U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/15/2005 - 06/16/2005 ** EVENT NUMBERS ** | !!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!! | Power Reactor | Event Number: 41743 | Facility: TURKEY POINT Region: 2 State: FL Unit: [ ] [4] [ ] RX Type: [3] W-3-LP,[4] W-3-LP NRC Notified By: GRANT MELIN HQ OPS Officer: BILL GOTT | Notification Date: 06/03/2005 Notification Time: 01:00 [ET] Event Date: 06/03/2005 Event Time: 00:33 [EDT] Last Update Date: 06/15/2005 | Emergency Class: UNUSUAL EVENT 10 CFR Section: 50.72(a) (1) (i) - EMERGENCY DECLARED | Person (Organization): ROBERT HAAG (R2) PATRICK HILAND (NRR) TIM MCGINTY (IRD) JOEL MUNDAY (R2) INSUNG LEE (DHS) CHRIS LIGGET (FEMA) MIKE SMITH (DOE) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 4 | N | N | 0 | Hot Standby | 0 | Hot Standby | Event Text DECLARED UNUSUAL EVENT DUE TO RCS LEAKAGE IN EXCESS OF TECHNICAL SPECIFICATION LIMIT "Declared Unusual Event due to RCS leakage greater than 10 gallons per minute. VCT level is lowering with constant plant temperature, pressure and pressurizer level. VCT level lowering at approximately 19 gallons per minute with associated rise in RWST level approximately 20 gallons per minute." The licensee will notify the NRC Resident Inspector. * * * UPDATE FROM MELIN TO W. GOTT AT 0120 ON 06/03/05 * * * The licensee briefed NRC Management (McGinty, P. Hiland, R. Haag, J Munday) that the leakage was verified to be CVCS leakage and not RCS leakage. The leakage was stopped at 0055 and the licensee is evaluating termination/retraction criteria. NRC will not enter Monitoring Mode. * * * UPDATE FROM G MELIN TO W. GOTT AT 0140 ON 06/03/05 * * * "At 0055, leakage stopped. Leakage verified to be CVCS leakage, not RCS. The leakage is stopped. Validating no other anomalies exist then will evaluate termination and retraction of UE notification." * * * UPDATE FROM G MELIN TO P. SNYDER AT 0221 ON 06/03/05 * * * "Notification of termination of Unusual Event at 0221. Plant validation complete. RCS gross leakage is 0.07 gallon per minute and plant parameters are stable. Leakage confirmed to be from CVCS system which has been isolated." The licensee will notify the NRC Resident Inspector. Notified R2DO (R. Haag), NRR EO (P. Hiland), IRD (T. McGinty), R2 (J. Munday), DHS (I. Lee), FEMA (C. Ligget), and DOE (M. Smith) * * * UPDATE ON 6/15/05 @ 1243 FROM JIM SPEICHER TO CHAUNCEY GOULD * * * RETRACTION Event Notice 41743 reported declaration of an Unusual Event at 00:33 on 6/3/05 for RCS leakage in excess of Technical Specification Limits. The source of leakage was subsequently determined to be from the Chemical and Volume Control System (CVCS) and not from the RCS. The Unusual Event was terminated at 02:00 6/3/05 after the leak was isolated. This event is retracted since the source of the leakage was not from the RCS and upon further review the event did not meet reporting requirements. The NRC Resident Inspector was notified. RDO (Tom Decker), EO (M. Mayfield) and IRD (Peter Wilson) were notified | General Information or Other | Event Number: 41764 | Rep Org: FLORIDA BUREAU OF RADIATION CONTROL Licensee: SAILOR ENGINEERING ASSOCIATES Region: 1 City: LAWRENCEVILLE State: GA County: License #: G114-1 Agreement: Y Docket: NRC Notified By: CHARLES ADAMS HQ OPS Officer: JOHN KNOKE | Notification Date: 06/10/2005 Notification Time: 17:33 [ET] Event Date: 06/10/2005 Event Time: [EDT] Last Update Date: 06/10/2005 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): TODD JACKSON (R1) PATRICIA HOLAHAN (NMSS) TAS email only (TAS) | Event Text AGREEMENT STATE REPORT - LOST TROXLER GAUGE The State of Florida reported that a Troxler gauge, Model # 3411B, Serial # 8280, was found in the trunk of a vehicle in which the occupants were being investigated for attempted robbery. The incident location was at a Wal-Mart store in Lake City, Florida. The gauge, which was impounded and placed in Florida's DOT District Office, was found undamaged. The Soil Moisture Density Gauge will remain in a licensed storage area until picked up by the owner. The isotopes used in the gauge are 10 mCi of Cs-137 and 40 mCi of Am-241/Be. Incident Number FL05-093 | General Information or Other | Event Number: 41768 | Rep Org: NC DIV OF RADIATION PROTECTION Licensee: FORSYTH MEMORIAL MEDICAL CENTER Region: 1 City: WINSTON-SALEM State: NC County: License #: 034-0878-3 Agreement: Y Docket: NRC Notified By: CLIFFTON R. HARRIS HQ OPS Officer: ARLON COSTA | Notification Date: 06/13/2005 Notification Time: 17:20 [ET] Event Date: 05/27/2005 Event Time: [EDT] Last Update Date: 06/13/2005 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): PAUL KROHN (R1) KERRY LANDIS (R2) PATRICIA HOLAHAN (NMSS) TAS (Email) () | Event Text NC AGREEMENT STATE REPORT ON HDR SOURCE MISSING IN TRANSIT A Varian Medical Systems technician replaced a source from a high dose rate (HDR) brachytherapy unit at the Forsyth Memorial Medical Center on 5/26/05. The technician then shipped the replaced source on 5/27/05 in a type A package via Federal Express to Excel Logistics (Freight Forwarder for Varian) in Sterling, Virginia. The shipped source contains 3.3 Curies of Iridium-192. The source was not received at Excel Logistics Sterling, VA. The Varian Radiation Safety Officer contacted the Federal Express on 6/10/05. The package was reported missing with its last known location at the Federal Express hub in Memphis, Tennessee. The search for the package is ongoing. | Power Reactor | Event Number: 41774 | Facility: DIABLO CANYON Region: 4 State: CA Unit: [1] [2] [ ] RX Type: [1] W-4-LP,[2] W-4-LP NRC Notified By: DAVE BAHNER HQ OPS Officer: MIKE RIPLEY | Notification Date: 06/15/2005 Notification Time: 00:10 [ET] Event Date: 06/14/2005 Event Time: 20:50 [PDT] Last Update Date: 06/15/2005 | Emergency Class: UNUSUAL EVENT 10 CFR Section: 50.72(a) (1) (i) - EMERGENCY DECLARED | Person (Organization): JACK WHITTEN (R4) PETE WILSON (NSIR) MICHAEL MAYFIELD (NRR) A. AKERS (DHS) J. DUNKER (FEMA) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | 2 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text NOTIFICATION OF UNUSUAL EVENT DUE TO TSUNAMI WARNING Diablo Canyon Units 1 and 2 declared a Notification of Unusual Event at 2050 PDT 06/14/05 due to the receipt of a Tsunami Warning from the California State Warning Center. The licensee notified State and local agencies and will notify the NRC Resident Inspector. The NRC remained in the Normal Mode. * * * UPDATE FROM D. BAHNER TO M. RIPLEY 0045 EDT 06/15/05 * * * The Tsunami Warning was cancelled and Diablo Canyon Units 1 and 2 terminated the Notification of Unusual Event at 2138 PDT 06/14/05. The licensee notified State and local agencies and the NRC Resident Inspector. | Power Reactor | Event Number: 41775 | Facility: HUMBOLDT BAY Region: 4 State: CA Unit: [3] [ ] [ ] RX Type: [3] GE-1 NRC Notified By: ZANE EASLEY HQ OPS Officer: BILL HUFFMAN | Notification Date: 06/15/2005 Notification Time: 00:00 [ET] Event Date: 06/14/2005 Event Time: 20:00 [PDT] Last Update Date: 06/15/2005 | Emergency Class: UNUSUAL EVENT 10 CFR Section: 50.72(a) (1) (i) - EMERGENCY DECLARED | Person (Organization): JACK WHITTEN (R4) MICHAEL MAYFIELD (NRR) PETER WILSON (IRD) C.W. (BILL) REAMER (NMSS) J. DUNKER (FEMA) A. AKERS (DHS) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 3 | N | N | 0 | Decommissioned | 0 | Decommissioned | Event Text NOTIFICATION OF UNUSUAL EVENT DUE TO TSUNAMI WARNING At 1951 PDT, an earthquake of magnitude 7.4 on the Richter scale was reported at a location near Crescent City, CA. This is approximately 85 miles NW of Humboldt Bay and about 300 miles NW of San Francisco, CA. Based on the earthquake, a Tsunami Warning was issued for California coastal sites by NOAA and promulgated by the California State Warning Center. Based on the Tsunami Warning, Humboldt declared an Unusual Event at 2000 PDT. The licensee stated that the earthquake was not felt at Humboldt but that precautionary measures had been taken to move plant staff to higher ground for personnel safety based on the Tsunami Warning. During the initial notification call from the licensee, notification was received from the California State Warning Center that the Tsunami Warring had been canceled. The licensee has been coordinating with local authorities. The NRC remained in the Normal Mode. * * * UPDATE FROM EASLEY TO HUFFMAN AT 1235 EDT ON 06/15/05 * * * Based on the cancellation of the Tsunami Warning the licensee terminated the Unusual Event at 2104 EDT. | Power Reactor | Event Number: 41777 | Facility: CALLAWAY Region: 4 State: MO Unit: [1] [ ] [ ] RX Type: [1] W-4-LP NRC Notified By: JOHN WEEKLEY HQ OPS Officer: STEVE SANDIN | Notification Date: 06/15/2005 Notification Time: 16:06 [ET] Event Date: 06/15/2005 Event Time: 08:02 [CDT] Last Update Date: 06/15/2005 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE | Person (Organization): JACK WHITTEN (R4) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text EMERGENCY OFFSITE FACILITY DECLARED INOPERABLE DUE TO AIR FILTRATION FAN FAILURE TO START "On 06/15/2005 at 08:02 [CDT] the Callaway Plant declared the Emergency Offsite Facility (EOF) Inoperable due to the EOF air filtration fan not starting when the system was switched from Normal to Filtration Mode. This was discovered during a scheduled emergency plan drill. "Repair of the ventilation system is being pursued in a priority manner. Compensatory measures have been put in place. The Backup Emergency Offsite Facility (EOF) is available to support the Emergency Plan. "The resident inspector was notified." | Power Reactor | Event Number: 41779 | Facility: COLUMBIA GENERATING STATION Region: 4 State: WA Unit: [2] [ ] [ ] RX Type: [2] GE-5 NRC Notified By: FRED SCHILL HQ OPS Officer: CHAUNCEY GOULD | Notification Date: 06/15/2005 Notification Time: 18:38 [ET] Event Date: 06/15/2005 Event Time: 14:00 [PDT] Last Update Date: 06/15/2005 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): JACK WHITTEN (R4) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | A/R | Y | 100 | Power Operation | 0 | Hot Shutdown | Event Text AUTOMATIC REACTOR SCRAM DUE TO TURBINE THROTTLE VALVE CLOSURE "On June 15, 2005 at 1400 PDT Columbia Generating Station experienced a Reactor Protection System (RPS) actuation while operating at full power. Currently, reactor level is being controlled with the feedwater system and reactor pressure is being controlled via the turbine bypass valves to the condenser. All safety systems functioned as expected and there was no ECCS system injection. The initial attempt to trip the main turbine from the control room was unsuccessful and it was subsequently tripped locally. At this time the plant is stable and indications show that the RPS actuation originated from closure of turbine throttle valves. Determination of the cause of the RPS actuation is ongoing at this time." All rods fully inserted and no relief valves lifted. The NRC Resident Inspector was notified. | |