Event Notification Report for March 26, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           03/25/1999 - 03/26/1999

                              ** EVENT NUMBERS **

35131  35447  35506  35507  35508  35509  35510  35511  35512  35513  35514  35515 


+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   35131       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 12/09/1998|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 22:17[EST]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        12/09/1998|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        18:20[EST]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  03/25/1999|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |MARK RING            R3      |
|  DOCKET:  0707002                              |WAYNE HODGES, EO     NMSS    |
+------------------------------------------------+BOB PIERSON          NMSS    |
| NRC NOTIFIED BY:  ERIC SPAETH                  |STU RUBIN, AEOD      IRD     |
|  HQ OPS OFFICER:  JOHN MacKINNON               |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NBNL                     RESPONSE-BULLETIN      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| NRC BULLETIN 91-01 RESPONSE, 4-HOUR NOTIFICATION - LOSS OF MODERATION  AND   |
| MASS CONTROL                                                                 |
|                                                                              |
| On 12/09/98 at 1820 EST, Plant Operations and Nuclear Criticality Safety     |
| personnel  identified that a Nuclear Criticality Safety Analysis (NCSA)      |
| requirement could not be maintained in the X-326 building.  NCSA-326_13.A06  |
| administrative control requirement #8 states, in part, "Within 8 hours after |
| cascade equipment shutdown (motor turned off) and with the system at a UF6   |
| negative, the system shall be pressurized with dry air or N2 buffer at 14    |
| psia or greater."  This cannot be accomplished for cell 25-7-2 due to the    |
| primary containment that was breached during a fire that occurred in the     |
| cell.  Also, cell 25-7-6 leaked to atmosphere prior to being buffered due to |
| possible failure of an expansion joint.  Each cell contains 12 converters,   |
| and the holes in the converters caused a loss of moderation control and loss |
| of mass control.  The holes in the converters can let air intrude into the   |
| converters which can cause a buildup of moisture in the converters.          |
|                                                                              |
| The certificate holder has isolated both cells and isolated the water system |
| going to both cells including the sprinkler system (fire protection system). |
| Visual inspection of a limited number of the converters and a review of      |
| typical cell inventory data reveals that the cells do not contain a critical |
| mass in them.  Also, the cells mentioned above have been isolated.           |
|                                                                              |
| The certificate holder notified the NRC Resident Inspector, the local        |
| Department of Energy (DOE) representative, and the state of Ohio.  The       |
| certificate holder also issued a press release.                              |
|                                                                              |
| * * * UPDATE AT 0512 EST ON 12/10/98 FROM ERIC SPAETH TO FANGIE JONES * * *  |
|                                                                              |
| This event notification is being updated to change the previous report of a  |
| 4-hour notification (loss of moderation and mass control) to a 24-hour       |
| notification due to current NDA scans that identify the deposits in          |
| converter 25-7-2 to be less than the calculated safe mass.  Loss of a single |
| contingency (moderation) remains a 24-hour notification.  Also, it was       |
| determined that the previous report of converter 25-7-6 leaking to           |
| atmosphere (potential loss of moderation control) was incorrect.  There was  |
| no failure in converter 25-7-6 that breached containment.                    |
|                                                                              |
| The certificate holder notified the NRC Resident Inspector, the local DOE    |
| representative, and the state of Ohio.  The NRC Operations Officer notified  |
| the R3DO (Mark Ring), NMSS EO (Wayne Hodges), and AEOD IRD (Joe Giitter).    |
|                                                                              |
| (See event #35130 and event #35132.)                                         |
|                                                                              |
| *** UPDATE ON 12/11/98 @ 1644 FROM SISLER TO GOULD ***                       |
|                                                                              |
| UPON FURTHER REVIEW OF THIS EVENT,  IT HAS BEEN DETERMINED THAT THE EVENT    |
| MEETS THE REPORTING CRITERIA  FOR OPERATIONS THAT COMPLY WITH THE DOUBLE     |
| CONTINGENCY PRINCIPLE WHERE MODERATION IS USED AS THE PRIMARY CRITICALITY    |
| CONTROL.  THE REPORTING CRITERIA CHANGED WHEN THE DEPOSIT IN 25-7-2 WAS      |
| DETERMINED TO BE LESS THAN A SAFE MASS.  NCSA-326_013.A06 ADMINISTRATIVE     |
| CONTROL REQUIREMENT NO. 8 WAS NOT RE-ESTABLISHED WITHIN 4 HOURS AFTER THE    |
| INITIAL OBSERVATION OF THE EVENT.  THAT CONTROL IS MODERATION, AND THE       |
| MODERATION CONTROL HAS YET TO BE RE-ESTABLISHED.  MASS CONTROL WAS           |
| MAINTAINED THROUGH THE EVENT.  THIS MEETS THE BULLETIN 91-01 4-HOUR          |
| REPORTING CRITERIA.  THIS EVENT SHOULD NOT HAVE BEEN DOWN GRADED TO A        |
| 24-HOUR REPORT.                                                              |
|                                                                              |
| PORTSMOUTH PERSONNEL NOTIFIED THE NRC RESIDENT INSPECTOR ALONG WITH DOE SITE |
| REPRESENTATIVE AND THE STATE.  THE NRC OPERATIONS OFFICER NOTIFIED THE R3DO  |
| (RING), NMSS EO (HODGES), AND AEOD IRD (CONGEL)                              |
|                                                                              |
| * * * UPDATE ON 3/25/99 AT 2111 EST BY RICK LARSON TO FANGIE JONES * * *     |
|                                                                              |
| Upon further review of this event, it has been determined that the event     |
| constituted only a single contingency in that the operation of the cascade   |
| is considered a single contingency in accordance with SAR 5.2.  Thus, the    |
| report of a double contingency loss was incorrect and the only contingency   |
| lost was moderation.  The report would still be an initial 4 hour            |
| notification requirement.                                                    |
|                                                                              |
| Portsmouth personnel notified the NRC Resident Inspector and the DOE site    |
| representative.  The NRC Operations Officer notified the R3DO (Melvyn        |
| Leach), NMSS EO (Robert Pierson), and IRO (Joseph Giitter).                  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35447       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: RIVER BEND               REGION:  4  |NOTIFICATION DATE: 03/08/1999|
|    UNIT:  [1] [] []                 STATE:  LA |NOTIFICATION TIME: 15:15[EST]|
|   RXTYPE: [1] GE-6                             |EVENT DATE:        03/08/1999|
+------------------------------------------------+EVENT TIME:        11:42[CST]|
| NRC NOTIFIED BY:  GEORGE TURNER                |LAST UPDATE DATE:  03/25/1999|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |GARY SANBORN         R4      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(vi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       82       Power Operation  |82       Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| INADVERTENT ACTUATION OF SINGLE OFFSITE SIREN DURING TESTING OF ACTUATION    |
| SYSTEM                                                                       |
|                                                                              |
| During Y2K testing of the offsite siren actuation system, a single siren     |
| actuated for about 5 seconds.  The test was terminated and the system        |
| returned to pretest conditions.  The licensee notified the Louisiana Office  |
| of Emergency Preparedness (LOEP) and informed them of the actuation.  The    |
| LOEP decided not to make a public announcement on the emergency alert system |
| as the siren was only actuated for a short period of time.                   |
|                                                                              |
| The licensee notified the local parishes and the NRC Resident Inspector.     |
|                                                                              |
| * * * UPDATE AT 1753 EST ON 3/25/99 BY GARY HOUSTON TO FANGIE JONES * * *    |
|                                                                              |
| The testing was not Y2K testing, but testing of a Y2K compliant software     |
| upgrade.  The Y2K testing was previously completed.  The licensee notified   |
| the NRC Resident Inspector.                                                  |
|                                                                              |
| The NRC Operations Officer notified the R4DO (Charles Cain).                 |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35506       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: GRAND GULF               REGION:  4  |NOTIFICATION DATE: 03/25/1999|
|    UNIT:  [1] [] []                 STATE:  MS |NOTIFICATION TIME: 00:18[EST]|
|   RXTYPE: [1] GE-6                             |EVENT DATE:        03/24/1999|
+------------------------------------------------+EVENT TIME:        21:00[CST]|
| NRC NOTIFIED BY:  DAVID H. HANKS               |LAST UPDATE DATE:  03/25/1999|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHARLES CAIN         R4      |
|10 CFR SECTION:                                 |                             |
|AINA 50.72(b)(2)(iii)(A) POT UNABLE TO SAFE SD  |                             |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION    |                             |
|NLCO                     TECH SPEC LCO A/S      |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| High Pressure Core Spray (HPCS) Division 3 Diesel Generator declared         |
| inoperable.                                                                  |
|                                                                              |
|                                                                              |
| HPCS (Division 3) EDG oil level was discovered to be out of specification    |
| low during normal rounds.  The Division 3 EDG was conservatively declared    |
| inoperable until further evaluations can be performed to determine final     |
| disposition of oil leakage from its inspection cover.  The licensee entered  |
| Technical Specification 3.8.1 (72 hour limiting conditioning of operation).  |
| All Emergency Core Cooling systems including HPCS are fully operable.        |
| Earlier in the day an undervoltage spike on the electrical grid caused the   |
| Division 3 EDG to start. The diesel was properly secured.                    |
|                                                                              |
| The NRC Resident Inspector was notified of this event by the licensee.       |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   35507       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 03/25/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 01:36[EST]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        03/24/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        19:00[EST]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  03/25/1999|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |PATRICK HILAND       R3      |
|  DOCKET:  0707002                              |ROBERT PIERSON       NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  ERIC SPAETH                  |                             |
|  HQ OPS OFFICER:  JOHN MacKINNON               |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|OCBB 76.120(c)(2)(ii)    EQUIP DISABLED/FAILS   |                             |
|OCBC 76.120(c)(2)(iii)   REDUNDANT EQUIP INOP   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| TSR allowed one of two smoke detectors to be inoperable during withdrawal    |
| operations when both smoke detectors have to be operable during withdrawal   |
| operations.                                                                  |
|                                                                              |
| On March 10, 1999, Operations personnel identified a deficiency in a TSR     |
| requirement for the Pigtail line Isolation System at ERP (extended range     |
| product), LAW (low assay withdrawal), and TAILS, (TSR 2.5.3.4). The TSR      |
| required action allowed continued withdrawal operations if one (1) smoke     |
| detector was inoperable.  The Pigtail Line Isolation System requires two (2) |
| Pyrotronics Smoke Detectors to actuate for the isolation valve to close.     |
| Operation personnel initiated a Compensatory Action (CA-99-009) for this     |
| anomaly to isolate the withdrawal cylinder and manifold per TSR 2.5.3.4b if  |
| one smoke detector is declared inoperable.                                   |
|                                                                              |
| Initially there was no evidence that the Pigtail Line Isolation System had   |
| been allowed to operate any applicable mode (modes II or III) with one or    |
| more inoperable smoke head.  As a follow up investigation to this            |
| deficiency, a search of the BPS system (problem report database) was         |
| conducted.  This search identified that on July 8, 1998, a Pyrotronic smoke  |
| head at the Law IA withdrawal position had been declared inoperable and      |
| cylinder filling operations had been allowed to continue.                    |
|                                                                              |
| This event is reportable due to a Safety System required by the TSR not      |
| being available or operable and no redundant equipment was available to      |
| perform the required safety function.                                        |
|                                                                              |
| The NRC Resident Inspector was notified of this event by the certificate     |
| holder.                                                                      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35508       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SUSQUEHANNA              REGION:  1  |NOTIFICATION DATE: 03/25/1999|
|    UNIT:  [] [2] []                 STATE:  PA |NOTIFICATION TIME: 02:34[EST]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        03/25/1999|
+------------------------------------------------+EVENT TIME:        01:30[EST]|
| NRC NOTIFIED BY:  GRANT FERNSLER               |LAST UPDATE DATE:  03/25/1999|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JACK MCFADDEN        R1      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| LOCAL LEAK RATE TEST PERFORMED ON THE "A" LOOP FEEDWATER CONTAINMENT         |
| PENETRATION FAILED.                                                          |
|                                                                              |
|                                                                              |
| An Appendix  "J" Local Leak Rate Test was performed on the "A" Loop          |
| Feedwater containment penetration.  The penetration piping was unable to be  |
| pressurized and therefore the leakrate exceeded Tech Spec limits.  The       |
| penetration is isolated and the condition does not represent an immediate    |
| threat to the public health or safety.                                       |
|                                                                              |
| The NRC Resident Inspector will notified of this event by the licensee.      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35509       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: CRYSTAL RIVER            REGION:  2  |NOTIFICATION DATE: 03/25/1999|
|    UNIT:  [3] [] []                 STATE:  FL |NOTIFICATION TIME: 08:52[EST]|
|   RXTYPE: [3] B&W-L-LP                         |EVENT DATE:        03/25/1999|
+------------------------------------------------+EVENT TIME:        08:12[EST]|
| NRC NOTIFIED BY:  SERGIO ORTIZ                 |LAST UPDATE DATE:  03/25/1999|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MARK LESSER          R2      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(vi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|3     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION MADE TO THE FLORIDA DEPARTMENT OF ENVIRONMENTAL         |
| PROTECTION CONCERNING A KEMPS RIDLEY SEA TURTLE BEING FOUND IN THE  INTAKE   |
| STRUCTURE.                                                                   |
|                                                                              |
| A SUB-ADULT KEMPS RIDLEY SEA TURTLE WAS FOUND IN THE PLANT'S INTAKE          |
| STRUCTURE. THE LIVE KEMPS RIDLEY SEA TURTLE WAS TRANSPORTED TO THE           |
| MARICULTURE CENTER FOR DISPOSITION/EVALUATION.  THE TURTLE WILL BE           |
| TRANSPORTED TO THE CLEARWATER MARINE SCIENCE CENTER FOR REHABILITATION. THE  |
| FLORIDA DEPARTMENT OF ENVIRONMENTAL PROTECTION WAS NOTIFIED BY THE LICENSEE  |
| OF THIS EVENT.                                                               |
|                                                                              |
| THE NRC RESIDENT INSPECTOR WILL BE NOTIFIED OF THIS EVENT BY THE LICENSEE.   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   35510       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  TEXAS DEPARTMENT OF HEALTH           |NOTIFICATION DATE: 03/25/1999|
|LICENSEE:  H & G INSPECTION                     |NOTIFICATION TIME: 15:45[EST]|
|    CITY:  HOUSTON                  REGION:  4  |EVENT DATE:        03/12/1999|
|  COUNTY:                            STATE:  TX |EVENT TIME:             [CST]|
|LICENSE#:  2181                  AGREEMENT:  Y  |LAST UPDATE DATE:  03/25/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |CHARLES CAIN         R4      |
|                                                |JOSEPH GIITTER       IRO     |
+------------------------------------------------+FRED COMBS           NMSS    |
| NRC NOTIFIED BY:                               |                             |
|  HQ OPS OFFICER:  FANGIE JONES                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|BAE1 20.2202(b)(1)       PERS OVEREXPOSURE      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT RECEIVED VIA FACSIMILE                                |
|                                                                              |
| The following text is a portion of a facsimile received from the Texas       |
| Department of Health:                                                        |
|                                                                              |
| "10 CFR Part 20.2202(b)(1) - Exposure (real or threatened) greater than or   |
| equal to TEDE of 5 rem, eye/lens 15 rem, skin/extremities 50 rads.           |
|                                                                              |
| "Incident report 7428:  A Texas licensee - H & G Inspection had a            |
| radiographer receive an annual 1998 whole body exposure of 5.4 R.   The      |
| Texas Department of Health Bureau of Radiation Control received the          |
| notification letter on 3/17/99 and is investigating."                        |
|                                                                              |
| There was no additional information available on the facsimile.              |
|                                                                              |
| See event number 35511.                                                      |
|                                                                              |
| (Call the NRC Operations Center for a contact telephone number and address.) |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   35511       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  TEXAS DEPARTMENT OF HEALTH           |NOTIFICATION DATE: 03/25/1999|
|LICENSEE:  H & G INSPECTION                     |NOTIFICATION TIME: 15:45[EST]|
|    CITY:  HOUSTON                  REGION:  4  |EVENT DATE:        03/12/1999|
|  COUNTY:                            STATE:  TX |EVENT TIME:             [CST]|
|LICENSE#:  2181                  AGREEMENT:  Y  |LAST UPDATE DATE:  03/25/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |CHARLES CAIN         R4      |
|                                                |JOSEPH GIITTER       IRO     |
+------------------------------------------------+FRED COMBS           NMSS    |
| NRC NOTIFIED BY:                               |                             |
|  HQ OPS OFFICER:  FANGIE JONES                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|BAE1 20.2202(b)(1)       PERS OVEREXPOSURE      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT RECEIVED VIA FACSIMILE                                |
|                                                                              |
| The following text is a portion of a facsimile received from the Texas       |
| Department of Health:                                                        |
|                                                                              |
| "10 CFR Part 20.2202(b)(1) - Exposure (real or threatened) greater than or   |
| equal to TEDE of 5 rem, eye/lens 15 rem, skin/extremities 50 rads.           |
|                                                                              |
| "Incident report 7429:  A Texas licensee - H & G Inspection had a            |
| radiographer receive an annual 1998 whole body exposure of 5.14 R.   The     |
| radiographer did not work together with the one in incident report 7428.     |
| The Texas Department of Health Bureau of Radiation Control received the      |
| notification letter on 3/17/99 and is investigating."                        |
|                                                                              |
| There was no additional information available on the facsimile.              |
|                                                                              |
| See event number 35510.                                                      |
|                                                                              |
| (Call the NRC Operations Center for a contact telephone number and address.) |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35512       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: COMANCHE PEAK            REGION:  4  |NOTIFICATION DATE: 03/25/1999|
|    UNIT:  [1] [2] []                STATE:  TX |NOTIFICATION TIME: 17:37[EST]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        03/25/1999|
+------------------------------------------------+EVENT TIME:        16:04[CST]|
| NRC NOTIFIED BY:  TOM BEAUDIN                  |LAST UPDATE DATE:  03/25/1999|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHARLES CAIN         R4      |
|10 CFR SECTION:                                 |                             |
|DDDD 73.71               UNSPECIFIED PARAGRAPH  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| PHYSICAL SECURITY REPORT                                                     |
|                                                                              |
| Unescorted access granted inappropriately to contract employee.  Immediate   |
| compensatory measures taken upon discovery.                                  |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
|                                                                              |
| Refer to the HOO Log for additional details.                                 |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   35513       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 03/25/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 18:16[EST]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        03/25/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        10:03[EST]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  03/25/1999|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |MELVYN LEACH         R3      |
|  DOCKET:  0707002                              |ROBERT PIERSON       NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  J. B. HALCOMB                |                             |
|  HQ OPS OFFICER:  FANGIE JONES                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NCFR                     NON CFR REPORT REQMNT  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| VALID ACTUATION OF A 'Q' SAFETY SYSTEM                                       |
|                                                                              |
| "At 1003 hours on March 25, 1999, during normal charging of cell 31-3-3      |
| prior to placing onstream, an Operations                                     |
| Front Line Manager was investigating a Cascade Automatic Data Processing     |
| smokehead alarm from this cell when a second smokehead alarmed.  He than saw |
| what appeared to be smoke above the Stage 6 area.                            |
|                                                                              |
| "All personnel in the area immediately evacuated, implemented the 'See &     |
| Flee' Procedure, activated the building recall system, and notified          |
| Emergency Response Forces.  The cell was taken offstream and cell pressure   |
| was reduced below atmosphere.                                                |
|                                                                              |
| "All airborne and surface contamination sample results were less than        |
| detectable and there was no release of                                       |
| Hazardous/Radioactive material or Radioactive/Radiological contamination     |
| exposure as a result of this event."                                         |
|                                                                              |
| The facility notified the NRC Resident Inspector and the DOE Site Manager.   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   35514       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  TEXAS DEPARTMENT OF HEALTH           |NOTIFICATION DATE: 03/25/1999|
|LICENSEE:  TEAM CONSULTANTS                     |NOTIFICATION TIME: 18:08[EST]|
|    CITY:  DALLAS                   REGION:  4  |EVENT DATE:        03/22/1999|
|  COUNTY:                            STATE:  TX |EVENT TIME:             [CST]|
|LICENSE#:  4012                  AGREEMENT:  Y  |LAST UPDATE DATE:  03/25/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |CHARLES CAIN         R4      |
|                                                |ROBERT PIERSON       NMSS    |
+------------------------------------------------+JOSEPH GIITTER       IRO     |
| NRC NOTIFIED BY:  HELEN WATKINS                |                             |
|  HQ OPS OFFICER:  FANGIE JONES                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|BAB1 20.2201(a)(1)(i)    LOST/STOLEN LNM>1000X  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT RECEIVED VIA FACSIMILE                                |
|                                                                              |
| The following text is a portion of a facsimile received from the Texas       |
| Department of Health:                                                        |
|                                                                              |
| "10 CFR Part 20.2201(a)(1)(I) - Report of theft/loss of greater than or      |
| equal to 1000 X App C value."                                                |
|                                                                              |
| Incident report 7431:  A Texas licensee - Team Consultants, reported that a  |
| Troxler 3411B, SN 11125, Moisture Density Gauge containing Cs-137 and        |
| Am-241:Be was stolen.  The Texas Department of Health Bureau of Radiation    |
| Control received the notification letter on 3/22/99 and is following up to   |
| obtain additional information.                                               |
|                                                                              |
| There was no additional information available on the facsimile.              |
|                                                                              |
| (Call the NRC Operations Center for a contact telephone number and address.) |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35515       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: RIVER BEND               REGION:  4  |NOTIFICATION DATE: 03/25/1999|
|    UNIT:  [1] [] []                 STATE:  LA |NOTIFICATION TIME: 21:11[EST]|
|   RXTYPE: [1] GE-6                             |EVENT DATE:        03/25/1999|
+------------------------------------------------+EVENT TIME:        16:40[CST]|
| NRC NOTIFIED BY:  JOEY CLARK                   |LAST UPDATE DATE:  03/25/1999|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHARLES CAIN         R4      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       78       Power Operation  |78       Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| ESF ACTUATION RESULTING IN ISOLATION OF A DIVISION 2 VALVE                   |
|                                                                              |
| "An invalid ESF actuation resulted in the isolation of Division 2 primary    |
| containment isolation valve RHSAOV62 SUPPRESSION POOL CLEANUP (SPC) SYSTEM   |
| SUCTION.                                                                     |
|                                                                              |
| "During outage preparation activities in the Reactor Building Dryer storage  |
| pool, level in the pool was inadvertently lowered approximately three and    |
| one-half inches, resulting in a non-ESF isolation signal from the division 2 |
| dryer pool level indicator.  The level change was caused by a siphon effect  |
| that was created through a vacuum hose being staged between the Dryer Pool   |
| and Refueling Cavity for pool cleanup.                                       |
|                                                                              |
| "The lowering level was terminated upon identification and all systems       |
| responded as designed."                                                      |
|                                                                              |
| The siphon action was started during 'bump' testing of the vacuuming system  |
| during setup due to the differences in pool levels of about one foot.  Work  |
| has been terminated until an investigation is completed and necessary        |
| changes to the work are made.                                                |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+


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