Event Notification Report for November 12, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           11/10/1999 - 11/12/1999

                              ** EVENT NUMBERS **

36331  36336  36338  36418  36419  36420  36421  36422  36423  36424  36425  36426 
36427  

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36331       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FT CALHOUN               REGION:  4  |NOTIFICATION DATE: 10/22/1999|
|    UNIT:  [1] [] []                 STATE:  NE |NOTIFICATION TIME: 13:04[EDT]|
|   RXTYPE: [1] CE                               |EVENT DATE:        10/22/1999|
+------------------------------------------------+EVENT TIME:        09:22[CDT]|
| NRC NOTIFIED BY:  ERICK MATZKE                 |LAST UPDATE DATE:  11/11/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |LINDA SMITH          R4      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - Steam Generator #RC-2A in Tech Spec Category C-3; Steam Generator          |
| inspections continuing -                                                     |
|                                                                              |
| At 0922 CDT on 10/22/99, during eddy current testing of the steam generators |
| (SG), it has been determined that 50 tubes in SG #RC-2A require plugging.    |
| This places SG #RC-2A in Technical Specification category C-3 per 3.17(2).   |
| Forty-four tubes have been determined to require plugging in SG #RC-2B at    |
| this time.  Eddy current testing is continuing on the SGs.  A 100% full      |
| length bobbin coil inspection program has been completed in both SGs.  A     |
| rotating pancake coil probe (Plus Point) is being used to inspect 100% of    |
| the top of the hot leg tube sheets for both SGs.  One hundred percent of     |
| these inspections for the 'A' SG are complete with about 99% evaluated.      |
| About 85% are complete on the 'B' SG with the rest expected to be completed  |
| on 10/22/99.  In addition, a large number of rotating pancake coil probe     |
| inspections are being conducted at other locations in the SGs.  In-situ      |
| pressure testing is being completed where needed.  To date, 4 tubes in the   |
| 'A' SG and 2 tubes in the 'B' SG have been pressure tested.  All 6 of these  |
| tubes have passed at 3 times normal operating differential pressure with     |
| zero leakage.                                                                |
|                                                                              |
| This report is conservatively being made prior to completing the SG testing  |
| and before completely evaluating the effect on the plant.  Further           |
| evaluation of reportability will be completed following the completion of    |
| the eddy current and in-situ pressure testing of the SGs.                    |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
|                                                                              |
| NOTE:  Refer to related Event #36338.                                        |
|                                                                              |
| * * * RETRACTION 0923 EST 11/9/1999 FROM MATZKE TAKEN BY STRANSKY * * *      |
|                                                                              |
| "Both steam generators were declared in category C-3 per Technical           |
| Specification 3.17 due to having greater than 1% of the inspected tubes      |
| being found defective. In steam generator RC-2A, 63 tubes were found         |
| defective out of 4901 inspected tubes. In steam generator RC-2B, 57 tubes    |
| were found defective out of 4905 inspected tubes.                            |
|                                                                              |
| "The technical specifications contain provisions for plugging tubes when     |
| they are found to contain defects that penetrate greater than 40%            |
| through-wall. Under this technical specification, it is expected that the    |
| plant may operate for a period of time with defects greater than 40%         |
| through-wall prior to being found and plugged. The tubes that were found to  |
| contain defects were plugged in accordance with technical specifications.    |
| The plugging criteria currently in use at Fort Calhoun Station requires that |
| all indications of corrosion detected by eddy current are plugged on         |
| detection due to the absence of a qualified technique for sizing             |
| indications.                                                                 |
|                                                                              |
| "Following eddy current testing of the steam generator tubes, in-situ        |
| pressure testing was performed on certain defects which exceeded the         |
| screening criteria. The criteria is based on the potential to exceed the     |
| performance criteria for leakage or structural integrity. The leakage        |
| performance criterion requires that leakage from all defects within a steam  |
| generator shall not exceed 1 gallon per minute under worst case accident     |
| differential pressure and the structural integrity performance criterion     |
| states that the tubes shall withstand pressure of up to three times normal   |
| operating differential pressure without burst. Selected indications which    |
| are representative of the worst of the population of indications found in    |
| the steam generators successfully passed in-situ pressure tests with no      |
| leakage at worst case accident differential pressure and no leakage at three |
| times normal operating differential pressure. There was no detectable        |
| primary-to-secondary leakage during operation prior to shutdown for the      |
| current refueling outage. Therefore, the steam generators were both          |
| available to perform their required safety functions as verified through     |
| in-situ pressure testing. Based on the testing performed, the tubes are not  |
| considered to have been seriously degraded, the plant was not in an          |
| unanalyzed condition, the steam generators would have performed their design |
| basis functions during accident conditions, and this did not constitute a    |
| condition outside the plant's operating and emergency procedures.            |
|                                                                              |
| "The original reports were made conservatively awaiting the completion of    |
| the inspection and testing program. The reports are now being retracted      |
| based on the complete testing results. The Fort Calhoun Station Technical    |
| Specification 30-day plugging report and 6-month inspection report will be   |
| submitted as required."                                                      |
|                                                                              |
| The NRC resident inspector has been informed of this retraction by the       |
| licensee. Notified R4DO (Smith).                                             |
|                                                                              |
| * * * UPDATE AT 1605 ON 11/11/99 MATZKE TO GOULD * * *  UNRETRACT A          |
| RETRACTION                                                                   |
|                                                                              |
| As a result of discussions with NRC personnel on 11/10/99, regarding         |
| reporting requirements, OPPD is withdrawing the retraction notification of   |
| 11/09/99, and changing the basis of the original notification to             |
| "voluntary".  This is because the reporting requirements of 10CFR50.72 were  |
| determined to be not applicable, and thus it is not clear that reporting     |
| pursuant to the technical specifications is required.  However, due to NRC   |
| desire for formal, prompt notification of this type of event and the absence |
| of explicit regulatory guidance, reporting on a voluntary basis appears      |
| appropriate.                                                                 |
|                                                                              |
| The 30 day steam generator tube plugging report to the NRC pursuant to       |
| Technical Specification 3.17(5)(i) has been sent.  The six month steam       |
| generator inspection report pursuant to Technical Specification 3.17(5)(ii)  |
| will be sent as required and will include the information requested in the   |
| second sentence of Technical Specification 3.17(5)(iii).                     |
|                                                                              |
| The licensess notified the NRC Resident Inspector.  The NRC Operations       |
| Officer notified R4DO (Linda Smith).                                         |
+------------------------------------------------------------------------------+

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36336       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: NINE MILE POINT          REGION:  1  |NOTIFICATION DATE: 10/22/1999|
|    UNIT:  [1] [] []                 STATE:  NY |NOTIFICATION TIME: 20:55[EDT]|
|   RXTYPE: [1] GE-2,[2] GE-5                    |EVENT DATE:        10/22/1999|
+------------------------------------------------+EVENT TIME:        19:55[EDT]|
| NRC NOTIFIED BY:  DON SHEEHAN                  |LAST UPDATE DATE:  11/10/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |WILLIAM COOK         R1      |
|10 CFR SECTION:                                 |                             |
|AOUT 50.72(b)(1)(ii)(B)  OUTSIDE DESIGN BASIS   |                             |
|NLCO                     TECH SPEC LCO A/S      |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       98       Power Operation  |98       Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - UNIT 1 IS OPERATING OUTSIDE ITS DESIGN BASIS IN ITS CURRENT OPERATING      |
| CONDITION -                                                                  |
|                                                                              |
| Unit 1 received information from its Engineering Department that Unit 1 is   |
| operating outside of design basis in its current operating condition.        |
| Specifically, with #11 Reactor Recirc Pump fully isolated, an analysis for   |
| thermal shock caused by initiation of #12 Emergency Cooling Loop injecting   |
| through #11 Reactor Recirc Loop suction nozzle has not been performed.       |
| Mitigating actions include isolating #12 Emergency Cooling Loop, in order to |
| return the plant to an analyzed condition, which requires that the plant     |
| enter a 7-Day Technical Specification Shutdown LCO until such time that an   |
| analysis for thermal shock has been performed.  Engineering Department has   |
| reasonable assurance that this analysis will be completed within the 7 days  |
| required by Unit 1 Tech Specs.                                               |
|                                                                              |
| All other Emergency Core Cooling System equipment is operable.               |
|                                                                              |
| This event has no effect on Unit 2.                                          |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
|                                                                              |
| * * * UPDATE AT 1349 ON 11/10/99 BY KIRCHNER TAKEN BY WEAVER * * *           |
|                                                                              |
| A licensee engineering supporting analysis has been performed which          |
| demonstrated that the plant has been operating within the design basis.      |
| Therefore, this event has been retracted.  The licensee notified the NRC     |
| resident inspector.  The NRC Operations Officer notified R1DO (Dan Holody).  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36338       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FT CALHOUN               REGION:  4  |NOTIFICATION DATE: 10/23/1999|
|    UNIT:  [1] [] []                 STATE:  NE |NOTIFICATION TIME: 20:59[EDT]|
|   RXTYPE: [1] CE                               |EVENT DATE:        10/23/1999|
+------------------------------------------------+EVENT TIME:        16:45[CDT]|
| NRC NOTIFIED BY:  KEVIN BOSTON                 |LAST UPDATE DATE:  11/11/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |LINDA SMITH          R4      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - Steam Generator #RC-2B is in Tech Spec Category C-3 -                      |
|                                                                              |
| In accordance with Tech Spec Section 3.17(5), Reporting Requirements, the    |
| following 4-hour non-emergency report is being made:                         |
|                                                                              |
| During eddy current testing of tubes of Steam Generator (SG) #RC-2B, greater |
| than 1% of the tubes tested were found to be defective.  The number of       |
| tested tubes during the 1999 refueling outage is 4905 in SG #RC-2B.  The     |
| number of tubes considered defective and require plugging exceeded 49        |
| tubes.                                                                       |
|                                                                              |
| SG #RC-2B was declared in Tech Spec 3.17, Table 3-13, Category C-3, at 1645  |
| CDT on 10/23/99.  Tube testing is being conducted under procedure            |
| SE-ST-RC-0003, Inservice Testing of Steam Generator Tubes.                   |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
|                                                                              |
| Note:  Refer to related Event #36331.                                        |
|                                                                              |
| *  *  * RETRACTION AT 0923 ON 11/09/99 FROM MATZKE TAKEN BY STRANSKY *  *    |
| *                                                                            |
|                                                                              |
| "Both steam generators were declared in Category C-3 per Technical           |
| Specification 3.17 due to having greater than 1% of the inspected tubes      |
| being found defective. In steam generator RC-2A, 63 tubes were found         |
| defective out of 4901 inspected tubes. In steam generator RC-2B, 57 tubes    |
| were found defective out of 4905 inspected tubes.                            |
|                                                                              |
| "The technical specifications contain provisions for plugging tubes when     |
| they are found to contain defects that penetrate greater than 40%            |
| through-wall. Under this technical specification, it is expected that the    |
| plant may operate for a period of time with defects greater than 40%         |
| through-wall prior to being found and plugged. The tubes that were found to  |
| contain defects were plugged in accordance with technical specifications.    |
| The plugging criteria currently in use at Fort Calhoun Station requires that |
| all indications of corrosion detected by eddy current are plugged on         |
| detection due to the absence of a qualified technique for sizing             |
| indications.                                                                 |
|                                                                              |
| "Following eddy current testing of the steam generator tubes, in-situ        |
| pressure testing was performed on certain defects which exceeded the         |
| screening criteria. The criteria is based on the potential to exceed the     |
| performance criteria for leakage or structural integrity. The leakage        |
| performance criterion requires that leakage from all defects within a steam  |
| generator shall not exceed 1 gallon per minute under worst case accident     |
| differential pressure and the structural integrity performance criterion     |
| states that the tubes shall withstand pressure of up to three times normal   |
| operating differential pressure without burst. Selected indications which    |
| are representative of the worst of the population of indications found in    |
| the steam generators successfully passed in-situ pressure tests with no      |
| leakage at worst case accident differential pressure and no leakage at three |
| times normal operating differential pressure. There was no detectable        |
| primary-to-secondary leakage during operation prior to shutdown for the      |
| current refueling outage. Therefore, the steam generators were both          |
| available to perform their required safety functions as verified through     |
| in-situ pressure testing. Based on the testing performed, the tubes are not  |
| considered to have been seriously degraded, the plant was not in an          |
| unanalyzed condition, the steam generators would have performed their design |
| basis functions during accident conditions, and this did not constitute a    |
| condition outside the plant's operating and emergency procedures.            |
|                                                                              |
| "The original reports were made conservatively awaiting the completion of    |
| the inspection and testing program. The reports are now being retracted      |
| based on the complete testing results. The Fort Calhoun Station Technical    |
| Specification 30-day plugging report and 6-month inspection report will be   |
| submitted as required."                                                      |
|                                                                              |
| The licensee notified the NRC Resident Inspector. The NRC Operations Officer |
| notified R4DO (Linda Smith).                                                 |
|                                                                              |
| *  *  * UPDATE AT 1605 ON 11/11/99 BY MATZKE TO GOULD * * *  UNRETRACT A     |
| RETRACTION                                                                   |
|                                                                              |
| As a result of discussions with NRC personnel on 11/10/99 regarding          |
| reporting requirements, OPPD is withdrawing the retraction notification of   |
| 11/09/99, and changing the basis of the original notification to             |
| "voluntary".  This is because the reporting requirements of 10CFR50.72 were  |
| determined to be not applicable, and thus it is not clear that reporting     |
| pursuant to the technical specifications is required.  However, due to NRC   |
| desire for formal, prompt notification of this type of event and the absence |
| of explicit regulatory guidance, reporting on a voluntary basis appears      |
| appropriate.                                                                 |
|                                                                              |
| The 30 day steam generator tube plugging report to the NRC pursuant to       |
| Technical Specification 3.17(5)(i) has been sent.  The six month steam       |
| generator inspection report pursuant to Technical Specification 3.17(5)(ii)  |
| will be sent as required and will include the information requested in the   |
| second sentence of Technical Specification 3.1 7(5)(iii).                    |
|                                                                              |
| The licensee notified the NRC Resident Inspector.  The NRC Operations        |
| Officer notified R4DO (Linda Smith).                                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   36418       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 11/10/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 14:33[EST]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        11/10/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:             [EST]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  11/10/1999|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |MICHAEL PARKER       R3      |
|  DOCKET:  0707002                              |JOHN HICKEY          NMSS    |
+------------------------------------------------+JOSEPH GIITTER       IRO     |
| NRC NOTIFIED BY:  ERIC SPAETH                  |                             |
|  HQ OPS OFFICER:  DOUG WEAVER                  |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NBNL                     RESPONSE-BULLETIN      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 4 HOUR BULLETIN 91-01 REPORT                                                 |
|                                                                              |
| On November 11, 1999 at 1020, the Nuclear Criticality Safety (NCS) staff     |
| determined that a Nuclear Criticality Safely Approval (NCSA) for X-705 was   |
| deficient.  The compressor turnover pit located in the equipment disassembly |
| north tear down area, has a sump pump which activates if solution should     |
| accumulate above 2.3 inches.  NCSA-0705_031.AOO analyzed the turnover pit,   |
| assuming a maximum enrichment of 3%.  The Nuclear Criticality Safety         |
| Evaluation (NCSE) for this operation failed to consider the contingency that |
| the Geometrically Safe Storage (GSS) located overhead, which was analyzed at |
| 100% enrichment, could leak into the compressor turnover pit.                |
|                                                                              |
| The licensee notified the NRC resident inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   36419       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  STATE OF LOUISIANA                   |NOTIFICATION DATE: 11/10/1999|
|LICENSEE:  MOORE & ASSOCIATES, INC.             |NOTIFICATION TIME: 16:00[EST]|
|    CITY:                           REGION:  4  |EVENT DATE:        11/10/1999|
|  COUNTY:  E. BATON ROUGE PAR.       STATE:  LA |EVENT TIME:        07:00[CST]|
|LICENSE#:                        AGREEMENT:  Y  |LAST UPDATE DATE:  11/10/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |LINDA SMITH          R4      |
|                                                |                             |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  TORY MEAUX                   |                             |
|  HQ OPS OFFICER:  DOUG WEAVER                  |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT - STOLEN MOISTURE/DENSITY GAUGE                       |
|                                                                              |
| The state of Louisiana reported that a Campbell moisture/density gauge,      |
| model MC3, serial number 6368, was stolen on 11/10/99.  The gauge was        |
| reported missing at 0700 CST on 11/10/99.  The gauge contains 10 �Ci of      |
| Cs-137 and a 50 �Ci AmBe source.  The gauge was stolen from the back of a    |
| truck at the offices of Moore & Associates.  The lock on the gauge had been  |
| cut.  The theft was reported to the local and state police departments.      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36420       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: HATCH                    REGION:  2  |NOTIFICATION DATE: 11/10/1999|
|    UNIT:  [1] [2] []                STATE:  GA |NOTIFICATION TIME: 17:39[EST]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        11/10/1999|
+------------------------------------------------+EVENT TIME:        15:49[EST]|
| NRC NOTIFIED BY:  BARRY COLEMAN                |LAST UPDATE DATE:  11/10/1999|
|  HQ OPS OFFICER:  DOUG WEAVER                  +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHARLES OGLE         R2      |
|10 CFR SECTION:                                 |                             |
|HFIT 26.73               FITNESS FOR DUTY       |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| FITNESS FOR DUTY REPORT                                                      |
|                                                                              |
| A supervisory contract employee was found to have used two illegal drugs     |
| during a random drug screening.                                              |
| The NRC resident inspector has been notified.                                |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36421       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BRUNSWICK                REGION:  2  |NOTIFICATION DATE: 11/10/1999|
|    UNIT:  [1] [2] []                STATE:  NC |NOTIFICATION TIME: 19:09[EST]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        11/10/1999|
+------------------------------------------------+EVENT TIME:        18:15[EST]|
| NRC NOTIFIED BY:  DAN HARDIN                   |LAST UPDATE DATE:  11/10/1999|
|  HQ OPS OFFICER:  DOUG WEAVER                  +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHARLES OGLE         R2      |
|10 CFR SECTION:                                 |                             |
|DDDD 73.71               UNSPECIFIED PARAGRAPH  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| SECURITY REPORT                                                              |
|                                                                              |
| UNESCORTED ACCESS GRANTED INAPPROPRIATELY.   IMMEDIATE CORRECTIVE ACTIONS    |
| TAKEN UPON DISCOVERY.  THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR.     |
| SEE THE HOO LOG FOR ADDITIONAL DETAILS.                                      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36422       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DUANE ARNOLD             REGION:  3  |NOTIFICATION DATE: 11/10/1999|
|    UNIT:  [1] [] []                 STATE:  IA |NOTIFICATION TIME: 21:27[EST]|
|   RXTYPE: [1] GE-4                             |EVENT DATE:        11/10/1999|
+------------------------------------------------+EVENT TIME:        19:10[CST]|
| NRC NOTIFIED BY:  DICK FOWLER                  |LAST UPDATE DATE:  11/10/1999|
|  HQ OPS OFFICER:  DOUG WEAVER                  +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MICHAEL PARKER       R3      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| INTERGRANULAR STRESS CORROSION CRACKING IDENTIFIED ON RECIRCULATION RISER    |
| WELD                                                                         |
|                                                                              |
| While performing ultrasonic examination of recirculation riser weld          |
| #RRF-F002, nozzle to safe end weld, indications of Intergranular Stress      |
| Corrosion Cracking (IGSCC) were identified.  Specifically, a 0.3 inch X 13   |
| inch long crack on the nozzle to safe end weld.   This nozzle was being      |
| inspected as part of an expanded inspection scope as a result of similar     |
| indications found on the 'B' recirc riser to safe end weld.  To date,        |
| indications have been found on the 'B', 'D', and 'F' nozzles with no         |
| indications on the 'A' and 'C' nozzles.  The 'E', 'G' and 'H' inspections    |
| have not been completed.                                                     |
|                                                                              |
| The licensee notified the NRC resident inspector.                            |
|                                                                              |
| See events #36402 and #36416.                                                |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   36423       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 11/10/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 22:02[EST]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        11/09/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        23:15[EST]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  11/10/1999|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |MICHAEL PARKER       R3      |
|  DOCKET:  0707002                              |ROBERT PIERSON       NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  JEFF CASTLE                  |                             |
|  HQ OPS OFFICER:  DOUG WEAVER                  |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NBNL                     RESPONSE-BULLETIN      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 24 HOUR BULLETIN 91-01 REPORT                                                |
|                                                                              |
| At 2315 on 11/09/99, a maintenance mechanic in the X-330 building identified |
| four pieces of equipment which violated NCSA-PLANT062.A02 requirement #4     |
| which states "Openings / penetrations made during maintenance activities     |
| shall be covered to minimize the potential for moderator collection and      |
| moist air exposure when unattended".  The violations were corrected by       |
| repairing or replacing the damaged covers by 0218 on 11/10/99.   One         |
| additional violation of the NCSA requirement was identified during followup  |
| facility walkdowns.   The additional piece of equipment was discovered in    |
| the X-330 building at 1030 on 11/10/99.  This deficiency was corrected at    |
| 1259 on 11/10/99.  This constitutes a loss of control such that only one     |
| double contingency control remains in place.                                 |
|                                                                              |
| The licensee notified the NRC resident inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36424       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BYRON                    REGION:  3  |NOTIFICATION DATE: 11/11/1999|
|    UNIT:  [] [2] []                 STATE:  IL |NOTIFICATION TIME: 03:06[EST]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        11/10/1999|
+------------------------------------------------+EVENT TIME:        22:20[CST]|
| NRC NOTIFIED BY:  MARRI MARCHIONDA             |LAST UPDATE DATE:  11/11/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MICHAEL PARKER       R3      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - S/G  LEVEL DROPPED TO REACTOR TRIP/AFW AUTO START SETPOINT DURING          |
| MAINTENANCE -                                                                |
|                                                                              |
| At 2220 CST on 11/10/99 with Unit 2 in Mode 5 (Cold Shutdown), priming of    |
| the feedwater isolation valves to support maintenance activities was in      |
| progress.  While priming the 'B' steam generator (S/G) feedwater isolation   |
| valve #2FW009B, the valve was opened and water back-flowed from the 'B' S/G  |
| into the feedwater piping and the S/G level decreased to the low level 2     |
| reactor trip setpoint of 36.3% which is also the setpoint for the autostart  |
| of the auxiliary feedwater (AFW) system.  The initial level in the 'B' S/G   |
| was 50%.  A reactor protection system actuation and engineered safety        |
| features actuation occurred and all plant systems responded normally for     |
| Mode 5.  The reactor trip breakers opened but the control rod drive system   |
| was out of service and not capable of control rod withdrawal.  The AFW       |
| auxiliary lube oil pumps auto started but the AFW pumps were in pull-to-lock |
| due to current plant conditions so the AFW pumps did not start.  The cause   |
| of the level decrease is due to unfilled feedwater piping following outage   |
| restoration.  Corrective action is being determined.  This event is          |
| reportable under the requirements of 10CFR50.72(b)(2)(ii).                   |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36425       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FERMI                    REGION:  3  |NOTIFICATION DATE: 11/11/1999|
|    UNIT:  [2] [] []                 STATE:  MI |NOTIFICATION TIME: 09:59[EST]|
|   RXTYPE: [2] GE-4                             |EVENT DATE:        11/11/1999|
+------------------------------------------------+EVENT TIME:        07:15[EST]|
| NRC NOTIFIED BY:  MIKE PHILIPPON               |LAST UPDATE DATE:  11/11/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MICHAEL PARKER       R3      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|2     N          Y       97       Power Operation  |97       Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - REACTOR WATER CLEANUP SYSTEM ISOLATION DUE TO HIGH DIFFERENTIAL            |
| TEMPERATURE -                                                                |
|                                                                              |
| A Reactor Water Cleanup (RWCU) System steam leak detection high differential |
| temperature alarm was received and the subsequent isolation of the outboard  |
| isolation valves #G33F004 and #G33F220 occurred.  The reactor building was   |
| immediately evacuated and access was restricted as a precaution until the    |
| cause of the high temperature alarm and RWCU System isolation could be       |
| determined.  Although it was confirmed that there was no steam leak, the     |
| RWCU System isolation signal was considered valid because an actual high     |
| differential temperature condition existed.  The valid isolation signal was  |
| a result of a trip of the Reactor Building HVAC System and the failure of    |
| the RWCU pump 'B' room cooler to automatically start on high room            |
| temperature.  Investigation revealed that the thermal overloads on the RWCU  |
| room cooler were tripped.  The Reactor Building HVAC System had tripped on   |
| low freezstat (temperature switch) temperature.  All other systems operated  |
| as expected, and the RWCU System remains shut down pending investigation of  |
| the failure of the 'B' room cooler to start.                                 |
|                                                                              |
| The NRC Resident Inspector was notified by the licensee.                     |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36426       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PALISADES                REGION:  3  |NOTIFICATION DATE: 11/11/1999|
|    UNIT:  [1] [] []                 STATE:  MI |NOTIFICATION TIME: 11:18[EST]|
|   RXTYPE: [1] CE                               |EVENT DATE:        11/10/1999|
+------------------------------------------------+EVENT TIME:        14:00[EST]|
| NRC NOTIFIED BY:  STEVE ELLIS                  |LAST UPDATE DATE:  11/11/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MICHAEL PARKER       R3      |
|10 CFR SECTION:                                 |                             |
|HFIT 26.73               FITNESS FOR DUTY       |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - TWO EMPTY BEER CANS FOUND IN A TRAILER INSIDE THE PLANT PROTECTED AREA -   |
|                                                                              |
| Plant janitors found two empty beer cans in a shower trailer in a            |
| maintenance workers area inside the plant protected area.  The licensee is   |
| interviewing the janitors and searched the trailer for additional cans; none |
| were found.  The licensee sent the cans to the local police for possible     |
| identification of fingerprints; results are pending.  The licensee searched  |
| the hand held items of people exiting the plant protected area; nothing      |
| unusual was found.  The licensee notified the NRC Resident Inspector and is  |
| continuing to investigate this incident.                                     |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36427       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: ARKANSAS NUCLEAR         REGION:  4  |NOTIFICATION DATE: 11/11/1999|
|    UNIT:  [] [2] []                 STATE:  AR |NOTIFICATION TIME: 17:53[EST]|
|   RXTYPE: [1] B&W-L-LP,[2] CE                  |EVENT DATE:        11/11/1999|
+------------------------------------------------+EVENT TIME:        16:45[CST]|
| NRC NOTIFIED BY:  SCOTT                        |LAST UPDATE DATE:  11/11/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |LINDA SMITH          R4      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| FAILURE OF INSIDE AND OUTSIDE CCW CONTAINMENT ISOLATION VALVES.              |
|                                                                              |
| ON 11/09/99, WHILE IN MODE 5, COLD SHUTDOWN, FOR MID-CYCLE OUTAGE, THE       |
| OUTSIDE CONTAINMENT ISOLATION VALVE FOR COMPONENT COOLING WATER (CCW) RETURN |
| (2CV-5255-1) FAILED TO FULLY CLOSE BASED ON FLOW NOISE DURING THE INITIAL    |
| STROKE. THE VALVE WAS STROKED 10 TIMES AND APPEARED TO CLOSE ON ALL STROKES  |
| FOLLOWING THE INITIAL ATTEMPT.  ON 11/10/99, THE INSIDE CONTAINMENT          |
| ISOLATION VALVE FOR CCW RETURN (2CV-5254-2) FAILED TO REACH THE TRAVEL LIMIT |
| ON ITS FIRST STROKE.  AN IMPROMPTU LEAK TEST USING WATER WITH 2CV-5254-2 IN  |
| ITS INITIAL POSITION INDICATED 300-500 ML/MIN LEAKAGE VIA THE VALVE SEAT.    |
| BOTH VALVES WERE OVERHAULED DURING THE REFUELING OUTAGE IN EARLY 1999 AND    |
| SUCCESSFULLY PASSED POST-MAINTENANCE TESTING. DETERMINATION OF THE CAUSE(S)  |
| AND RESTORATION OF BOTH VALVES TO AN OPERABLE STATUS WILL BE COMPLETED       |
| BEFORE PLANT STARTUP.  THERE DOES NOT APPEAR TO BE FIRM EVIDENCE CONCERNING  |
| A TIME OF FAILURE BEFORE THE CONDITIONS WERE DISCOVERED.  ON NOVEMBER 11,    |
| 1999, DURING A REVIEW OF THESE CONDITIONS AFFECTING THE SAME CONTAINMENT     |
| PENETRATION, IT WAS DETERMINED THAT THEY MET THE REPORTING CRITERION OF      |
| 10CFR5O.72(b)(2)(I) AS A SERIOUS DEGRADATION OF A PRINCIPAL SAFETY BARRIER   |
| (REACTOR CONTAINMENT) FOUND WHILE SHUTDOWN.                                  |
|                                                                              |
| THE RESIDENT INSPECTOR WAS NOTIFIED.                                         |
+------------------------------------------------------------------------------+


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