Event Notification Report for November 12, 2020
U.S. Nuclear Regulatory Commission
Operations Center
EVENT REPORTS FOR
11/11/2020 - 11/12/2020
EVENT NUMBERS
54995
54995
Power Reactor
Event Number: 54995
Facility: Vogtle
Region: 2 State: GA
Unit: [] [2] []
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: Jason Thomas
HQ OPS Officer: Brian P. Smith
Region: 2 State: GA
Unit: [] [2] []
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: Jason Thomas
HQ OPS Officer: Brian P. Smith
Notification Date: 11/12/2020
Notification Time: 21:14 [ET]
Event Date: 11/12/2020
Event Time: 17:32 [EST]
Last Update Date: 11/12/2020
Notification Time: 21:14 [ET]
Event Date: 11/12/2020
Event Time: 17:32 [EST]
Last Update Date: 11/12/2020
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
Person (Organization):
MARK MILLER (R2DO)
MARK MILLER (R2DO)
| Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
|---|---|---|---|---|---|---|
| 2 | A/R | Y | 100 | Power Operation | 0 | Hot Standby |
AUTOMATIC REACTOR TRIP DUE TO TURBINE TRIP
"At 1732 EST on November 12, 2020, with Unit 2 in Mode 1 and 100 percent power, the reactor automatically tripped due to a turbine trip. The trip was not complex with all systems responding normally post trip. Operations responded and stabilized the plant. Decay heat is being removed by the steam generators through the steam dumps into the condenser. Unit 1 is not affected.
"An automatic actuation of the Auxiliary Feedwater System (AFW) also occurred. The AFW auto-start is an expected response from the reactor trip.
"Due to the Reactor Protection System actuation while critical, this event is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B), as well as in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the Auxiliary Feedwater System. There was no impact on the health and safety of the public or plant personnel.
"The NRC Resident Inspector has been notified."
"At 1732 EST on November 12, 2020, with Unit 2 in Mode 1 and 100 percent power, the reactor automatically tripped due to a turbine trip. The trip was not complex with all systems responding normally post trip. Operations responded and stabilized the plant. Decay heat is being removed by the steam generators through the steam dumps into the condenser. Unit 1 is not affected.
"An automatic actuation of the Auxiliary Feedwater System (AFW) also occurred. The AFW auto-start is an expected response from the reactor trip.
"Due to the Reactor Protection System actuation while critical, this event is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B), as well as in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the Auxiliary Feedwater System. There was no impact on the health and safety of the public or plant personnel.
"The NRC Resident Inspector has been notified."