Event Notification Report for January 15, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           01/14/1999 - 01/15/1999

                              ** EVENT NUMBERS **

35206  35248  35259  35260  35261  35262  35263  35264  35265  35266  

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35206       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PERRY                    REGION:  3  |NOTIFICATION DATE: 12/30/1998|
|    UNIT:  [1] [] []                 STATE:  OH |NOTIFICATION TIME: 19:03[EST]|
|   RXTYPE: [1] GE-6                             |EVENT DATE:        12/30/1998|
+------------------------------------------------+EVENT TIME:        16:00[EST]|
| NRC NOTIFIED BY:  HENRY KELLY                  |LAST UPDATE DATE:  01/14/1999|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MONTE PHILLIPS       R3      |
|10 CFR SECTION:                                 |                             |
|NLTR                     LICENSEE 24 HR REPORT  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 24-HOUR REPORT REQUIRED BY PLANT OPERATING LICENSE DUE TO VIOLATION OF       |
| TECHNICAL SPECIFICATIONS                                                     |
|                                                                              |
| The licensee has discovered that a solenoid-operated isolation valve on a    |
| 3/8" diameter sample line from the secondary containment was excluded from   |
| the plant technical specifications (TS), and, consequently, it was not       |
| subject to surveillances required by the TS.  The valve is located on a      |
| secondary containment atmosphere sample line which connects to the           |
| post-accident sampling system.  The licensee has verified that the valve is  |
| closed.                                                                      |
|                                                                              |
| The NRC resident inspector has been informed of this event by the licensee.  |
|                                                                              |
| * * * UPDATE AT 2117 EST ON 01/14/99 FROM BRIAN STETSON TO S. SANDIN * * *   |
|                                                                              |
| The following text is a portion of a facsimile received from the licensee:   |
|                                                                              |
| "During the extent of condition investigation of Condition Report 98-2142,   |
| it was identified that instrument vent and drain valves associated with the  |
| reactor core isolation cooling system (E51) and the annulus exhaust gas      |
| treatment system (M15) could fit the definition of secondary containment     |
| isolation valves as discussed in Technical Specification Bases 3.6.4.2.      |
| However, these valves are not surveilled and checked closed every 31 days as |
| required by Surveillance Requirement 3.6.4.2.1.  There are 12 valves (3/8")  |
| associated with E51, and 8 valves (1/4") associated with M15."               |
|                                                                              |
| The licensee plans to continue its evaluation and has informed the NRC       |
| Resident Inspector.  The NRC Operations Officer notified the R3DO (Gavula).  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35248       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: CLINTON                  REGION:  3  |NOTIFICATION DATE: 01/13/1999|
|    UNIT:  [1] [] []                 STATE:  IL |NOTIFICATION TIME: 10:21[EST]|
|   RXTYPE: [1] GE-6                             |EVENT DATE:        01/13/1999|
+------------------------------------------------+EVENT TIME:        08:35[CST]|
| NRC NOTIFIED BY:  ROBERT POWER                 |LAST UPDATE DATE:  01/14/1999|
|  HQ OPS OFFICER:  LEIGH TROCINE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JIM GAVULA           R3      |
|10 CFR SECTION:                                 |                             |
|AESS 50.72(b)(1)(v)      EMERGENCY SIREN INOP   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| LOSS OF HALF OF THE OFFSITE EMERGENCY SIRENS DUE TO FREEZING RAIN            |
|                                                                              |
| The following text is a portion of a facsimile received from the licensee:   |
|                                                                              |
| "10CFR50.72(b)(1)(v) requires that a facility notify the NRC Operations      |
| Center during any event that results in a major loss of emergency offsite    |
| response capability.  Due to weather conditions causing area power outages,  |
| a system test of the emergency sirens was conducted.  During this test, it   |
| was discovered that 22 out of 44 emergency sirens were not functioning.      |
| Therefore, Clinton Power Station is making a notification pursuant to        |
| 10CFR50.72(b)(1)(v)."  The licensee's current site policy is to make a       |
| notification of this type if less than 90% of the emergency sirens are       |
| available.                                                                   |
|                                                                              |
| The licensee notified the NRC resident inspector.                            |
|                                                                              |
| *** UPDATE ON 01/14/99 @ 1442 EST FROM POWERS TO GOULD ***                   |
|                                                                              |
| As of 0930 CST, the plant restored power to all but four emergency sirens.   |
|                                                                              |
| The NRC resident inspector will be notified by the licensee.  The R3DO       |
| (Gavula) was notified by the NRC operations officer.                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35259       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BIG ROCK POINT           REGION:  3  |NOTIFICATION DATE: 01/14/1999|
|    UNIT:  [1] [] []                 STATE:  MI |NOTIFICATION TIME: 03:26[EST]|
|   RXTYPE: [1] GE-1                             |EVENT DATE:        01/14/1999|
+------------------------------------------------+EVENT TIME:        03:00[EST]|
| NRC NOTIFIED BY:  MIKE AZURE                   |LAST UPDATE DATE:  01/14/1999|
|  HQ OPS OFFICER:  LEIGH TROCINE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JIM GAVULA           R3      |
|10 CFR SECTION:                                 |                             |
|AENS 50.72(b)(1)(v)      ENS INOPERABLE         |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Decommissioned   |0        Decommissioned   |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| LOSS OF EMERGENCY NOTIFICATION SYSTEM (ENS) AND COMMERCIAL TELEPHONES        |
|                                                                              |
| At 0300, it was discovered that the FTS-2000 ENS telephone line and the      |
| offsite commercial telephone lines were out of service. The cause of this    |
| telephone outage is unknown at this time.  However, the licensee stated that |
| there does not seem to be a trunk line problem.  The licensee has contacted  |
| Ameritech and a local telephone representative.  Offsite communications are  |
| available via the use of cellular telephones and base radios to the Michigan |
| State Police and to the licensee's power control (load dispatcher).  Outside |
| calls can be made from those locations if it is necessary for the licensee   |
| to relay information.                                                        |
|                                                                              |
| (Call the NRC Operations Center for a licensee cellular telephone number.)   |
|                                                                              |
| ******************** UPDATE AT 1009 ON 01/14/99 FROM GARY RUEHLE TO TROCINE  |
| ********************                                                         |
|                                                                              |
| Telephone service was restored at approximately 0930, and the ENS line       |
| tested satisfactorily at 1009.  The telephone outage was due to an Ameritech |
| problem.                                                                     |
|                                                                              |
| The NRC operations officer notified the R3DO (Gavula).                       |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Hospital                                         |Event Number:   35260       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  HAWAIIAN EYE CENTER                  |NOTIFICATION DATE: 01/14/1999|
|LICENSEE:  HAWAIIAN EYE CENTER                  |NOTIFICATION TIME: 13:00[EST]|
|    CITY:  WAHIAWA                  REGION:  4  |EVENT DATE:        01/14/1999|
|  COUNTY:  HONOLULU                  STATE:  HI |EVENT TIME:             [HST]|
|LICENSE#:  53-18343-01           AGREEMENT:  N  |LAST UPDATE DATE:  01/14/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |BLAIR SPITZBERG      R4      |
|                                                |JOHN SURMEIER, EO    NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  CYNTHIA SEMBRANO             |                             |
|  HQ OPS OFFICER:  STEVE SANDIN                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|LADM 35.33(a)            MED MISADMINISTRATION  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| LICENSEE REPORTED THAT NUMEROUS PATIENTS RECEIVED LESS THAN THE PRESCRIBED   |
| Sr-90 DOSE.                                                                  |
|                                                                              |
| IN 1998, TWELVE (12) PATIENTS WERE DIAGNOSED AND TREATED FOR PTERYGIUM, A    |
| SUPERFICIAL GROWTH ON THE LENS OF THE EYE,  ELEVEN HUNDRED (1,100) RADS WAS  |
| PRESCRIBED FOR EACH; HOWEVER, DUE TO THE LICENSEE NOT APPLYING A DECAY       |
| FACTOR TO THE STRONTIUM-90 SOURCE, PATIENTS RECEIVED APPROXIMATELY 600 RADS. |
| THE TWO (2) EYE APPLICATORS (SERIAL #s 0302 AND 431 - EACH 100 mCi Sr-90)    |
| WERE  RECEIVED FROM NEW ENGLAND NUCLEAR IN MARCH 1979.  THE DISCREPANCY IN   |
| THE PRESCRIBED VERSUS ADMINISTERED DOSE WAS DISCOVERED DURING AN ONSITE      |
| INSPECTION  BY THE NRC ON 01/13/99.  THE LICENSEE IS CONTINUING ITS          |
| INVESTIGATION TO DETERMINE APPROPRIATE CORRECTIVE ACTIONS.                   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35261       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: HARRIS                   REGION:  2  |NOTIFICATION DATE: 01/14/1999|
|    UNIT:  [1] [] []                 STATE:  NC |NOTIFICATION TIME: 13:06[EST]|
|   RXTYPE: [1] W-3-LP                           |EVENT DATE:        01/14/1999|
+------------------------------------------------+EVENT TIME:        09:18[EST]|
| NRC NOTIFIED BY:  MARK PALMER                  |LAST UPDATE DATE:  01/14/1999|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |AL BELISLE           R2      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|APRE 50.72(b)(2)(vi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     A/R        Y       100      Power Operation  |0        Hot Standby      |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AUTOMATIC REACTOR TRIP ON TRIP OF TWO OF THREE REACTOR COOLANT PUMPS AND     |
| LOSS OF TWO 6.9-kV BUSES                                                     |
|                                                                              |
| During relay calibration on the 'A' 6.9-kV non-safety bus, the bus was       |
| unexpectedly deenergized.  The 'C' 6.9-kV bus is a swing bus and was tied to |
| the 'A' 6.9-kV bus, which caused it to be deenergized also.  This caused the |
| loss of two of three reactor coolant pumps, and in turn, caused an automatic |
| reactor trip from 100% power.  All systems functioned as expected, all rods  |
| fully inserted, and auxiliary feedwater started on low steam generator level |
| as expected.  All safety systems are operable except the 'A' containment     |
| hydrogen analyzer which is out of service for planned maintenance.           |
|                                                                              |
| The exact cause of the loss of the 6.9-kV buses is currently under           |
| investigation.                                                               |
|                                                                              |
| The licensee notified the NRC Resident Inspector, the State of North         |
| Carolina, and the local county.                                              |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35262       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FITZPATRICK              REGION:  1  |NOTIFICATION DATE: 01/14/1999|
|    UNIT:  [1] [] []                 STATE:  NY |NOTIFICATION TIME: 13:38[EST]|
|   RXTYPE: [1] GE-4                             |EVENT DATE:        01/14/1999|
+------------------------------------------------+EVENT TIME:        13:11[EST]|
| NRC NOTIFIED BY:  RICK PLASSE                  |LAST UPDATE DATE:  01/14/1999|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          UNU                   |CURT COWGILL         RI      |
|10 CFR SECTION:                                 |JOHN STOLZ, NRR      EO      |
|AAEC 50.72(a)(1)(i)      EMERGENCY DECLARED     |FRANK CONGEL         IRO     |
|NOCM                     COMM ASST BRIEF        |SULLIVAN             FEMA    |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| THE LICENSEE DECLARED AN UNUSUAL EVENT DUE TO A FIRE LASTING LONGER THAN 15  |
| MINUTES INSIDE THE PROTECTED AREA.  (REFER TO EVENT #s 35263 AND 35264 FOR   |
| RELATED EVENTS.)                                                             |
|                                                                              |
| AT 1256 EST, OPERATORS RECEIVED A REPORT OF AN ONGOING FIRE IN THE VICINITY  |
| OF THE HYDROGEN TANK FARM AREA APPROXIMATELY 300 FEET WEST OF THE PLANT.     |
| THE SOURCE IS A HYDROGEN RELEASE.  THE LOCATION OF THE SOURCE HAS NOT BEEN   |
| IDENTIFIED.  THE LICENSEE EVACUATED PERSONNEL IN THE AREA AND DECLARED AN    |
| UNUSUAL EVENT AT 1311 EST DUE TO AN ONGOING FIRE LASTING LONGER THAN 15      |
| MINUTES.  OFFSITE FIRE ASSISTANCE WAS REQUESTED FROM THE SCRIBA FIRE         |
| DEPARTMENT.  ALL PERSONNEL ARE ACCOUNTED FOR WITH ONE KNOWN MINOR INJURY.    |
| ALL SAFETY EQUIPMENT IS AVAILABLE.  BOTH 115-kV SOURCES OF OFFSITE POWER     |
| WERE DEENERGIZED AS A SAFETY PRECAUTION TO ALLOW FIREFIGHTERS' ACCESS.  THE  |
| LICENSEE IS MAINTAINING ELECTRICAL LOADS ON GENERATOR OUTPUT WITH THE        |
| STANDBY EMERGENCY DIESEL GENERATORS RUNNING UNLOADED.  THE LICENSEE INFORMED |
| NEW YORK STATE AND THE NRC RESIDENT INSPECTOR.                               |
|                                                                              |
| * * * UPDATE AT 1424 EST ON 01/14/99 * * *                                   |
|                                                                              |
| AT 1424 EST, THE NRC ENTERED THE MONITORING PHASE OF NORMAL MODE.            |
|                                                                              |
| * * * UPDATE AT 1500 EST ON 01/14/99 * * *                                   |
|                                                                              |
| A COMMISSIONERS' ASSISTANTS BRIEFING WAS CONDUCTED.  THE FOLLOWING           |
| NOTIFICATIONS WERE MADE (* OFFICE DID NOT PARTICIPATE):  IRO (CONGEL AND     |
| WEINSTEIN); JACKSON (MILLER); DICUS (CHAN); DIAZ (HSIA); McGAFFIGAN (BEALL); |
| MERRIFIELD (McCABE); EDO (HILTZ); DEDE (MITCHELL*); NRR EO (STOLZ); R1DO     |
| (COWGILL); PAO (GILLILAND); CAO (MADDEN); SECY (BATES); SP (LARKINS); IP     |
| (FAULKNER); BRIEFER (COWGILL); SRI (RASMUSSEN); AND NRR (BAWA, WONG, LONG,   |
| AND CONNELL).                                                                |
|                                                                              |
| * * * UPDATE AT 1730 EST ON 01/14/99 * * *                                   |
|                                                                              |
| A COMMISSIONERS' ASSISTANTS BRIEFING WAS CONDUCTED.  THE FOLLOWING           |
| NOTIFICATIONS WERE MADE:  IRO (CONGEL), JACKSON (MILLER), DICUS (CHAN), DIAZ |
| (HSIA), McGAFFIGAN (BEALL), MERRIFIELD (McCABE), EDO (HILTZ), BRIEFER        |
| (COWGILL), SRI (RASMUSSEN), AND NRR (BAWA AND WILLIAM).                      |
|                                                                              |
| * * * UPDATE AT 2111 EST ON 01/14/99 FROM TOM KERR TO FANGIE JONES * * *     |
|                                                                              |
| THE LICENSEE TERMINATED THE UNUSUAL EVENT AT  2105 EST.  THE LICENSEE        |
| INFORMED THE NRC RESIDENT INSPECTOR.                                         |
|                                                                              |
| * * * UPDATE AT 2120 EST ON 01/14/99 * * *                                   |
|                                                                              |
| THE NRC EXITED THE MONITORING PHASE OF NORMAL MODE AT 2108 EST.  THE NRC     |
| OPERATIONS OFFICER NOTIFIED THE NRR EO (BOGER), IRO (CONGEL), AND FEMA       |
| (CANUPP).                                                                    |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35263       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: NINE MILE POINT          REGION:  1  |NOTIFICATION DATE: 01/14/1999|
|    UNIT:  [1] [] []                 STATE:  NY |NOTIFICATION TIME: 14:23[EST]|
|   RXTYPE: [1] GE-2,[2] GE-5                    |EVENT DATE:        01/14/1999|
+------------------------------------------------+EVENT TIME:        13:47[EST]|
| NRC NOTIFIED BY:  REVETTE                      |LAST UPDATE DATE:  01/14/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          UNU                   |GENE KELLY           R1      |
|10 CFR SECTION:                                 |JOHN STOLZ, NRR      EO      |
|AAEC 50.72(a)(1)(i)      EMERGENCY DECLARED     |CIBOCH               FEMA    |
|                                                |FRANK CONGEL         IRO     |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| THE LICENSEE DECLARED AN UNUSUAL EVENT DUE TO PLANT'S PROXIMITY TO A         |
| HYDROGEN FIRE AT FITZPATRICK.  (REFER TO EVENT #s 35262 AND 35264 FOR        |
| RELATED EVENTS.)                                                             |
|                                                                              |
| THE LICENSEE IS DOING A PRECAUTIONARY STAFFING OF ITS TECHNICAL SUPPORT      |
| CENTER DUE TO THE FIRE AT FITZPATRICK.                                       |
|                                                                              |
| THE LICENSEE HAS NOTIFIED THE NRC RESIDENT INSPECTOR AS WELL AS STATE,       |
| LOCAL, AND OTHER AGENCIES.  THERE WILL BE NO PRESS RELEASE.                  |
|                                                                              |
| * * * UPDATE AT 2139 EST ON 01/14/99 FROM STAN LUCAS TO S.SANDIN * * *       |
|                                                                              |
| UNIT 1 EXITED THE UNUSUAL EVENT AT 2125 EST BASED ON TERMINATION OF THE      |
| FITZPATRICK UNUSUAL EVENT.                                                   |
|                                                                              |
| THE LICENSEE INFORMED STATE/LOCAL AGENCIES AND THE NRC RESIDENT INSPECTOR.   |
| THE NRC OPERATIONS OFFICER NOTIFIED R1DO (KELLY), NRR EO (BOGER), IRO        |
| (CONGEL), AND FEMA (STEINDURF).                                              |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35264       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: NINE MILE POINT          REGION:  1  |NOTIFICATION DATE: 01/14/1999|
|    UNIT:  [] [2] []                 STATE:  NY |NOTIFICATION TIME: 14:23[EST]|
|   RXTYPE: [1] GE-2,[2] GE-5                    |EVENT DATE:        01/14/1999|
+------------------------------------------------+EVENT TIME:        13:47[EST]|
| NRC NOTIFIED BY:  WEAVER                       |LAST UPDATE DATE:  01/14/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          UNU                   |GENE KELLY           R1      |
|10 CFR SECTION:                                 |JOHN STOLZ, NRR      EO      |
|AAEC 50.72(a)(1)(i)      EMERGENCY DECLARED     |CIBOCH               FEMA    |
|                                                |FRANK CONGEL         IRD     |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| THE LICENSEE DECLARED AN UNUSUAL EVENT DUE TO PLANT'S PROXIMITY TO A         |
| HYDROGEN FIRE AT FITZPATRICK.  (REFER TO EVENT #s 35262 AND 35263 FOR        |
| RELATED EVENTS.)                                                             |
|                                                                              |
| THE LICENSEE IS EVACUATING PERSONNEL FROM ITS BUILDINGS LOCATED ON THE EAST  |
| SIDE OF THE SITE OUTSIDE THE PROTECTED AREA FENCE.  THESE BUILDINGS WERE     |
| APPROXIMATELY SEVERAL HUNDRED YARDS FROM THE FIRE SITE.  THIS ACTION WAS     |
| RECOMMENDED BY A LOCAL OFFICIAL BASED ON THE FIRE AT THE FITZPATRICK SITE    |
| WHICH BORDERS NINE MILE POINT'S EAST BOUNDARY.  IT IS REPORTED THAT HYDROGEN |
| WILL BE VENTED FOR SEVERAL HOURS.  WIND DIRECTION IS FROM FITZPATRICK SITE   |
| TOWARDS NINE MILE POINT.                                                     |
|                                                                              |
| THE NRC RESIDENT INSPECTOR WAS NOTIFIED ALONG WITH STATE, LOCAL, AND OTHER   |
| GOVERNMENT AGENCIES.  THE LICENSEE PLANS TO ISSUE A PRESS RELEASE.           |
|                                                                              |
| * * * UPDATE AT 2139 EST ON 01/14/99 FROM STAN LUCAS TO S.SANDIN * * *       |
|                                                                              |
| UNIT 2 EXITED THE UNUSUAL EVENT AT 2125 EST BASED ON TERMINATION OF THE      |
| FITZPATRICK UNUSUAL EVENT.                                                   |
|                                                                              |
| THE LICENSEE INFORMED STATE/LOCAL AGENCIES AND THE NRC RESIDENT INSPECTOR.   |
| THE NRC OPERATIONS OFFICER NOTIFIED THE R1DO (KELLY), NRR EO (BOGER), IRO    |
| (CONGEL) AND FEMA (STEINDURF).                                               |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35265       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BROWNS FERRY             REGION:  2  |NOTIFICATION DATE: 01/14/1999|
|    UNIT:  [] [] [3]                 STATE:  AL |NOTIFICATION TIME: 20:26[EST]|
|   RXTYPE: [1] GE-4,[2] GE-4,[3] GE-4           |EVENT DATE:        01/14/1999|
+------------------------------------------------+EVENT TIME:        16:40[CST]|
| NRC NOTIFIED BY:  RODNEY NACOSTE               |LAST UPDATE DATE:  01/14/1999|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |AL BELISLE           R2      |
|10 CFR SECTION:                                 |                             |
|AINB 50.72(b)(2)(iii)(B) POT RHR INOP           |                             |
|NLCO                     TECH SPEC LCO A/S      |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|                                                   |                          |
|3     N          Y       100      Power Operation  |100      Power Operation  |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| LICENSEE DECLARED HIGH PRESSURE COOLANT INJECTION (HPCI) INOPERABLE DUE TO   |
| AN OIL LEAK OBSERVED DURING START OF THE PUMP.                               |
|                                                                              |
| THE FOLLOWING TEXT IS A PORTION OF A FACSIMILE RECEIVED FROM THE LICENSEE:   |
|                                                                              |
| "DURING THE PERFORMANCE OF [PROCEDURE] 3-SR-3.5.1.7,  HPCI MAIN AND BOOSTER  |
| PUMP SET DEVELOPED HEAD AND FLOW RATE TEST, WHILE THE HPCI PUMP WAS          |
| STARTING, AN OIL LEAK DEVELOPED ON [VALVE] 3-SV-73-18, HPCI STOP VALVE.  ONE |
| STUD WAS FOUND SHEARED FROM THE STOP VALVE.  HPCI WAS SUBSEQUENTLY DECLARED  |
| INOPERABLE, AND THE APPROPRIATE [LIMITING CONDITIONS FOR OPERATION] WERE     |
| ENTERED."                                                                    |
|                                                                              |
| THE LICENSEE IS CONDUCTING AN INVESTIGATION TO DETERMINE THE CAUSE OF THE    |
| FAILURE AND THE APPROPRIATE CORRECTIVE ACTIONS.                              |
|                                                                              |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35266       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DRESDEN                  REGION:  3  |NOTIFICATION DATE: 01/14/1999|
|    UNIT:  [] [2] [3]                STATE:  IL |NOTIFICATION TIME: 21:27[EST]|
|   RXTYPE: [1] GE-1,[2] GE-3,[3] GE-3           |EVENT DATE:        01/14/1999|
+------------------------------------------------+EVENT TIME:        20:12[CST]|
| NRC NOTIFIED BY:  SALGADO                      |LAST UPDATE DATE:  01/14/1999|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JAMES CREED, REG 3   IAT     |
|10 CFR SECTION:                                 |JOHN DAVIDSON, NMSS  IAT     |
|DDDD 73.71               UNSPECIFIED PARAGRAPH  |RICHARD ROSANO, NRR  IAT     |
|                                                |BRUCE BOGER, NRR     EO      |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|3     N          Y       100      Power Operation  |100      Power Operation  |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| There was an unauthorized entry into the protected area, and immediate       |
| compensatory measures were taken upon discovery.  (Contact the NRC           |
| Operations Center for additional details.)                                   |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+


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