Event Notification Report for November 3, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           11/02/1999 - 11/03/1999

                              ** EVENT NUMBERS **

35790  36385  36386  36387  36388  36389  

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   35790       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT      |NOTIFICATION DATE: 06/03/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 14:44[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        06/02/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        16:30[CDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  11/02/1999|
|    CITY:  PADUCAH                  REGION:  3  +-----------------------------+
|  COUNTY:  McCRACKEN                 STATE:  KY |PERSON          ORGANIZATION |
|LICENSE#:  GDP-1                 AGREEMENT:  Y  |DAVID HILLS          R3      |
|  DOCKET:  0707001                              |DON COOL             NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  THOMAS WHITE                 |                             |
|  HQ OPS OFFICER:  FANGIE JONES                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|OCBA 76.120(c)(2)(i)     ACCID MT EQUIP FAILS   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| THREE SPRINKLER SYSTEMS DECLARED INOPERABLE DUE TO CORRODED HEADS (24-hour   |
| report)                                                                      |
|                                                                              |
| "On 06/02/99 at 1630 CDT, the Plant Shift Superintendent (PSS) was notified  |
| that numerous sprinkler heads were corroded, affecting 16 sprinkler systems  |
| in C-337 and one system in C-333, such that the ability of the sprinklers to |
| flow sufficient water was called into question.  Subsequently, these         |
| sprinkler systems were declared inoperable, and TSR-required actions         |
| establishing roving fire patrols were initiated.  This deficiency was        |
| detected during scheduled system inspections conducted by Fire Protection    |
| personnel.  Currently, functionality of the sprinkler heads has not been     |
| fully evaluated by Fire Protection personnel, and the remaining cascade      |
| buildings are currently being inspected, and if necessary, this report will  |
| be updated to identify any additional areas.  It has been determined that    |
| this event is reportable under 10CFR76.120(c)(2) as an event in which        |
| equipment is disabled or fails to function as designed."  The NRC resident   |
| inspector has been notified of this event.                                   |
|                                                                              |
| * * * UPDATE AT 1022 EDT ON 06/04/99 FROM CAGE TO TROCINE * * *              |
|                                                                              |
| "Two sprinkler heads on system D-1 in C-337 and two sprinkler heads on       |
| system 27 in C-335 were identified to also be corroded.  These were          |
| identified to the PSS on 06/03/99 at 1600 CDT and 1601 CDT, respectively,    |
| and determined to require an update to this report by the PSS.  It has been  |
| determined that this event is reportable under 10CFR76.120(c)(2) as an event |
| in which equipment is disabled or fails to function as designed."  Paducah   |
| personnel notified the NRC resident inspector of this update.  The NRC       |
| operations officer notified the R3DO (Hills) and NMSS EO (Combs).            |
|                                                                              |
| * * * UPDATE AT 2152 EDT ON 06/17/99 FROM WALKER TO POERTNER * * *           |
|                                                                              |
| "Three sprinkler heads on system C-15 and five sprinkler heads on system B-8 |
| in C-333 were identified to also be corroded.  The PSS was notified of this  |
| condition at 1300 CDT on 06/17/99 and determined that an update to this      |
| report was required.  It has been determined that this event is reportable   |
| under 10CFR76.120(c)(2) as an event in which equipment is disabled or fails  |
| to function as designed."  Paducah personnel notified the NRC resident       |
| inspector of this update.  The NRC operations officer notified the R3DO      |
| (Madera).                                                                    |
|                                                                              |
| * * * UPDATE 1440 EDT 6/18/1999 FROM UNDERWOOD TAKEN BY STRANSKY * * *       |
|                                                                              |
| "Two sprinkler heads on system C-15 and one sprinkler head on system B-8 in  |
| C-333 were identified to have corrosion.  The PSS was notified of this       |
| condition at 1350 CDT on 06/18/99.  The area of the fire patrol for system   |
| C-15 was expanded to include the two heads identified as corroded.  The one  |
| head on system B-8 was in the area already being patrolled.  The PSS         |
| determined that an update to this report was required."  The NRC resident    |
| inspector has been informed of this update.  Notified R3DO (Madera).         |
|                                                                              |
| * * * UPDATE 1315 EDT 6/25/1999 FROM WALKER TAKEN BY STRANSKY * * *          |
|                                                                              |
| "Two sprinkler heads on system D-8 and three sprinkler heads on system D-7   |
| in C-337 were identified to have corrosion.  The PSS was notified of the     |
| condition on system D-8 at 0125 CDT on 06/25/99 and at 1019 CDT on 06/25/99  |
| for system D-7.  Both systems were immediately declared inoperable and LCO   |
| fire patrol actions were implemented.  It was determined that an update to   |
| this report was required."  The NRC resident inspector has been informed of  |
| this update.  Notified R3DO (Jordan).                                        |
|                                                                              |
| * * * UPDATE 2119 EDT 7/30/1999 FROM CAGE TAKEN BY STRANSKY * * *            |
|                                                                              |
| "Five sprinkler heads and one sprinkler piping tee on C-337 system D-7 were  |
| identified to have corrosion. The PSS was notified of these corroded system  |
| parts and declared the system inoperable at 0931 CDT on 07/30/99.  LCO       |
| required fire patrols of the affected area were initiated.  The PSS          |
| determined that an update to this event report was required."  The NRC       |
| resident inspector has been informed of this update.  Notified R3DO          |
| (Wright).                                                                    |
|                                                                              |
| * * * UPDATE AT 1655 EDT ON 07/31/99 FROM WHITE TAKEN BY STRANSKY * * *      |
|                                                                              |
| "Two sprinkler heads on C-337 System D-1 were identified to have corrosion.  |
| The PSS was notified of these corroded system parts and declared the system  |
| inoperable at 1155 CDT on 7/31/99.  LCO required fire patrols of the         |
| affected area were initiated.  The PSS determined that an update to this     |
| report was required."  The NRC resident inspector has been informed of this  |
| update.  Notified R3DO (Wright).                                             |
|                                                                              |
| * * * UPDATE AT 1546 EDT ON 08/10/99 FROM WHITE TAKEN BY STRANSKY * * *      |
|                                                                              |
| "Two sprinkler heads on C-337 system C-15 were identified to have corrosion. |
| The PSS was notified of these corroded system parts and declared the system  |
| inoperable at 1130 CDT on 8/10/99.  LCO required fire patrols of the         |
| affected area were initiated.  The PSS determined that an update to this     |
| report was required."  The NRC resident inspector has been informed of this  |
| update.  Notified R3DO (Burgess).                                            |
|                                                                              |
| * * * UPDATE AT 1154 EDT ON 08/22/99 FROM WALKER TO POERTNER * * *           |
|                                                                              |
| Four adjacent sprinkler heads on the C-333 building System B-1 were          |
| identified to have corrosion.  The PSS was notified of the corroded system   |
| parts and declared the system inoperable at 0918 CDT on 08/22/99.  LCO       |
| required fire patrols were initiated.  The NRC Resident Inspector will be    |
| notified.  The NRC Operations Officer notified the R3DO (Clayton).           |
|                                                                              |
| * * * UPDATE 2015 EDT ON 08/28/99 FROM W. F. GAGE TO S. SANDIN * * *         |
|                                                                              |
| Two adjacent sprinkler heads on the C-337 building System D-11 were          |
| identified to have corrosion.  The PSS was notified of these corroded system |
| parts and declared the system inoperable at 1420 CDT on 08/28/99.   LCO      |
| required fire patrols of the affected area were initiated.  Paducah          |
| personnel informed the NRC Resident Inspector.  The NRC Operations Officer   |
| notified the R3DO (Leach) and NMSS EO (Piccone).                             |
|                                                                              |
| * * * UPDATE 2037 EDT ON 08/29/99 FROM KEVIN BEASLEY TO S. SANDIN * * *      |
|                                                                              |
| Two adjacent sprinkler heads on the C-337 building System D-15 were          |
| identified to have corrosion and the PSS declared the system inoperable at   |
| 0925 CDT on 08/29/99.  Also two adjacent heads on the C-337 building System  |
| D-10 were identified to have corrosion and the PSS declared the system       |
| inoperable at 1450 CDT.   LCO required fire patrols for both of the affected |
| areas were initiated in the time frame required by TSR.  Paducah personnel   |
| informed the NRC Resident Inspector.  The NRC Operations Officer notified    |
| the R3DO (Leach) and NMSS EO (Piccone).                                      |
|                                                                              |
| * * * UPDATE AT 0930 EDT ON 09/01/99  BY ERIC WALKER TO FANGIE JONES * * *   |
|                                                                              |
| Add two adjacent sprinkler heads on the C-337 building System D-14 were      |
| declared inoperable.  Paducah personnel informed the NRC Resident Inspector. |
| The NRC Operations Officer notified the R3DO (David Hills) and NMSS (Robert  |
| Pierson).                                                                    |
|                                                                              |
| * * * UPDATE AT 1133 EDT ON 09/08/99  BY TOM WHITE TO FANGIE JONES * * *     |
|                                                                              |
| Add two adjacent sprinkler heads on the C-331 building System 26 were        |
| declared inoperable at 2155 CDT on 09/07/99.  An LCO required fire patrol    |
| for the affected area was initiated in the time frame required by the TSR.   |
| Paducah personnel informed the NRC Resident Inspector.  The NRC Operations   |
| Officer notified the R3DO (Monte Phillips) and NMSS (Josie Piccone).         |
|                                                                              |
| * * * UPDATE AT 0948 ON 09/30/99 BY ERIC WALKER TO DOUG WEAVER * * *         |
|                                                                              |
| Add two adjacent sprinkler heads on the C-333 building System B-15 were      |
| identified to have corrosion and the PSS declared the system inoperable at   |
| 0815 CDT on 9/30/99.  An LCO required fire patrol for the affected area was  |
| initiated in the time frame required by the TSR.  Paducah personnel informed |
| the NRC Resident Inspector.   The NRC operations officer notified the R3DO   |
| (Vegel) and NMSS (Cool).                                                     |
|                                                                              |
| * * * UPDATE AT 1600 ON 10/13/99 BY WALKER TO GOULD * * *                    |
|                                                                              |
| Two adjacent sprinkler heads on the C-333 building System A-11 were          |
| Identified to have corrosion and the PSS declared the system inoperable at   |
| 1307 CDT on 10/13/99.  An LCO required fire patrol for the affected area was |
| initiated in the time frame required by the TSR.  Paducah personnel informed |
| the NRC Resident Inspector.   The NRC operations officer notified the R3DO   |
| (Madera) and NMSS (Moore).                                                   |
|                                                                              |
| * * * UPDATE AT 1520 ON 10/19/99 FROM UNDERWOOD TAKEN BY STRANSKY * * *      |
|                                                                              |
| Six sprinkler heads on the C-337 building System D-16 were identified to     |
| have corrosion and the PSS declared the system inoperable at 1052 CDT on     |
| 10/19/99.  An LCO required fire patrol for the affected area was initiated   |
| in the time frame required by the TSR.  The NRC Resident Inspector has been  |
| informed of this update.  The NRC Operations Officer notified R3DO           |
| (Jorgensen).                                                                 |
|                                                                              |
| * * * UPDATE AT 2140 ON 10/19/99 FROM WALKER TAKEN BY STRANSKY * * *         |
|                                                                              |
| Seven sprinkler heads on the C-337 building System A-7 were identified to    |
| have corrosion, and another four had been painted over.  In addition, three  |
| adjacent sprinkler heads on the C-337 building System A-8 were identified to |
| have corrosion.  The PSS declared the systems inoperable at 1900 CDT on      |
| 10/19/99.  An LCO required fire patrols for the affected areas were          |
| initiated in the time frame required by the TSR.  The NRC Resident Inspector |
| has been informed of this update.  The NRC Operations Officer notified R3DO  |
| (Wright).                                                                    |
|                                                                              |
| * * * UPDATE AT 1713 ON 10/21/99 FROM CAGE TAKEN BY JOLLIFFE * * *           |
|                                                                              |
| Four sprinkler heads on the C-337 building System A-5, twelve sprinkler      |
| heads on the C-337 building System A-8, three sprinkler heads on the C-337   |
| building System A-9, and six sprinkler heads on the C-337 building System    |
| B-8 were identified to have corrosion.  On 10/21/99, the PSS declared        |
| Systems A-5 and A-9 inoperable at 1028 CDT, System A-8 inoperable at 1227    |
| CDT and System B-8 inoperable at 1406 CDT.   An LCO required fire patrol for |
| the affected areas was initiated in the time frame required by the TSR..     |
| The NRC Resident Inspector has been informed of this update.  The NRC        |
| Operations Officer notified the R3DO Bruce Jorgensen.                        |
|                                                                              |
| * * * UPDATE AT 2128 ON 10/22/99 FROM ERIC WALKER TAKEN BY JOLLIFFE * * *    |
|                                                                              |
| At 1400 CDT on 10/22/99, the PSS was notified that numerous corroded         |
| sprinkler heads were discovered in the C-337 building on sprinkler systems   |
| B-1, B-3, B-5, B-6, B-7, B-11 and D-17.  Due to the number of systems called |
| into question, the PSS declared all of the sprinkler systems in C-337 on the |
| cell floor (a total of 66 systems) inoperable and TSR required actions       |
| establishing roving fire patrols were initiated within the required time     |
| frame.  The NRC Resident lnspector has been informed of this update.  The    |
| NRC Operations Officer notified the R3DO Bruce Jorgensen.                    |
|                                                                              |
| * * * UPDATE AT 1239 ON 10/24/99 FROM TOM WHITE TAKEN BY JOLLIFFE * * *      |
|                                                                              |
| At 1200 CDT on 10/23/99, the PSS was notified that numerous corroded         |
| sprinkler heads were discovered in the C-337 building on sprinkler systems   |
| B-13 and B-14 on the ground floor,  The PSS declared these systems           |
| inoperable and TSR required actions establishing roving fire patrols were    |
| initiated within the required time frame.  At 1600 CDT on 10/23/99, the PSS  |
| was notified that numerous corroded sprinkler heads were discovered in the   |
| C-337 building on sprinkler systems A-16, B-12, C-8, C-12, C-15, D-5 and D-8 |
| on the cell floor,  These systems have already been declared inoperable and  |
| fire patrols are already being performed.  The NRC Resident Inspector has    |
| been notified of this update.  The NRC Operations Officer notified the R3DO  |
| Bruce Jorgensen.                                                             |
|                                                                              |
| * * * UPDATE AT 1117 ON 10/25/99 FROM W. F. CAGE TAKEN BY SANDIN * * *       |
|                                                                              |
| At 1940 CDT on 10/24/99, the PSS was notified that numerous corroded         |
| sprinkler heads had been discovered on High Pressure Fire Water Systems C-4, |
| C-5, C-6 and C-8, located in the C-337 building.  These systems had          |
| previously been declared inoperable and fire patrols were already being      |
| performed at the time of discovery.  The NRC Resident Inspector has been     |
| notified of this update.  The NRC Operations Officer notified R3DO           |
| (Lanksbury) and NMSS (Brain Smith).                                          |
|                                                                              |
| * * * UPDATE AT 2235 ON 10/27/99 BY WHITE TAKEN BY MACKINNON * * *           |
|                                                                              |
| At 1517 CDT on 10/27/99, the PSS was notified that nine corroded sprinkler   |
| heads had been discovered on High Pressure Fire Water System A-12 located in |
| the C-333 building.  This system has been declared inoperable and fire       |
| patrols have been initiated.  The NRC Resident Inspector has been notified   |
| of this update.  The NRC Operations Officer notified R3DO (Jordan) and NMSS  |
| EO (Hickey).                                                                 |
|                                                                              |
| * * * UPDATE AT 2150 ON 10/30/99 BY UNDERWOOD TAKEN BY WEAVER * * *          |
|                                                                              |
| At 1950 CDT on 10/30/99, the PSS was notified that numerous corroded         |
| sprinkler heads had been discovered on High Pressure Fire Water Systems A-5, |
| A-9, A-11, C-5, and C-7 in the C-333 building.  Reference ATR-1 1999-6699    |
| and 6702.  These systems have been declared inoperable and fire patrols have |
| been initiated.  Also, due to the number of inoperable sprinkler heads, the  |
| remaining systems on the cell floor of C-333 were called into question and   |
| declared inoperable.  Fire patrols for the entire cell floor have been       |
| initialed.  The PSS determined that an update to this report was required.   |
| The NRC Resident Inspector has been notified of this update.  The NRC        |
| Operations Officer notified R3DO (Jordan) and NMSS EO (Hickey).              |
|                                                                              |
| * * * UPDATE AT 2111 ON 10/31/99 BY UNDERWOOD TAKEN BY WEAVER * * *          |
|                                                                              |
| At 1412 CDT on 10/31/99, the PSS was notified that five corroded sprinkler   |
| heads had been discovered on High Pressure Fire Water System 9 in the C-335  |
| building.  There were two adjacent corroded heads discovered in two separate |
| locations and a third individual head at a different location.  The system   |
| was declared inoperable and fire patrols were initiated.  The corroded heads |
| have since been replaced and the system returned to operable status.   The   |
| NRC Resident Inspector was notified of this update.  The NRC Operations      |
| Officer notified R3DO (Jordan) and NMSS EO (Hickey).                         |
|                                                                              |
| * * * UPDATE AT 2121 ON 11/01/99 BY KEVIN BEASLEY TAKEN BY JOLLIFFE * * *    |
|                                                                              |
| At 0930 CST on 11/01/99, the PSS was notified that three corroded sprinkler  |
| heads had been discovered on the High Pressure Fire Water System B-4 in the  |
| C-337 building.  Two of these sprinkler heads are adjacent.  Two adjacent    |
| corroded sprinkler heads were also discovered on the High Pressure Fire      |
| Water System B-5 in the C-337 building.  These systems were declared         |
| inoperable and fire patrols were initiated.  Work has been initiated to      |
| replace the corroded heads.  The NRC Resident Inspector has been notified of |
| this update.  The NRC Operations Officer notified the R3DO Jim Creed.        |
|                                                                              |
| * * * UPDATE AT 2143 ON 11/02/99 BY KEVIN BEASLEY TAKEN BY JOLLIFFE * * *    |
|                                                                              |
| At 1400 CST on 11/02/99, the PSS was notified that numerous corroded         |
| sprinkler heads had been discovered on High Pressure Fire Water Systems C-8  |
| and D-7 in the C-333 building.  These systems had been previously declared   |
| inoperable and fire patrols were being performed at the time of discovery.   |
| Work has been initiated to replace the corroded heads.  The NRC Resident     |
| Inspector has been notified of this update.  The NRC Operations Officer      |
| notified the R3DO Jim Creed.                                                 |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36385       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PALISADES                REGION:  3  |NOTIFICATION DATE: 11/02/1999|
|    UNIT:  [1] [] []                 STATE:  MI |NOTIFICATION TIME: 11:45[EST]|
|   RXTYPE: [1] CE                               |EVENT DATE:        11/02/1999|
+------------------------------------------------+EVENT TIME:        09:00[EST]|
| NRC NOTIFIED BY:  BOB VINCENT                  |LAST UPDATE DATE:  11/02/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JAMES CREED          R3      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - INDICATIONS DISCOVERED ON CONTROL ROD DRIVE SEAL HOUSINGS -                |
|                                                                              |
| At 0900 on 11/02/99, a dye penetrant (PT) examination of the control rod     |
| drive seal housing for control rod #44 revealed a potential crack-like       |
| indication in the Reactor Coolant System pressure boundary.  The PT          |
| examination was performed to investigate a boric acid deposit on the         |
| exterior surface of the housing which was discovered during a previous       |
| visual inspection.  A small indication was also found on the seal housing    |
| for control rod #30.  The plant is in a refueling outage.  An investigation  |
| to characterize the indications and determine their cause and extent is in   |
| progress.  This situation will be resolved prior to plant restart.           |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36386       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FT CALHOUN               REGION:  4  |NOTIFICATION DATE: 11/02/1999|
|    UNIT:  [1] [] []                 STATE:  NE |NOTIFICATION TIME: 17:45[EST]|
|   RXTYPE: [1] CE                               |EVENT DATE:        11/02/1999|
+------------------------------------------------+EVENT TIME:        16:00[CST]|
| NRC NOTIFIED BY:  ERICK MATZKE                 |LAST UPDATE DATE:  11/02/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CLAUDE JOHNSON       R4      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(vi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - STATE NOTIFIED OF AN OIL/GREASE RELEASE IN EXCESS OF THEIR NPDES RELEASE   |
| PERMIT LIMIT -                                                               |
|                                                                              |
| On 10/04/99, a mixture of oil and grease was released from the plant.  The   |
| licensee sent a composite sample of the mixture to an offsite facility for   |
| analysis.  At 1600 CST on 11/02/99, the licensee received the results of the |
| analysis and notified the State of Nebraska that the release (13 mg/l) was   |
| in excess of the station's NPDES release permit limit (10 mg/l).             |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36387       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: GRAND GULF               REGION:  4  |NOTIFICATION DATE: 11/02/1999|
|    UNIT:  [1] [] []                 STATE:  MS |NOTIFICATION TIME: 19:06[EST]|
|   RXTYPE: [1] GE-6                             |EVENT DATE:        11/02/1999|
+------------------------------------------------+EVENT TIME:        16:56[CST]|
| NRC NOTIFIED BY:  ERNEST MATHES                |LAST UPDATE DATE:  11/02/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CLAUDE JOHNSON       R4      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - MSIVs LEAKING ABOVE ACCEPTABLE LEAK RATE DURING AN LLRT -                  |
|                                                                              |
| During a local leak rate test with the plant in a refueling outage, the      |
| licensee discovered excess leakage past the 'A' main steam line inboard and  |
| outboard main steam isolation valves (#B21-F022A and #B21-F028A).  This      |
| condition exceeded the acceptable leak rate.  The licensee is determining    |
| corrective action.                                                           |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36388       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: QUAD CITIES              REGION:  3  |NOTIFICATION DATE: 11/02/1999|
|    UNIT:  [] [2] []                 STATE:  IL |NOTIFICATION TIME: 20:57[EST]|
|   RXTYPE: [1] GE-3,[2] GE-3                    |EVENT DATE:        11/02/1999|
+------------------------------------------------+EVENT TIME:        19:01[CST]|
| NRC NOTIFIED BY:  TOM OSELAND                  |LAST UPDATE DATE:  11/02/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JAMES CREED          R3      |
|10 CFR SECTION:                                 |                             |
|AOUT 50.72(b)(1)(ii)(B)  OUTSIDE DESIGN BASIS   |                             |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION    |                             |
|NLCO                     TECH SPEC LCO A/S      |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - HIGH PRESSURE COOLANT INJECTION (HPCI) SYSTEM INOPERABLE -                 |
|                                                                              |
| During performance of the HPCI Steam Exhaust Vacuum Breaker Line Check       |
| Valves IST Functional Test, one of four check valves failed to meet its      |
| acceptance criteria.  The licensee isolated the check valve, declared the    |
| HPCI System inoperable, and entered a 14 day LCO.  All other Emergency Core  |
| Cooling Systems are operable.                                                |
|                                                                              |
| The licensee plans to notify the NRC Resident Inspector.                     |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36389       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: LASALLE                  REGION:  3  |NOTIFICATION DATE: 11/02/1999|
|    UNIT:  [] [2] []                 STATE:  IL |NOTIFICATION TIME: 21:16[EST]|
|   RXTYPE: [1] GE-5,[2] GE-5                    |EVENT DATE:        11/02/1999|
+------------------------------------------------+EVENT TIME:        19:47[CST]|
| NRC NOTIFIED BY:  LARRY BLUNK                  |LAST UPDATE DATE:  11/02/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JAMES CREED          R3      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(vi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - OFFSITE AGENCIES NOTIFIED OF THE PRESENCE OF OIL LADEN GRAVEL ONSITE -     |
|                                                                              |
| The licensee notified the Illinois Emergency Management Agency and the       |
| National Response Center of the presence of oil in the pea gravel around the |
| oil filling station underground storage tanks.  The oil was present in a two |
| inch layer of gravel at the top of the water table approximately five feet   |
| below ground level.  The filling station consists of a 10,000 gallon diesel  |
| fuel tank, a 10,000 gallon gasoline tank, and a 1,000 gallon waste oil tank. |
| No fire, explosion, or vapor hazards have been identified.  The tanks will   |
| continue to be excavated for State Fire Marshall inspection on 11/04/99.     |
| The oil laden pea gravel will be removed and disposed of properly.           |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+


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