U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/14/2006 - 04/17/2006 ** EVENT NUMBERS ** | Power Reactor | Event Number: 42504 | Facility: PRAIRIE ISLAND Region: 3 State: MN Unit: [1] [ ] [ ] RX Type: [1] W-2-LP,[2] W-2-LP NRC Notified By: DOUG SMITH HQ OPS Officer: BILL GOTT | Notification Date: 04/14/2006 Notification Time: 16:07 [ET] Event Date: 04/14/2006 Event Time: 14:25 [CDT] Last Update Date: 04/14/2006 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): THOMAS KOZAK (R3) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | M/R | Y | 100 | Power Operation | 0 | Hot Standby | Event Text MANUAL REACTOR TRIP DUE TO CONDENSATE PUMP AND FEEDWATER PUMP TRIP "At 1425 on April 14, 2006, a lockout trip of 11 Condensate Pump occurred. The condensate pump trip caused an expected lockout trip of 11 Main Feedwater Pump trip. With the loss of 50% of feedwater pump capacity, the Shift Supervisor directed a manual Unit 1 reactor trip. The manual reactor trip was successful and all systems responded as expected. The reactor protection system actuation is reportable under 10CFR 50.72(b)(2). A reactor trip from full power results in an expected steam generator narrow range level shrink to 0%. This resultant narrow range steam generator level caused an expected Auxiliary Feedwater System Actuation. Both 11 and 12 Auxiliary Feedwater Pumps started as expected. Auxiliary feedwater actuation is reportable under10CFR 50.72(b)(3). "Investigation is underway to determine the cause of 11 Condensate Pump lockout. "Plant operations are underway per emergency procedure 1ES-0.1, Reactor Trip Recovery, and 1C1.3, Unit 1 Shutdown, to stabilize the plant in Mode 3, Hot Standby." All control rods fully inserted. Steam generators are discharging steam to the condenser steam dump system. The Auxiliary Feedwater Pumps are maintaining Steam Generator level. The electrical grid is stable. The licensee will notify the NRC Resident Inspector. | Power Reactor | Event Number: 42505 | Facility: RIVER BEND Region: 4 State: LA Unit: [1] [ ] [ ] RX Type: [1] GE-6 NRC Notified By: VERNON CARLSON HQ OPS Officer: MARK ABRAMOVITZ | Notification Date: 04/15/2006 Notification Time: 20:52 [ET] Event Date: 04/15/2006 Event Time: 16:15 [CDT] Last Update Date: 04/16/2006 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL | Person (Organization): TROY PRUETT (R4) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | A/R | Y | 100 | Power Operation | 0 | Hot Shutdown | Event Text REACTOR SCRAM FROM 100% POWER "At 1615 CDT time on April 15th, 2006 with the Reactor at 100% power, River Bend Station experienced a reactor scram resulting from a RPS actuation. All plant systems performed as designed. The reactor is stable with pressure and temperature being controlled by feed water system and main steam bypass valves, respectively. The cause of the scram is not known at this time. The plant is conducting causal investigations to fully understand the cause of the plant scram." All control rods fully inserted, no safety valves lifted, and no Emergency Safety Feature actuations occurred on the scram. The electrical grid is stable. The licensee notified the NRC Resident Inspector. * * * UPDATE AT 1033 EDT ON 4/16/06 FROM KENNETH HIGGINBOTHAM TO S. SANDIN * * * "River Bend Station status on 04/16/2006: The unit is in Mode 3, Hot Shutdown, and stable. Investigation of the plant trip found an optical isolator in the control circuit for the end-of-cycle recirculation pump trip failed causing both recirculation pumps to shift to slow speed. The pump downshift placed reactor power and flow into the exclusion region of the power to flow map. The reactor received trip signals from APRM E & H heat flux exceeding their corresponding trip set points. The optical isolator is being replaced. Plant restart will commence pending successful replacement of the optical isolator." The licensee informed the NRC Resident Inspector. Notified R4DO (Pruett). | Power Reactor | Event Number: 42506 | Facility: VOGTLE Region: 2 State: GA Unit: [1] [ ] [ ] RX Type: [1] W-4-LP,[2] W-4-LP NRC Notified By: STEVE PHILLIPS HQ OPS Officer: STEVE SANDIN | Notification Date: 04/17/2006 Notification Time: 01:20 [ET] Event Date: 04/17/2006 Event Time: 00:26 [EDT] Last Update Date: 04/17/2006 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): ROBERT HAAG (R2) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | M/R | Y | 33 | Power Operation | 0 | Hot Standby | Event Text UNIT 1 MANUALLY TRIPPED DUE TO FAILURE OF A MAIN FEED REGULATING VALVE TO CONTROL STEAM GENERATOR LEVEL "Unit 1 reactor was manually tripped from 33% RTP due to the Loop 3 Main Feed Regulating Valve (MFRV) 1LV-0530 not controlling steam generator level in manual or AUTO. "A unit shutdown was in progress at the time of the trip due to concerns with the Loop 3 MFRV. The unit shutdown had commenced from 100% power on 04/16/2006 at 1603 hrs. "All systems functioned as required on the reactor trip including a feedwater isolation and the Loop 3 MRFV closing as expected. The unit is presently in Mode 3 at normal operating temperature and pressure. An investigation team is being assembled concerning the Loop 3 MFRV." All control rods fully inserted. No primary or secondary reliefs/safeties lifted during the transient. Unit 1 is currently in Mode 3 Hot Standby controlling Steam Generator Water Level using Auxiliary Feedwater supplied by both Motor Driven and the Steam Driven pumps. Decay Heat is being removed via the Bypass Valves to the Main Condenser. Offsite power is stable and all EDGs are available, if necessary. The licensee informed the NRC Resident Inspector. | |