Information Notice No. 91-69: Errors in Main Steam Line Break Analyses for Determining Containment Parameters
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, D.C. 20555
November 1, 1991
NRC INFORMATION NOTICE 91-69: ERRORS IN MAIN STEAM LINE BREAK ANALYSES
FOR DETERMINING CONTAINMENT PARAMETERS
Addressees
All holders of operating licenses or construction permits for pressurized
water reactors (PWRs).
Purpose
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information
notice to alert addressees to a safety problem that may result from not
considering the possibility that feedwater could continue to flow following
a main steam line break (MSLB) inside the containment. This problem is
applicable to plants equipped with feedwater isolation susceptible to single
failure. It is expected that recipients will review the information for
applicability to their facilities and consider actions, as appropriate, to
avoid similar problems. However, suggestions contained in this information
notice are not NRC requirements; therefore, no specific action or written
response is required.
Description of Circumstances
On October 18, 1991, the Northeast Nuclear Energy Company notified the NRC
of a problem at the Millstone Nuclear Power Station, Unit 2, that could
cause the facility to exceed containment design limits. The licensee found
this concern during MSLB analyses for the forthcoming replacement of the
steam generators. In performing the analyses, the licensee identified that
during full power operation, with a break on a main steam line, and with
offsite power available, a single failure of a feedwater control valve to
close could result in higher peak containment temperature and pressure than
the design limits. The containment design limits for temperature and
pressure were 289�F and 54 psig; the new analysis shows preliminary values
of 420�F and 68 psig, respectively. Previously, the licensee's worst case
analysis assumed loss of offsite power with a MSLB.
Discussion
NRC Bulletin No. 80-04, "Analysis of a PWR Main Steam Line Break with
Continued Feedwater Addition" and Standard Review Plan (NUREG 800) Section
6.2.1.4 provide guidance for assuming a single failure of any active
component, with and without offsite power available, and discuss the effect
of such a failure on the ability to ensure containment integrity following a
MSLB. The Bulletin also addresses the possibility of the reactor returning
to power. Offsite power remaining available could be more limiting for
containment parameters.
9110290103
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IN 91-69
November 1, 1991
Page 2 of 2
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Reactor Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contacts: Thomas Koshy, NRR
(301) 492-1176
William LeFave, NRR
(301) 492-2385
Attachment: List of Recently Issued NRC Information Notices
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