U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/16/2012 - 08/17/2012 ** EVENT NUMBERS ** | Power Reactor | Event Number: 48197 | Facility: FERMI Region: 3 State: MI Unit: [2] [ ] [ ] RX Type: [2] GE-4 NRC Notified By: JEFF GROSS HQ OPS Officer: JOHN SHOEMAKER | Notification Date: 08/16/2012 Notification Time: 21:02 [ET] Event Date: 08/16/2012 Event Time: 14:58 [EDT] Last Update Date: 08/17/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE | Person (Organization): JOHN GIESSNER (R3DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | N | Y | 68 | Power Operation | 68 | Power Operation | Event Text INTEGRATED PLANT COMPUTER FAILURE "At approximately 1458 EDT on 8/16/12, a portion of the Fermi 2 Integrated Plant Computer System (IPCS) failed. This resulted in a loss of approximately 60 percent of data on the Safety Parameters Display System (SPDS). "While IPCS and SPDS are not fully functional, the Emergency Plan can still be implemented if a plant emergency does occur, as assessment capabilities are available under alternate means. "Repairs are in progress. A follow up message will be made when IPCS and SPDS are restored to fully functional status. "This notification is being made pursuant to the requirements 10 CFR 50.72(b)(3)(xiii), any event that results in a major loss of emergency assessment capability." The licensee has notified the NRC Resident Inspector. * * * UPDATE FROM GROFF TO KLCO ON 8/17/12 AT 0429 EDT* * * "At approximately 1458 EDT on 8/16/12, a portion of the Fermi 2 Integrated Plant Computer System (IPCS) failed. This resulted in a loss of approximately 60 percent of data on the Safety Parameters Display System (SPDS). "At 2340 [EDT], plant personnel were able to restore full functionality of IPCS and SPDS, restoring full Emergency assessment capabilities to all onsite emergency response facilities." The licensee notified the NRC Resident Inspector. Notified the R3DO (Giessner). | Power Reactor | Event Number: 48198 | Facility: SEQUOYAH Region: 2 State: TN Unit: [ ] [2] [ ] RX Type: [1] W-4-LP,[2] W-4-LP NRC Notified By: TRACY SUDOKO HQ OPS Officer: MARK ABRAMOVITZ | Notification Date: 08/16/2012 Notification Time: 22:09 [ET] Event Date: 08/16/2012 Event Time: 19:26 [EDT] Last Update Date: 08/16/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): EUGENE GUTHRIE (R2DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | A/R | Y | 100 | Power Operation | 0 | Hot Standby | Event Text REACTOR TRIP FROM A REACTOR COOLANT PUMP TRIP "At 1926 EDT on 8/16/2012, Unit 2 reactor automatically tripped on single loop loss of flow, following #4 RCP trip. Cause of RCP trip is under investigation. "Following the reactor trip, all safety related equipment operated as designed. Auxiliary feedwater actuated as expected on loss of the operating main feedwater pumps. "Unit 2 is currently being maintained in Mode 3 at NOP/NOT [normal operating pressure/normal operating temperature], with auxiliary feedwater supplying the steam generator. "Method of decay heat removal is via steam dumps to condenser. Current RCS conditions: Temp = 547 degrees F and stable, Pressure = 2235 psig and stable. No indication of any primary/secondary leakage. All rods are inserted. Electrical alignment is normal, supplied from offsite power. No impact to Unit 1: Unit 1 is operating at 100% power / Mode 1." The licensee notified the NRC Resident Inspector. | |