Event Notification Report for September 16, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           09/15/1999 - 09/16/1999

                              ** EVENT NUMBERS **

36149  36156  36163  36164  36165  36166  36167  36168  36169  36170  36171  

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36149       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: NORTH ANNA               REGION:  2  |NOTIFICATION DATE: 09/12/1999|
|    UNIT:  [1] [2] []                STATE:  VA |NOTIFICATION TIME: 09:30[EDT]|
|   RXTYPE: [1] W-3-LP,[2] W-3-LP                |EVENT DATE:        09/12/1999|
+------------------------------------------------+EVENT TIME:        09:04[EDT]|
| NRC NOTIFIED BY:  VICKY HARTE                  |LAST UPDATE DATE:  09/15/1999|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |ROBERT HAAG          R2      |
|10 CFR SECTION:                                 |                             |
|AENS 50.72(b)(1)(v)      ENS INOPERABLE         |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       60       Power Operation  |60       Power Operation  |
|2     N          N       0        Hot Standby      |0        Hot Standby      |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| LOST SAFETY PARAMETER DISPLAY SYSTEM AND THE TECHNICAL SUPPORT CENTER        |
| COMPUTER                                                                     |
|                                                                              |
| Power was lost  to the Safety Parameter Display System (SPDS) and the        |
| Technical Support Center (TSC) computer system at 0904 EDT on 9/12/99.  The  |
| bus supplying power to the battery charger for the SPDS and TSC computer was |
| lost when the supply breaker opened on a ground detection, on the            |
| underground cable supply.  The normal alternate power supply to the battery  |
| charger was previously lost, some time ago, due to another ground on its     |
| underground cable supply.  The licensee made the decision to preserve the    |
| battery and deenergized the battery bus.  Also, with the TSC computer system |
| out-of-service, the control room will serve as the alternate TSC facility.   |
|                                                                              |
| This event is a major loss of emergency  assessment capability and is        |
| reportable.  Troubleshooting and repairs to the electrical distribution      |
| system are in progress.  Also, the licensee is investigating an alternate    |
| methods to power the battery charger.                                        |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
|                                                                              |
|                                                                              |
| ***Update on 09/15/99 at 1255ET by Kemp taken by MacKinnon***                |
|                                                                              |
| Power was restored to the TSC and the SPDS was restored to service at 1132ET |
| today (09/15/99).  R2DO (Chris Christensen) notified.                        |
|                                                                              |
| The NRC Resident Inspector will be informed by the licensee of this update.  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36156       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SAINT LUCIE              REGION:  2  |NOTIFICATION DATE: 09/13/1999|
|    UNIT:  [1] [2] []                STATE:  FL |NOTIFICATION TIME: 17:30[EDT]|
|   RXTYPE: [1] CE,[2] CE                        |EVENT DATE:        09/13/1999|
+------------------------------------------------+EVENT TIME:        17:13[EDT]|
| NRC NOTIFIED BY:  STEVE MERRILL                |LAST UPDATE DATE:  09/15/1999|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          UNU                   |ROBERT HAAG          R2      |
|10 CFR SECTION:                                 |JOSEPH GIITTER       IRO     |
|AAEC 50.72 (a) (1) (I)   EMERGENCY DECLARED     |DAN SULLIVAN         FEMA    |
|                                                |FRANK CONGEL         IRO     |
|                                                |ELINOR ADENSAM       NRR     |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Hot Shutdown     |0        Hot Shutdown     |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNUSUAL EVENT DECLARED DUE TO ENTERING EAL 5B ITEM 1 (CONFIRMED HURRICANE    |
| WARNING IN EFFECT)                                                           |
|                                                                              |
| The licensee entered an Unusual Event per Emergency Action Level 5B item 1.  |
| All emergency diesel generators are fully operable and the electrical grid   |
| is stable.  All emergency core cooling systems are fully operable. The state |
| was notified of the Unusual Event classification.  Local counties will be    |
| notified of the Unusual Event classification by the state of Florida.        |
|                                                                              |
| The NRC Resident Inspector will be notified of this event by the licensee.   |
|                                                                              |
| * * * UPDATE 0930 9/14/1999 BY STRANSKY * * *                                |
|                                                                              |
| The NRC entered the Monitoring Phase of Normal Mode at 0930 on 9/14/1999 in  |
| preparation of potential landfall by Hurricane Floyd.                        |
|                                                                              |
| * * * COMMISSIONER'S ASSISTANTS BRIEF, 1000 EDT ON 9/14/99 * * *             |
|                                                                              |
| Luis Reyes the R2RA conducted the brief, IRO (Frank Congel), NRR (Tad        |
| Marsh), NMSS (Josie Piccone), PA (William Beecher), SP (Fred Combs), R2 IRC  |
| (Pierce Skinner), CA (Betsy Keeling), EDO Staff (Leonard Wert), IP (Karen    |
| Henderson), SECY (Andrew Bates), Chairman Dicus Off (Thomas Hiltz), Comm.    |
| McGaffigan Off (James Beall), Comm. Diaz Off (Anthony Hsia), Comm.           |
| Merrifield Off (Lynne Stauss)                                                |
|                                                                              |
| *** COMMISSIONER'S ASSISTANCE BRIEF, 2000 EDT ON 9/14/99 ***                 |
|                                                                              |
| Luis Reyes the R2RA conducted the brief, EDO (Jim Dyer), IRO ( Joe Giitter), |
| NRR EO (Bill Beckner), NMSS (Josie Piccone), CA (Betsy Keeling), Chairman    |
| Dicus Off (Tom Hiltz), Comm McGaffigan (James Beall),  Comm Merrifield       |
| (Lynne Stauss & John Thoma), NRC R2 (Bruce Mallett & Anne Boland) .          |
|                                                                              |
| * * * UPDATE AT 0059 EDT ON 9/15/99 BY JACK BREEN TO FANGIE JONES * * *      |
|                                                                              |
| Unusual Event was terminated at 0040 EDT when the hurricane warning was      |
| lifted by the National Hurricane Center.  The licensee notified the NRC      |
| Resident Inspector and intends notifying the state and surrounding counties  |
| of exiting the Unusual Event.  R2DO (Chris Christensen), NRR EO (William     |
| Beckner), and FEMA (Wayne Storer) notified.                                  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36163       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BRUNSWICK                REGION:  2  |NOTIFICATION DATE: 09/14/1999|
|    UNIT:  [1] [2] []                STATE:  NC |NOTIFICATION TIME: 23:30[EDT]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        09/14/1999|
+------------------------------------------------+EVENT TIME:        23:10[EDT]|
| NRC NOTIFIED BY:  THOMAS WOODALL               |LAST UPDATE DATE:  09/16/1999|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          UNU                   |CHRIS CHRISTENSEN    R2      |
|10 CFR SECTION:                                 |WILLIAM BECKNER      NRR     |
|AAEC 50.72 (a) (1) (I)   EMERGENCY DECLARED     |FRANK CONGEL         IRO     |
|                                                |WAYNE STORER         FEMA    |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNUSUAL EVENT DECLARED DUE TO ENTERING EAL 2.1 SECTION 14.1.2 (NATURAL EVENT |
| - HURRICANE WARNING).                                                        |
|                                                                              |
| The licensee entered an Unusual Event per Emergency Action Level 2.1 Section |
| 14.1.2.  All emergency diesel generators and their emergency core cooling    |
| systems are fully operable. The electrical grid is stable. The licensee said |
| that they would have to enter Abnormal Operating Procedure 13 two hours      |
| before wind speed increased to 75 mph.  The licensee projects that they have |
| 27 hours until hurricane force winds reach their site.                       |
| The licensee has notified the state of North Carolina and surrounding        |
| counties of entering an unusual event classification.                        |
|                                                                              |
| The NRC Resident Inspector will be informed of this event by the licensee.   |
|                                                                              |
| * * * UPDATE 0845EDT ON 9/15/99 FROM DON DEWEY TO S. SANDIN * * *            |
|                                                                              |
| The licensee decided at 0830EDT to reduce power on both units to 40% by      |
| 1000EDT and hold.  A decision as to whether a shutdown should continue will  |
| be made at that time.  Unit 1 and 2 are currently at 76% and 82% power,      |
| respectively.  The licensee will inform the NRC Resident Inspector.          |
| Notified R2 IRC(Skinner).                                                    |
|                                                                              |
|                                                                              |
| ***UPDATE AT 1248ET ON 09/15/99 BY DON DEWEY TAKEN BY MACKINNON***           |
|                                                                              |
| Brunswick Unit 2 was manually scrammed from 31% reactor power at 1118 hours. |
| All systems operated as expected.                                            |
|                                                                              |
| Brunswick Unit 1 was manually scrammed from 35% reactor power at 1206 hours. |
| All systems operated as expected.                                            |
|                                                                              |
| All Emergency Core Cooling Systems and the Emergency Diesel Generators are   |
| fully operable if needed. The offsite electrical grid at this time is        |
| stable.  On site wind speed is 32 mph.                                       |
|                                                                              |
| R2DO (Chris Christensen &  Pierce Skinner), NRR (Bill Beckner & Bob Dennig)  |
| and IRO (Joe Giitter)  notified.                                             |
|                                                                              |
| The NRC Resident Inspector was notified of this event update by the          |
| licensee.                                                                    |
|                                                                              |
| ***UPDATE AT 2016ET ON 09/15/99 BY ROBBINS TAKEN BY MACKINNON***             |
|                                                                              |
| Brunswick Unit 2 entered a cold shutdown condition at 1935 hours and         |
| Brunswick Unit 2 entered a cold shutdown condition at 1955 hours.  Onsite    |
| wind speed is 34 mph.  R2DO (Chris Christensen) & NRC Region 2 IRC (Anne     |
| Boland) notified.                                                            |
|                                                                              |
| The NRC Resident Inspector was notified of this update by the licensee.      |
|                                                                              |
| * * * UPDATE 0510EDT ON 9/16/99 VIA FAX TO S. SANDIN * * *                   |
|                                                                              |
| Message #6  was received via fax:                                            |
|                                                                              |
| "32 of the 35 Emergency Warning Sirens are now indicating an inoperable      |
| status due to a loss of power.  Some siding panels from the turbine building |
| have been lost.  The turbine building radiological conditions are monitored. |
| Both Units are in cold shutdown." [see event #36169]  Meteorological         |
| conditions as of 0458EDT were wind direction from 240-280 degrees, speed     |
| 75-95 mph, stability class D with rain.  Notified R2 IRC(Reyes).             |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36164       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BRUNSWICK                REGION:  2  |NOTIFICATION DATE: 09/15/1999|
|    UNIT:  [1] [2] []                STATE:  NC |NOTIFICATION TIME: 11:31[EDT]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        09/15/1999|
+------------------------------------------------+EVENT TIME:        09:35[EDT]|
| NRC NOTIFIED BY:  DAVID JENKINS                |LAST UPDATE DATE:  09/15/1999|
|  HQ OPS OFFICER:  WILLIAM POERTNER             +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHRIS CHRISTENSEN    R2      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(vi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       60       Power Operation  |60       Power Operation  |
|2     N          Y       60       Power Operation  |60       Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION DUE TO OPENING STORM DRAIN BYPASS VALVES                |
|                                                                              |
| On September 15, 1999, at 0935 EDT, the bypass valves from the site's storm  |
| drain basin directly to the circulating water discharge canal were opened to |
| prevent site flooding (which could cause significant damage to plant         |
| equipment and/or possibly endanger personnel safety) due to the impending    |
| arrival of hurricane Floyd.  Past experience has shown that the installed    |
| pump capacity will not keep up with the rain expected during a hurricane.    |
| The valves were opened prior to hurricane force winds reaching the site to   |
| avoid exposing personnel to the hurricane.   Opening these valves is a       |
| reportable event (to the state of North Carolina) in accordance with the     |
| site National Pollutant Discharge Elimination System permit.                 |
|                                                                              |
| The NRC resident has been notified.                                          |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Hospital                                         |Event Number:   36165       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  WILLIAM BEAUMONT HOSPITAL            |NOTIFICATION DATE: 09/15/1999|
|LICENSEE:  WILLIAM BEAUMONT HOSPITAL            |NOTIFICATION TIME: 14:59[EDT]|
|    CITY:  ROYAL OAK                REGION:  3  |EVENT DATE:        09/15/1999|
|  COUNTY:                            STATE:  MI |EVENT TIME:        11:00[EDT]|
|LICENSE#:  21-01333-01           AGREEMENT:  N  |LAST UPDATE DATE:  09/15/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |GARY SHEAR           R3      |
|                                                |JOSIE PICCONE        NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  CHERYL SCHULTZ               |                             |
|  HQ OPS OFFICER:  JOHN MacKINNON               |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|LADM 35.33(a)            MED MISADMINISTRATION  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| PATIENT RECEIVED A PLACEBO INSTEAD OF 20 GRAY OF P-32.                       |
|                                                                              |
| A patient signed a consent form to participate in a coronary brachytherapy   |
| trial to evaluate the Guidant Coronary Afterloader.  The patient was         |
| randomized to receive 20 Gray to the proximal left anterior descending       |
| coronary artery with P-32, but the Radiation Oncology physicist programmed   |
| the afterloader to use the placebo source wire instead.  Therefore, the      |
| patient did not receive the prescribed dose of 20 Gray.  The root cause for  |
| the error was that the Radiation Oncologist did not adequately confirm the   |
| written directive prior to treatment.  There was no documentation on the     |
| randomization order to guide the physicist in selecting the proper           |
| treatment, so he relied on his memory, which failed.                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36166       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: INDIAN POINT             REGION:  1  |NOTIFICATION DATE: 09/15/1999|
|    UNIT:  [2] [] []                 STATE:  NY |NOTIFICATION TIME: 16:06[EDT]|
|   RXTYPE: [2] W-4-LP,[3] W-4-LP                |EVENT DATE:        09/15/1999|
+------------------------------------------------+EVENT TIME:        15:36[EDT]|
| NRC NOTIFIED BY:  PHIL SANTINI                 |LAST UPDATE DATE:  09/15/1999|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |NIEL DELLA GRECA     R1      |
|10 CFR SECTION:                                 |                             |
|AEXT 50.72(b)(1)(iii)    EXTERNAL THREAT        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|2     N          N       0        Hot Shutdown     |0        Hot Shutdown     |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| HURRICANE WINDS PREDICTED TO COME WITHIN 500 NM OF SITE                      |
|                                                                              |
| At 1536, the licensee was notified that the National Weather Service had     |
| issued hurricane warnings for North Carolina and Virginia, with hurricane    |
| force winds extending 140 miles outward from the center of Hurricane Floyd.  |
| The licensee considers that the arrival of hurricane force winds within 500  |
| nautical miles (NM) of Indian Point, concurrent with hurricane warnings is   |
| imminent. This notification is being made in accordance with Technical       |
| Specification 3.14.a and Abnormal Operating Instruction 28.07. The NRC       |
| resident inspector will be informed of this notification by the licensee.    |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36167       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SURRY                    REGION:  2  |NOTIFICATION DATE: 09/15/1999|
|    UNIT:  [1] [2] []                STATE:  VA |NOTIFICATION TIME: 22:17[EDT]|
|   RXTYPE: [1] W-3-LP,[2] W-3-LP                |EVENT DATE:        09/15/1999|
+------------------------------------------------+EVENT TIME:        22:00[EDT]|
| NRC NOTIFIED BY:  DON KARNS                    |LAST UPDATE DATE:  09/16/1999|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          UNU                   |CHRIS CHRISTENSEN    R2      |
|10 CFR SECTION:                                 |ANN BOLAND           R2      |
|AAEC 50.72 (a) (1) (I)   EMERGENCY DECLARED     |WILLIAM BECKNER      NRR     |
|                                                |FRANK CONGEL         IRO     |
|                                                |BELCHER              FEMA    |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |83       Power Operation  |
|2     N          Y       100      Power Operation  |47       Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNUSUAL EVENT DECLARED DUE TO APPROACHING HURRICANE                          |
|                                                                              |
| An Unusual Event was declared at 2200 EDT due to the expected onset of       |
| hurricane force winds within the following 12 hours. The licensee currently  |
| expects that hurricane force winds will occur onsite at 1000 EDT. Both units |
| are currently being shut down in anticipation of the hurricane arrival.      |
| Shutdown of Unit 2 commenced at 1906 EDT, and Unit 1 began shutting down at  |
| 2040 EDT. The NRC resident inspector has been informed of this               |
| notification.                                                                |
|                                                                              |
| * * * UPDATE 0210EDT ON 9/16/99 FROM DALE JONES TO S. SANDIN * * *           |
|                                                                              |
| The licensee is holding power at 46% on Unit 1 and 35% on Unit 2 pending an  |
| assessment of the path of Hurricane Floyd.  Current projections for maximum  |
| sustained wind on site indicate less than 60 mph due to the more easterly    |
| course change.  Notified R2DO(Christensen) and R2(Boland).                   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36168       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BROWNS FERRY             REGION:  2  |NOTIFICATION DATE: 09/15/1999|
|    UNIT:  [] [2] []                 STATE:  AL |NOTIFICATION TIME: 22:55[EDT]|
|   RXTYPE: [1] GE-4,[2] GE-4,[3] GE-4           |EVENT DATE:        09/15/1999|
+------------------------------------------------+EVENT TIME:        18:25[CDT]|
| NRC NOTIFIED BY:  JOSEPH BENNETT               |LAST UPDATE DATE:  09/15/1999|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHRIS CHRISTENSEN    R2      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(vi)     OFFSITE NOTIFICATION   |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     M/R        Y       52       Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| REACTOR MANUALLY SCRAMMED FROM 52% REACTOR POWER DUE TO AN UNCONTROLLABLE    |
| LOSS OF ELECTROHYDRAULIC CONTROL (EHC) FLUID.                                |
|                                                                              |
|                                                                              |
| At approximately 1750 on 09/15/99, failure of an EHC system pressure sensing |
| line resulted in an uncontrollable loss of EHC fluid.  Attempts to maintain  |
| EHC reservoir level failed, and a 1825 hours, the reactor was manually       |
| scrammed from 52% reactor power in preparation for removing the EHC system   |
| from service.  Reactor power was initially at 100% and it was reduced to 52% |
| before the reactor was manually scrammed.  The scram resulted in a low       |
| reactor vessel water level, causing an automatic isolation of Primary        |
| Containment Isolation System (PCIS) groups 2 (Drywell isolations), 3         |
| (Reactor Water Cleanup trip/isolation), &8 (transversing incore probe system |
| isolation).  EOI-1  was entered due to low reactor vessel water level        |
| {decreased to negative 28.5", Top of Active Fuel (TAF) is negative 162"} and |
| to control reactor pressure with the loss of the EHC system.  No Main Steam  |
| Safety Relief Valves (MSRVs) were actuated during this event.  All control   |
| rods fully inserted into the core.                                           |
|                                                                              |
| The licensee started that restart is projected for 1600 hours on 09/16/99.   |
|                                                                              |
|                                                                              |
| NRC Region 2 Section Chief (Paul Fredrickson) was notified of this event by  |
| the licensee.                                                                |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36169       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BRUNSWICK                REGION:  2  |NOTIFICATION DATE: 09/16/1999|
|    UNIT:  [1] [2] []                STATE:  NC |NOTIFICATION TIME: 01:21[EDT]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        09/16/1999|
+------------------------------------------------+EVENT TIME:        00:50[EDT]|
| NRC NOTIFIED BY:  DAVE JESTER                  |LAST UPDATE DATE:  09/16/1999|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHRIS CHRISTENSEN    R2      |
|10 CFR SECTION:                                 |ANNE BOLAND          R2      |
|AARC 50.72(b)(1)(v)      OTHER ASMT/COMM INOP   |                             |
|APRE 50.72(b)(2)(vi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|2     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| PARTIAL LOSS OF EMERGENCY SIREN CAPABILITY DURING HURRICANE FLOYD            |
|                                                                              |
| "[Operations was] informed by Brunswick Plant Emergency Preparedness         |
| personnel that 13 emergency warning offsite sirens have failed as a result   |
| of Hurricane Floyd.                                                          |
|                                                                              |
| "[The initial safety significance evaluation characterized the significance  |
| of the loss of the sirens as] minimal.   Backup alert measures are in place. |
| Local agencies have been notified.                                           |
|                                                                              |
| "[Corrective action(s) include a] complete investigation into the cause of   |
| the failure and complete required repairs."                                  |
|                                                                              |
| The thirteen [13] sirens are located primarily on the beach and on Bald Head |
| Island and Boiling Spring Lake  in Brunswick county.  There are an           |
| additional seventeen [17] operable sirens currently available in Brunswick   |
| county and five [5] more in New Hanover county.  The loss of the 13 sirens   |
| was related to loss of power as detected by an external operability check    |
| performed by a computer.  The licensee will not initiate repairs until the   |
| storm passes.                                                                |
|                                                                              |
| The licensee informed state/local agencies and the NRC Resident Inspector.   |
|                                                                              |
| * * * UPDATE 0510EDT ON 9/16/99 VIA FAX TO S. SANDIN * * *                   |
|                                                                              |
| Thirty-two [32] of the thirty-five [35] sirens are out-of-service.  See      |
| event #36163 for additional information.  Notified R2 IRC (Reyes).           |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36170       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: HARRIS                   REGION:  2  |NOTIFICATION DATE: 09/16/1999|
|    UNIT:  [1] [] []                 STATE:  NC |NOTIFICATION TIME: 02:32[EDT]|
|   RXTYPE: [1] W-3-LP                           |EVENT DATE:        09/16/1999|
+------------------------------------------------+EVENT TIME:        01:55[EDT]|
| NRC NOTIFIED BY:  KEVIN ABELL                  |LAST UPDATE DATE:  09/16/1999|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHRIS CHRISTENSEN    R2      |
|10 CFR SECTION:                                 |ANNE BOLAND          R2      |
|AARC 50.72(b)(1)(v)      OTHER ASMT/COMM INOP   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| PARTIAL LOSS OF EMERGENCY SIREN CAPABILITY DURING HURRICANE FLOYD            |
|                                                                              |
| "The Plant was operating at 100% power when 22 Warning Sirens became         |
| inoperable due to loss of power. The counties of Chatham, Harnett, and Wake  |
| are each affected. Wind speeds in these areas are higher than normal due to  |
| the effects of hurricane Floyd. One additional Warning Siren in Wake County  |
| was previously inoperable due to failing its periodic test. Repairs will be  |
| made when wind speed subsides."                                              |
|                                                                              |
| Harris has a total of 81 sirens of which 22 represents slightly greater than |
| 25%.  Residents living within 5 miles of the site have tone alert radios as  |
| a backup.  The licensee informed the NRC resident inspector and will inform  |
| state/local agencies.                                                        |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36171       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: LIMERICK                 REGION:  1  |NOTIFICATION DATE: 09/16/1999|
|    UNIT:  [] [2] []                 STATE:  PA |NOTIFICATION TIME: 04:30[EDT]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        09/16/1999|
+------------------------------------------------+EVENT TIME:        01:15[EDT]|
| NRC NOTIFIED BY:  DOUG AMTSFIELD               |LAST UPDATE DATE:  09/16/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |NIEL DELLA GRECA     R1      |
|10 CFR SECTION:                                 |                             |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - Secondary containment integrity lost due to a hatch cover being removed    |
| during maintenance activities -                                              |
|                                                                              |
| At 0115 on 09/16/99. Limerick Generating Station Unit 2 experienced a loss   |
| of secondary containment integrity.  At the time of the event. the Standby   |
| Gas Treatment (SBGT) System was in service.  The Reactor Enclosure HVAC      |
| System was not in service due to maintenance activities. The SBGT System was |
| unable to maintain reactor enclosure pressure greater than 0.25 inches of    |
| vacuum water gauge per Technical Specifications due to a hatch cover being   |
| removed for maintenance inspection activities.  This event could have        |
| prevented the fulfillment of the safety function of structures or systems    |
| that are needed to control the release of radioactive materials or mitigate  |
| the consequences of an accident.  The hatch cover was reinstalled properly   |
| by 0126 and the SBGT System was able to draw a vacuum on the reactor         |
| enclosure area greater than 0.25 inches of vacuum water gauge.               |
|                                                                              |
| The licensee informed the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+


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