrical circuit to correct |
| for a degraded voltage condition and was completed on 1/24/99. Post |
| modification testing was completed on 1/31/99. HPCS has been declared |
| inoperable but is available, if needed, pending completion of additional |
| testing. The licensee will inform the NRC Resident Inspector. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 37088 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SUMMER REGION: 2 |NOTIFICATION DATE: 06/15/2000|
| UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 22:10[EDT]|
| RXTYPE: [1] W-3-LP |EVENT DATE: 06/15/2000|
+------------------------------------------------+EVENT TIME: 21:37[EDT]|
| NRC NOTIFIED BY: DAN GOLDSTON |LAST UPDATE DATE: 06/15/2000|
| HQ OPS OFFICER: STEVE SANDIN +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |RUDOLPH BERNHARD R2 |
|10 CFR SECTION: | |
|ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |99 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| UNIT COMMENCED A CONTROLLED TECH SPEC REQUIRED SHUTDOWN TO MODE 2 FOR |
| REPAIRS |
| |
| "The 'C' steam generator Feedwater Isolation Valve, XVG1611C, air operator |
| developed an air leak and was declared inoperable 6/13/00 at 1549EDT. |
| Efforts to stop the leak were unsuccessful. At 2137EDT on 6/15/00 a |
| controlled power reduction to mode 2 was started. Current plans are to |
| repair the operator in mode 2 and return to power operation." |
| |
| The air leak is ongoing with the affected valve in use (open). The licensee |
| anticipates entering mode 2 by 0600EDT on 6/16/00 and has informed the NRC |
| Resident Inspector. |
+------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021