Event Notification Report for August 25, 1999
U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
08/24/1999 - 08/25/1999
** EVENT NUMBERS **
36059 36060 36061 36062 36063 36064 36065 36066 36067 36068
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 36059 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 08/23/1999|
| UNIT: [1] [] [] STATE: FL |NOTIFICATION TIME: 14:25[EDT]|
| RXTYPE: [1] CE,[2] CE |EVENT DATE: 08/23/1999|
+------------------------------------------------+EVENT TIME: 12:36[EDT]|
| NRC NOTIFIED BY: JIM HURCHALLA |LAST UPDATE DATE: 08/24/1999|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |KENNETH BARR R2 |
|10 CFR SECTION: | |
|ARPS 50.72(b)(2)(ii) RPS ACTUATION | |
|AESF 50.72(b)(2)(ii) ESF ACTUATION | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 M/R Y 100 Power Operation |0 Hot Standby |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| MANUAL REACTOR TRIP DUE TO LOSS OF MAIN CONDENSER VACUUM |
| |
| The reactor was manually tripped (all rods inserted) due to low main |
| condenser vacuum at 1236 EDT. The cause of the low vacuum is under |
| investigation and is unknown at this time. When the trip occurred the 'A' |
| side non-essential 6.9 kV bus failed to transfer from the auxiliary (plant) |
| power to startup (offsite) source resulting in the loss of two of four |
| reactor coolant pumps. The cause of the failure to transfer is also unknown |
| and under investigation. |
| |
| The plant is stable in hot standby with forced circulation via the remaining |
| two reactor coolant pumps. Feedwater is via the main feedwater system and |
| steaming is via the steam bypass system. |
| |
| The licensee notified the NRC Resident Inspector. |
| |
| |
| *** UPDATE ON 8/24/99 @ 0915 BY HALL TO GOULD *** |
| |
| THIS UPDATE IS TO INCLUDE THE ACTUATION OF THE AFAS-2 (AUX FEEDWATER |
| ACTUATION SYSTEM) FOR 4 MINS TO THE #2 STEAM GENERATOR. THIS RESPONSE IS |
| EXPECTED AND NORMAL. |
| |
| THE RESIDENT INSPECTOR WAS NOTIFIED. |
| |
| THE REG 2 RDO(BARR) WAS NOTIFIED. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 36060 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 08/24/1999|
| UNIT: [1] [2] [3] STATE: CT |NOTIFICATION TIME: 06:52[EDT]|
| RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 08/24/1999|
+------------------------------------------------+EVENT TIME: 06:30[EDT]|
| NRC NOTIFIED BY: ACKERMAN |LAST UPDATE DATE: 08/24/1999|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |KATHLEEN MODES R1 |
|10 CFR SECTION: | |
|APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N N 0 Refueling |0 Refueling |
|2 N Y 100 Power Operation |100 Power Operation |
|3 N Y 100 Power Operation |100 Power Operation |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| OFF SITE NOTIFICATION DUE TO FIRE OUTSIDE OF THE PROTECTED AREA. |
| |
| A FIRE WAS REPORTED AT THE COMPRESSOR OIL SEPARATOR IN THE SWITCHYARD |
| OUTSIDE THE PROTECTED AREA. THE FIRE WAS EXTINGUISHED WITHIN 10 MINS WITH |
| ASSISTANCE FROM OFF SITE FIRE DEPARTMENT. THE FIRE CONSISTED MOSTLY OF |
| SMOKE AND SOME FLAMES, BUT THERE WAS NO APPARENT DAMAGE TO THE COMPRESSOR OR |
| SWITCHYARD. THE STATE DEPARTMENT OF ENVIRONMENTAL PROTECTION AND THE COUNTY |
| WERE NOTIFIED. |
| |
| THE RESIDENT INSPECTOR WILL BE NOTIFIED. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 36061 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 08/24/1999|
| UNIT: [1] [2] [] STATE: PA |NOTIFICATION TIME: 09:15[EDT]|
| RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 08/24/1999|
+------------------------------------------------+EVENT TIME: 08:45[EDT]|
| NRC NOTIFIED BY: GRANT FERNSLER |LAST UPDATE DATE: 08/24/1999|
| HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |KATHLEEN MODES R1 |
|10 CFR SECTION: | |
|AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N Y 100 Power Operation |100 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| UNAVAILABILITY OF NOTIFICATION SYSTEMS FOR PAGER ACTIVATION |
| |
| On 8/24/99 the station was conducting an Emergency Plan Drill. During the |
| activities one of the participants learned that the telenotification system |
| (including its backup) which is used to page individuals in the event of an |
| actual emergency had failed. In accordance with 10CFR50.72(b)(1)(v) this |
| constitutes a Loss of Emergency Response Capability . |
| |
| The telenotification system is now operable. The licensee determined that a |
| power source was disconnected. |
| |
| The NRC resident inspector has been notified. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|General Information or Other |Event Number: 36062 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG: T.A. HOUSTON & ASSOCIATES |NOTIFICATION DATE: 08/24/1999|
|LICENSEE: T.A. HOUSTON & ASSOCIATES |NOTIFICATION TIME: 11:49[EDT]|
| CITY: CULPEPER REGION: 2 |EVENT DATE: 08/06/1999|
| COUNTY: STATE: VA |EVENT TIME: 16:00[EDT]|
|LICENSE#: 45-025073-01 AGREEMENT: N |LAST UPDATE DATE: 08/24/1999|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |SCOTT SPARKS R2 |
| |JOHN HICKEY NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: T.A. HOUSTON | |
| HQ OPS OFFICER: CHAUNCEY GOULD | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|NINF INFORMATION ONLY | |
|BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| TROXLER MOISTURE DENSITY GAUGE LOST DURING SHIPMENT |
| |
| A TROXLER MOISTURE DENSITY GAUGE MODEL 3411B SERIAL #15637 CONTAINING 8 |
| MILLICURIES OF CESIUM-137 AND 40 MILLICURIES OF AMERICIUM WHICH WAS SHIPPED |
| FROM T.A. HOUSTON & ASSOCIATES IN CULPEPER VA TO THE TROXLER COMPANY IN |
| RESEARCH TRIANGLE PARK, NC ON 8/6/99 HAS NOT REACHED ITS DESTINATION AS OF |
| 8/13/99. FEDERAL EXPRESS, THE CARRIER, AND TROXLER BOTH HAVE BEEN |
| CONTACTED. THE TRACKING NUMBER IS 813439593699. THE GAUGE WAS BEING |
| SHIPPED TO TROXLER FOR CALIBRATION AND ROUTINE MAINTENANCE. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 36063 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: HADDAM NECK REGION: 1 |NOTIFICATION DATE: 08/24/1999|
| UNIT: [1] [] [] STATE: CT |NOTIFICATION TIME: 12:18[EDT]|
| RXTYPE: [1] W-4-LP |EVENT DATE: 08/24/1999|
+------------------------------------------------+EVENT TIME: 11:10[EDT]|
| NRC NOTIFIED BY: BRIAN CAMPBELL |LAST UPDATE DATE: 08/24/1999|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |KATHLEEN MODES R1 |
|10 CFR SECTION: | |
|HFIT 26.73 FITNESS FOR DUTY | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N N 0 Decommissioned |0 Decommissioned |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| FITNESS FOR DUTY REPORT |
| |
| A contractor was determined to be under the influence of alcohol and it was |
| confirmed by positive test results. The contractor's access authorization |
| to the plant has been terminated. Refer to the HOO log for additional |
| details. |
| |
| The licensee informed the NRC Resident Inspector and the Department of |
| Environmental Protection for Connecticut . |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Fuel Cycle Facility |Event Number: 36064 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 08/24/1999|
| RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 12:54[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 08/23/1999|
| 6903 ROCKLEDGE DRIVE |EVENT TIME: 17:18[EDT]|
| BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 08/24/1999|
| CITY: PIKETON REGION: 3 +-----------------------------+
| COUNTY: PIKE STATE: OH |PERSON ORGANIZATION |
|LICENSE#: GDP-2 AGREEMENT: N |MELVYN LEACH R3 |
| DOCKET: 0707002 |JOHN HICKEY NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: RON CRABTREE | |
| HQ OPS OFFICER: FANGIE JONES | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| CRITICALITY ACCIDENT ALARM SYSTEM SLAVE UNITS MAY NOT MEET REQUIRED |
| STANDARD |
| |
| "At 1718 HOURS ON 8/23/99 THE PLANT SHIFT SUPERINTENDENT WAS NOTIFIED THAT |
| THE CRITICALITY ACCIDENT ALARM SYSTEM (CAAS) SLAVE UNITS MAY NOT MEET ANSI |
| 8.3, SECTION 5.5 STANDARD. ANSI 8.3 IDENTIFIES THAT THE CAAS SYSTEM SHALL |
| AUTOMATICALLY INITIATE AN EVACUATION ALARM SIGNAL WITHIN ONE HALF SECOND OF |
| THE ALARM SETPOINT BEING EXCEEDED. ENGINEERING COULD NOT PROVIDE ASSURANCE |
| THAT THE CAAS SLAVE UNITS WOULD MEET THIS REQUIREMENT. FACILITIES WITH CAAS |
| CLUSTERS (DETECTORS) AND THEIR EVACUATION HORNS ARE COMPLIANT WITH ANSI 8.3. |
| SECTION 55 REQUIREMENT. |
| |
| "THE SAFETY SIGNIFICANCE IS MINIMAL SINCE THE SLAVES WILL STILL PROVIDE |
| ALARM INDICATION |
| BEFORE SIMILAR INDICATIONS WOULD BE PROVIDED UNDER THE TSR LCO ACTIONS |
| IMPLEMENTED." |
| |
| FOR INFORMATION: THE ALARMS DISCUSSED HERE ARE REMOTE ALARMS IN AREAS |
| WITHIN SO MANY FEET OF THE AREA OF CONCERN, BUT OUTSIDE THE BUILDING OR |
| ROOM. |
| |
| PLANT PERSONNEL HAVE INFORMED THE NRC RESIDENT INSPECTOR AND THE ONSITE DOE |
| REPRESENTATIVE. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 36065 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DIABLO CANYON REGION: 4 |NOTIFICATION DATE: 08/24/1999|
| UNIT: [1] [2] [] STATE: CA |NOTIFICATION TIME: 15:28[EDT]|
| RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 08/24/1999|
+------------------------------------------------+EVENT TIME: 10:32[PDT]|
| NRC NOTIFIED BY: JOHN RAAB |LAST UPDATE DATE: 08/24/1999|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |PHIL HARRELL R4 |
|10 CFR SECTION: | |
|APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N Y 100 Power Operation |100 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION OF THE CAPTURE AND SUBSEQUENT RELEASE OF A GREEN SEA |
| TURTLE |
| |
| The licensee notified the National Marine Fisheries Service of the capture |
| and subsequent planned release of a green sea turtle, which is protected |
| under the Endangered Species Act. |
| |
| The licensee plans to notify the NRC Resident Inspector. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 36066 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 08/24/1999|
| UNIT: [] [2] [] STATE: TX |NOTIFICATION TIME: 17:53[EDT]|
| RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 08/24/1999|
+------------------------------------------------+EVENT TIME: 14:38[CDT]|
| NRC NOTIFIED BY: WILLIAM VALAGURA |LAST UPDATE DATE: 08/24/1999|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: |PHIL HARRELL R4 |
|10 CFR SECTION: | |
|AESF 50.72(b)(2)(ii) ESF ACTUATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
| | |
|2 N Y 100 Power Operation |100 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| ENGINEERED SAFETY FEATURES ACTUATION DUE TO AN ELECTRICAL FAULT |
| |
| "At 1438 Hrs, August 24, 1999, the Unit 2 Standby Transformer locked out due |
| to an electrical fault on one of the lighting arrestors installed on the |
| transformer. Due to the loss of power to the Unit 2 Standby Transformer, the |
| Train C Standby Diesel Generator started and loaded all Mode II (LOOP) |
| Engineered Safety Features equipment as required. The Train 'B' Standby |
| Diesel Generator was in service for monthly surveillance testing at the time |
| of the event, so the Train 'B' Engineered Safety Features equipment never |
| lost power. |
| |
| "The electrical voltage perturbation also resulted in a Reactor Coolant |
| System letdown isolation. Letdown has subsequently been returned to service |
| for Reactor Coolant System inventory control. Also, two radiation monitors |
| used to monitor plant radiological effluents were affected by the voltage |
| perturbation. The Condenser Air Removal System Radiation Monitor RT-8027 |
| momentarily lost communications with the Radiation Monitoring System |
| Computer. The condition has cleared and the monitor has been returned to |
| service. The Unit Vent Radiation Monitor RT-8010A lost communication with |
| the Radiation Monitoring System Computer during the perturbation as well. |
| This monitor remains out of service (the Wide Range Unit Vent Accident |
| Radiation Monitor RT-8010B remained in service through out the event). |
| |
| "Unit 2 is currently stable at 100% power. Preparations are being made to |
| reenergize the deenergized Unit 2 Standby Buses from the Unit 1 Standby |
| Transformer. |
| |
| "In addition to the start of the Train 'C' Standby Diesel Generator, the |
| Train 'C' Centrifugal Charging Pump and the Train 'C' Auxiliary Feedwater |
| Pump also started as required. The automatic actuation of these Engineered |
| Safety Features components is reportable per 10 CFR 50.72(b)(2))." |
| |
| The licensee notified the NRC Resident Inspector. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Other Nuclear Material |Event Number: 36067 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG: EASTERN ISOTOPES |NOTIFICATION DATE: 08/24/1999|
|LICENSEE: EASTERN ISOTOPES |NOTIFICATION TIME: 19:08[EDT]|
| CITY: STERLING REGION: 2 |EVENT DATE: 08/24/1999|
| COUNTY: STATE: VA |EVENT TIME: 09:00[EDT]|
|LICENSE#: 45-25221-01 AGREEMENT: N |LAST UPDATE DATE: 08/24/1999|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |SCOTT SPARKS R2 |
| |JOE HOLONICH NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: ALAN JONES | |
| HQ OPS OFFICER: FANGIE JONES | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|BAE1 20.2202(b)(1) PERS OVEREXPOSURE | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| POSSIBLE OVEREXPOSURE TO EMPLOYEES' EXTREMITIES |
| |
| Eastern Isotopes received their June 1999 exposure report from their vendor, |
| Proxtronics (Burke, VA), which indicated one individual received 50 rem to |
| the extremities as indicated by finger rings. The report also indicated |
| that two other individuals received higher than expected doses to their |
| extremities, 25 rem and 36 rem. Initial investigation indicated that the |
| highest dosage occurred to an individual who had the least number of duties |
| involving possible exposure. The individuals involved have been removed |
| from duties involving further exposures while further investigations are |
| carried out. The vendor has been contacted and suspects their standards and |
| controls, which they are investigating. A preliminary report from the |
| vendor is expected tomorrow. |
| |
| Eastern Isotopes handles Technetium and F18 (FDG). |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 36068 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: VERMONT YANKEE REGION: 1 |NOTIFICATION DATE: 08/25/1999|
| UNIT: [1] [] [] STATE: VT |NOTIFICATION TIME: 04:29[EDT]|
| RXTYPE: [1] GE-4 |EVENT DATE: 08/25/1999|
+------------------------------------------------+EVENT TIME: 01:48[EDT]|
| NRC NOTIFIED BY: DENNIS MAY |LAST UPDATE DATE: 08/25/1999|
| HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |KATHLEEN MODES R1 |
|10 CFR SECTION: | |
|AESF 50.72(b)(2)(ii) ESF ACTUATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| UNEXPECTED HIGH PRESSURE COOLANT INJECTION SYSTEM SUCTION SWAPOVER DURING |
| ROUTINE EMERGENCY DIESEL GENERATOR TESTING |
| |
| While using the "Diesel Generator Undervoltage Test Auto Start Switch" to |
| start the 'B' emergency diesel generator as part of a routine surveillance |
| test, an unexpected high pressure coolant injection system suction swapover |
| occurred, and three valves actuated to swap the suction from the condensate |
| storage tank (normal) to the torus. Apparently, a low spike was received on |
| both the DC1 system and condensate storage tank level when the "Diesel |
| Generator Undervoltage Test Auto Start Switch" was operated. After the |
| condensate storage tank and torus levels were verified to be normal, the |
| licensee swapped the high pressure coolant injection suction back to its |
| normal lineup. The licensee is currently investigating the cause of this |
| transient. |
| |
| The 'B' emergency diesel generator started as expected. |
| |
| The licensee plans to notify the NRC resident inspector and the State of |
| Vermont. |
+------------------------------------------------------------------------------+
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