Morning Report for August 1, 2001
Headquarters Daily Report AUGUST 01, 2001 *************************************************************************** REPORT NEGATIVE NO INPUT ATTACHED INPUT RECEIVED RECEIVED HEADQUARTERS X REGION I X REGION II X REGION III X REGION IV X PRIORITY ATTENTION REQUIRED MORNING REPORT - REGION III AUGUST 1, 2001 Licensee/Facility: Notification: Exelon Generation Company, Llc MR Number: 3-01-0026 Byron 1 2 Date: 07/24/01 Byron,Illinois SRI Via Telecon Dockets: 50-454,50-455 PWR/W-4-LP,PWR/W-4-LP Subject: UNIT 2C STEAM GENERATOR PRIMARY TO SECONDARY LEAKAGE Discussion: On July 24, 2001, the licensee informed the Senior Resident Inspector of an identified primary to secondary leak in the Unit 2C steam generator. The initial leak rate was approximately 2-3 gallons per day (gpd) and slowly increased to about 6-7 gpd on August 1, 2001. The leakage was identified by slightly elevated radiation levels at the steam jet air ejector exhaust, the steam generator blowdown system, and the main steam line. At this time, the leakage is very low; however, the licensee has implemented additional grab sampling at the steam jet air ejector exhaust. The licensee has also created a higher level of awareness with the operators. The administrative limits for shutdown are 75 gpd leakage or an increase of greater than 30 gpd within 1 hour. Technical Specification limits are 150 gpd on one steam generator or 600 gpd total. Regional Action: The resident inspectors are monitoring the activities with support from regional specialists. Contact: Ann Marie Stone (630)829-9729 _
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021