U.S. Nuclear Regulatory Commission Operations Center Event Reports For 5/22/2018 - 5/23/2018 ** EVENT NUMBERS ** |
Agreement State | Event Number: 53400 | Rep Org: TEXAS DEPT OF STATE HEALTH SERVICES Licensee: TOLUNAY-WONG ENGINEERS INCORPORATED Region: 4 City: HOUSTON State: TX County: License #: L04848 Agreement: Y Docket: NRC Notified By: KAREN BLANCHARD HQ OPS Officer: ANDREW WAUGH | Notification Date: 05/14/2018 Notification Time: 12:39 [ET] Event Date: 05/12/2018 Event Time: 00:00 [CDT] Last Update Date: 05/14/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): HEATHER GEPFORD (R4DO) NMSS_EVENTS_NOTIFICATION (EMAIL) MARK MACDONALD (ILTAB) - CNSNS (MEXICO) (EMAIL) | This material event contains a "Less than Cat 3" level of radioactive material. | Event Text TEXAS AGREEMENT STATE REPORT - STOLEN TROXLER GAUGE
The following information was obtained from the State of Texas via email:
"On May 14, 2018, the licensee notified the Agency [Texas Department of State Health Services] that on the morning of May 12, 2018, one of its Troxler model 3430+ moisture/density gauges (SN: 69854), containing a 40 milliCurie americium-241 source (SN: 47-19592) and an 8 milliCurie cesium-137 source (SN: 77-13965), had been stolen from a licensee's vehicle while it was parked at a restaurant in Houston, Texas. The gauge was locked inside its transport case which was secured with chains in the back of the licensee's vehicle. The technician had stopped to eat breakfast between picking up the gauge at the licensed site and reporting to the temporary job site. When he arrived at the job site, he found the chains cut, the gauge and standard plate had been stolen, but the transport case was still there. The technician reported the theft to his supervisors who did not report to the licensee's radiation safety officer until May 14th. The theft has been reported to local law enforcement. An investigation into this event is ongoing."
Texas Incident Number: 9571
THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL
Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf |
Agreement State | Event Number: 53402 | Rep Org: NE DIV OF RADIOACTIVE MATERIALS Licensee: CHURCH OF JESUS CHRIST OF LATTER DAY SAINTS - NORFOLK Region: 4 City: NORFOLK State: NE County: License #: GL0370 Agreement: Y Docket: NRC Notified By: MALISA MCCOWN HQ OPS Officer: ANDREW WAUGH | Notification Date: 05/15/2018 Notification Time: 17:28 [ET] Event Date: 05/15/2018 Event Time: 00:00 [CDT] Last Update Date: 05/15/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): HEATHER GEPFORD (R4DO) NMSS_EVENTS_NOTIFICATION (EMAIL) | This material event contains a "Less than Cat 3" level of radioactive material. | Event Text NEBRASKA AGREEMENT STATE REPORT - TWO MISSING TRITIUM EXIT SIGNS
The following information was obtained from the State of Nebraska via email:
"GL0370 Church of Jesus Christ of Latter Day Saints - Norfolk submitted their Annual Renewal and Inventory on March 9, 2018. On May 15, 2018, GL0370 re-submitted their Inventory, indicating that two tritium exit signs were missing. A follow-up phone call placed to the licensee indicated the licensee did not actually conduct an inventory of the devices prior to the March 9th documentation. They have searched through all back records and can find no indication of when the devices were removed.
"Source number 1 information: Device name: Sealed Source Luminous Manufacturer: Isolite Model Number: SLX60 Serial Number: 10-7234 Radionuclide: H-3 Activity: 10 Ci
"Source number 2 information: Device name: Sealed Source Luminous Manufacturer: Isolite Model Number: SLX60 Serial Number: 10-17588 Radionuclide: H-3 Activity: 10 Ci"
Nebraska Item Number: NE180004
THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL
Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.p |
Power Reactor | Event Number: 53416 | Facility: COOPER Region: 4 State: NE Unit: [1] [] [] RX Type: [1] GE-4 NRC Notified By: TERREL HIGGINS HQ OPS Officer: THOMAS KENDZIA | Notification Date: 05/22/2018 Notification Time: 13:36 [ET] Event Date: 05/22/2018 Event Time: 09:00 [CDT] Last Update Date: 05/22/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(xi) - OFFSITE NOTIFICATION | Person (Organization): JASON KOZAL (R4DO) | Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text UNPLANNED PUBLIC NOTIFICATION DURING A DRILL
"On 05/22/2018, Cooper Nuclear Station (CNS) was conducting an Emergency Response Organization (ERO) drill which included state and local involvement. At approximately 09:00 CST Nebraska Emergency Management Agency (NEMA) inadvertently broadcasted CNS' declaration of a Notice of Unusual Event for the drill over the public scanner. This resulted in various members of the public or news media inquiring about the perceived event or posting erroneous information via Twitter, television news outlets, newspapers, and radio stations. These news outlets have been informed that CNS was conducting a drill and do not intend to release any stories regarding this event. There is no evidence of a formal news release at this time. However, due to the uncontrolled source of the information, the determination was made to make this report.
"This unplanned media event is a 4 hour report, in accordance with 10CFR50.72(b)(2)(xi). This event is not significant with respect to the health and safety of the public.
"The licensee notified the NRC Resident Inspector." |
Power Reactor | Event Number: 53418 | Facility: OYSTER CREEK Region: 1 State: NJ Unit: [1] [] [] RX Type: [1] GE-2 NRC Notified By: BRYAN EAGAN HQ OPS Officer: THOMAS KENDZIA | Notification Date: 05/22/2018 Notification Time: 15:36 [ET] Event Date: 05/22/2018 Event Time: 10:28 [EDT] Last Update Date: 05/22/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 26.719 - FITNESS FOR DUTY | Person (Organization): ANTHONY DIMITRIADIS (R1DO) FFD GROUP (EMAIL) | Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text FITNESS FOR DUTY - LICENSED OPERATOR CONFIRMED POSITIVE TEST
"A licensed operator had a confirmed positive test during a random fitness-for-duty test. The individual was not performing licensed duties. The individual's qualifications and plant access were removed. A work performance investigation has been completed. Work performed by the individual has been verified to be compliant with all standards.
"The NRC Resident Inspector has been notified." |
!!!!! THIS EVENT HAS BEEN RETRACTED.THIS EVENT HAS BEEN RETRACTED !!!!! | Power Reactor | Event Number: 53419 | Facility: BEAVER VALLEY Region: 1 State: PA Unit: [1] [] [] RX Type: [1] W-3-LP,[2] W-3-LP NRC Notified By: JIM DOUGHERTY HQ OPS Officer: THOMAS KENDZIA | Notification Date: 05/22/2018 Notification Time: 18:38 [ET] Event Date: 05/22/2018 Event Time: 12:56 [EDT] Last Update Date: 06/21/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(i) - PLANT S/D REQD BY TS 50.72(b)(3)(ii)(B) - UNANALYZED CONDITION 50.72(b)(3)(v)(B) - POT RHR INOP 50.72(b)(3)(v)(D) - ACCIDENT MITIGATION | Person (Organization): ANTHONY DIMITRIADIS (R1DO) | Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text GAS VOIDS DISCOVERED IN BOTH TRAINS OF LOW HEAD SAFETY INJECTION
"On 5/22/2018, while operating at approximately 100 percent power, Ultrasonic Testing of the Beaver Valley Power Station (BVPS) Unit 1 Low Head Safety Injection (LHSI) pump suction piping identified gas voids in excess of the acceptable limit for void volume. Both trains of LHSI were declared inoperable. Technical Specification (TS) 3.5.2 for both trains of the LHSI system was entered along with TS 3.0.3 which requires the initiation of a plant shutdown. Time of TS entry was 12:56 (EDT).
"Plant shutdown was commenced at 15:56 (EDT) in accordance with plant procedures.
"At 15:59 (EDT) Train 'A' LHSI was restored to operable status, TS 3.0.3 Action was exited and the power reduction was stopped at approximately 99 percent.
"At 17:43 (EDT) Train 'B' LHSI was restored to operable status, TS 3.5.2 Actions were exited.
"This is reportable per 10 CFR 50.72(b)(3)(ii) Unanalyzed Condition, 10 CFR 50.72(b)(3)(v) Event or Condition that Could Have Prevented the Fulfillment of a Safety Function and 10 CFR 50. 72(b )(2)(i) TS Required Shutdown.
"The NRC Resident Inspector has been notified."
* * * RETRACTION ON 6/21/18 AT 1535 EDT FROM SHAWN KEENER TO RICHARD SMITH * * *
"Further engineering evaluation has determined that the gas voids that existed at the time of discovery would not have rendered the LHSI [Low Head Safety Injection] system inoperable if it were required to actuate. The engineering evaluation concluded that filling of the containment sump during a Design Basis Accident would result in a void volume reduction such that the void in the LHSI suction piping would not be large enough to significantly impact the operability of the system. Therefore, the system remained operable but degraded. No TSs [Technical Specifications] were required to be entered and no shutdown was required. As such, all three reporting criteria do not apply and are being retracted.
"The NRC Resident Inspector has been notified."
Notified R1DO (Burritt). |
Part 21 | Event Number: 53422 | Rep Org: WESTINGHOUSE ELECTRIC COMPANY Licensee: WESTINGHOUSE Region: 1 City: CRANBERRY TOWNSHIP State: PA County: License #: Agreement: Y Docket: NRC Notified By: JAMES GRESHAM HQ OPS Officer: THOMAS KENDZIA | Notification Date: 05/23/2018 Notification Time: 14:19 [ET] Event Date: 05/23/2018 Event Time: 00:00 [EDT] Last Update Date: 05/23/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 21.21(d)(3)(i) - DEFECTS AND NONCOMPLIANCE | Person (Organization): ANTHONY DIMITRIADIS (R1DO) EUGENE GUTHRIE (R2DO) ROBERT DALEY (R3DO) JASON KOZAL (R4DO) - PART 21/50.55 REACTORS (EMAIL) | Event Text PART 21 - WEAR OF THERMAL SLEEVE IN WESTINGHOUSE CONTROL ROD DRIVE MECHANISMS
The following notification is an excerpt from the received report:
"Westinghouse nuclear steam supply system (NSSS) plants that have thermal sleeves in the control rod drive mechanism (CRDM) penetration tubes, wear of the thermal sleeve flange against the tube could have safety consequences that were not previously considered. Recent operating experience, during startup procedures at an Electricite de France (EdF) plant, has shown the possibility for the flange remnant from a thermal sleeve to interfere with control rod movement."
Potential affected plants include, A. W. Vogtle 1 & 2, Braidwood 1 & 2, Byron 1 & 2, Callaway, Catawba 1 & 2, Comanche Peak 1 & 2, Diablo Canyon 1 & 2, McGuire 1 & 2, Millstone 3, Seabrook, Sequoyah 1 & 2, Shearon Harris, South Texas 1 & 2, Watts Bar 1 & 2, Wolf Creek, Beaver Valley 1 & 2, D.C. Cook 1 & 2, Indian Point 2 & 3, North Anna 1 & 2, Point Beach 1 & 2, Prairie Island 1 & 2, R. E. Ginna, Salem 1 & 2, Surry 1 & 2, and Turkey Point 3 & 4.
Name and address of the individual or individuals informing the Commission. James A. Gresham Westinghouse Electric Company 1000 Westinghouse Drive, Suite 259 Cranberry Township, Pennsylvania 16066 Direct tel: (412) 374-4643 Direct fax: (724) 940-8560 e-mail: greshaja@westinghouse.com |
Power Reactor | Event Number: 53423 | Facility: COMANCHE PEAK Region: 4 State: TX Unit: [] [2] [] RX Type: [1] W-4-LP,[2] W-4-LP NRC Notified By: LOREN STUCK HQ OPS Officer: THOMAS KENDZIA | Notification Date: 05/23/2018 Notification Time: 16:10 [ET] Event Date: 05/23/2018 Event Time: 08:48 [CDT] Last Update Date: 05/23/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE | Person (Organization): JASON KOZAL (R4DO) | Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text LOSS OF EMERGENCY ASSESSMENT CAPABILITY
"At time 0848 (CDT), Main Steamline Radiation Monitor 2-RE-2328 (Main Steamline 2-04) lost communications and was declared non-functional. "With this radiation monitor non-functional, all of the emergency action levels for a steam generator tube rupture in steam generator 2-04 could neither be evaluated nor monitored. This unplanned condition is reportable as a loss of assessment capability per 10CFR50.72(b)(3)(xiii).
"Comanche Peak Nuclear Power Plant [CPNPP] has assurance of steam generator integrity and fuel cladding integrity and there is a negligible safety significance to the current condition from a public health and safety perspective.
"Additionally, compensatory measures are in place to assure adequate monitoring capability is available to implement the CPNPP emergency plan in the unlikely event of challenges to the steam generator or fuel cladding. The N16 radiation monitor serves as a backup with alarm function and Radiation Protection technicians have been briefed on taking local readings with a Geiger-Mueller tube on MSL 2-04.
"Corrective actions are being pursued to restore 2-RE-2328 to a functional status.
"The NRC Resident Inspector has been notified." |
Power Reactor | Event Number: 53424 | Facility: PALO VERDE Region: 4 State: AZ Unit: [] [2] [] RX Type: [1] CE,[2] CE,[3] CE NRC Notified By: DAVID HECKMAN HQ OPS Officer: HOWIE CROUCH | Notification Date: 05/23/2018 Notification Time: 17:37 [ET] Event Date: 05/23/2018 Event Time: 11:28 [MST] Last Update Date: 05/23/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL | Person (Organization): JASON KOZAL (R4DO) | Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | A/R | Y | 100 | Power Operation | 0 | Hot Standby | Event Text AUTOMATIC REACTOR TRIP ON LOW DEPARTURE FROM NUCLEATE BOILING RATIO
"The following event description is based on information currently available. If through subsequent reviews of this event additional information is identified that is pertinent to this event or alters the information being provided at this time a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73.
"On May 23, 2018, at approximately 1128 Mountain Standard Time (MST), the Palo Verde Nuclear Generating Station (PVNGS) Unit 2 control room received reactor protection system alarms for low departure from nucleate boiling ratio and an automatic reactor trip occurred. Prior to the reactor trip, Unit 2 was operating normally at 100 percent power. Plant operators entered the reactor trip procedures and diagnosed an uncomplicated reactor trip. All CEAs [control element assemblies] fully inserted into the core. No emergency classification was required per the PVNGS Emergency Plan.
"The Unit 2 safety-related electrical buses remained energized from normal offsite power during the event. There was no impact to the required circuits between the offsite transmission network and the onsite Class 1E Electrical Power Distribution System; the offsite power grid is stable.
"No major equipment was inoperable prior to the event that contributed to the event or complicated operator response. Unit 2 is currently stable in Mode 3 with the reactor coolant system at normal operating temperature and pressure. The cause of the reactor trip is under investigation.
"The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The event did not adversely affect the safe operation of the plant or the health and safety of the public. "The NRC Resident Inspector has been informed of the Unit 2 reactor trip."
Decay is being removed via steam dumps to condenser. Units 1 and 3 at Palo Verde were unaffected by the transient and continue to operate at 100 percent power. |
Power Reactor | Event Number: 53426 | Facility: CALLAWAY Region: 4 State: MO Unit: [1] [] [] RX Type: [1] W-4-LP NRC Notified By: JEREMY CZESCHIN HQ OPS Officer: THOMAS KENDZIA | Notification Date: 05/23/2018 Notification Time: 18:32 [ET] Event Date: 05/23/2018 Event Time: 07:30 [CDT] Last Update Date: 05/23/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 26.719 - FITNESS FOR DUTY | Person (Organization): JASON KOZAL (R4DO) FFD GROUP (EMAIL) | Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text FITNESS FOR DUTY
"On May 23, 2018 Callaway determined that a violation of one provision of the site's Fitness for Duty (FFD) policy occurred. FFD pre-access testing confirmed a test failure for alcohol. The violation was committed by a non-licensed supervisory employee. The individual did not hold unescorted access to the plant but did perform behavioral observation program (BOP) duties. The BOP qualification has been removed.
"The NRC Resident Inspector has been notified by the licensee." | |