U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/27/2009 - 11/30/2009 ** EVENT NUMBERS ** | General Information or Other | Event Number: 45519 | Rep Org: NE DIV OF RADIOACTIVE MATERIALS Licensee: BECTON DICKINSON INFUSION THERAPY SYSTEM INC. Region: 4 City: BROKEN BOW State: NE County: License #: 04-01-01 Agreement: Y Docket: NRC Notified By: BRYAN MILLER HQ OPS Officer: DONALD NORWOOD | Notification Date: 11/24/2009 Notification Time: 15:14 [ET] Event Date: 11/23/2009 Event Time: 18:45 [CST] Last Update Date: 11/24/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): NEIL OKEEFE (R4DO) JIM LUEHMAN (FSME) | Event Text AGREEMENT STATE REPORT - FAILURE OF SOURCE UP INDICATOR SWITCH The following report was received via E-mail: "At or around 6:45 PM on November 23, 2009 the irradiator at Becton Dickinson in Broken Bow, NE experienced a box jam. The master timer timed out and sent the source into the pool as normal. The source movement bell continued to ring beyond the normal time. The operator on duty entered the control room and noted that the fault indicator lights for source switch, source pass time out were activated. Both source up and source down indicator lights were on. The operator went to the source cylinder room on the roof and verified that physically the cylinder had traveled to the full down position. The source cable was determined to be tight as normal. The area was also surveyed for any radiation above background. None was noted. "The operator then called the RSO and informed him of the situation. The RSO came to the plant. Since the source up indicator was activated, the area monitor was disabled. The cell door was manually opened and the air to the source cylinder disabled. Two operators along with the RSO slowly entered the cell with two survey meters. No radiation above background was detected. "It was determined that the source up switch plunger had become stuck in the closed position. This plunger was removed, cleaned and lubricated. No other machine issues were noted and normal operation ensued. "Reporting Requirement: 30.509(b)(2) - events involving failure or disability to function when equipment is required to be available and operable and no redundant equipment is available and operable, includes source disconnection and failure to retract source." Nebraska Item Number: NE090017 | Power Reactor | Event Number: 45522 | Facility: TURKEY POINT Region: 2 State: FL Unit: [ ] [4] [ ] RX Type: [3] W-3-LP,[4] W-3-LP NRC Notified By: ROGER MONTGOMERY HQ OPS Officer: JOHN KNOKE | Notification Date: 11/27/2009 Notification Time: 05:00 [ET] Event Date: 11/26/2009 Event Time: 23:40 [EST] Last Update Date: 11/27/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): MARVIN SYKES (R2DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 4 | N | N | 0 | Hot Standby | 0 | Hot Standby | Event Text TWO SHUTDOWN BANK RODS WERE DROPPED FROM FULLY WITHDRAWN POSITION "With Unit 4 borated to a cold shutdown condition following the Unit 4 Cycle 25 refueling outage, post-modification acceptance testing was being performed on the Rod Position Indication System prior to reactor startup. While performing this test, two shutdown bank rods showed indication of being fully inserted from a fully withdrawn position. Off-normal procedures were entered and the Reactor Protection System (RPS) was subsequently manually actuated. All remaining rods were fully inserted in accordance with plant procedures. Investigations are in progress to determine and repair the cause of the dropped rods." The licensee has notified the NRC Resident Inspector. | Other Nuclear Material | Event Number: 45524 | Rep Org: KAKIVIK ASSET MANAGEMENT Licensee: KAKIVIK ASSET MANAGEMENT Region: 4 City: ANCHORAGE State: AK County: License #: 50-27667-01 Agreement: N Docket: NRC Notified By: KEENAN REMELE HQ OPS Officer: DONG HWA PARK | Notification Date: 11/27/2009 Notification Time: 15:36 [ET] Event Date: 11/27/2009 Event Time: 08:00 [YST] Last Update Date: 11/27/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: 30.50(b)(2) - SAFETY EQUIPMENT FAILURE | Person (Organization): NEIL OKEEFE (R4DO) JIM LUEHMAN (FSME) | Event Text FAILURE TO FULLY RETRACT THE SOURCE OF A RADIOGRAPHY CAMERA Technicians were performing radiography when the source in an Industrial Nuclear Corporation (INC) IR-100 radiography camera was unable to be fully retracted. This was caused by a frozen lock on the device which occurred due to freezing weather conditions. A certified technician serviced the lock. The lock was returned to a fully functional condition, and the source was returned to the safe and secure position. No personnel over exposure occurred. The licensee could not provide the serial number of the camera at the time of the report due to the remote location where the radiography was taking place. Similar events: EN #45384, 45469, 45496 | Power Reactor | Event Number: 45525 | Facility: DRESDEN Region: 3 State: IL Unit: [ ] [ ] [3] RX Type: [1] GE-1,[2] GE-3,[3] GE-3 NRC Notified By: BRUCE FARNZEN HQ OPS Officer: CHARLES TEAL | Notification Date: 11/28/2009 Notification Time: 03:15 [ET] Event Date: 11/27/2009 Event Time: 22:05 [CST] Last Update Date: 11/28/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(v)(D) - ACCIDENT MITIGATION | Person (Organization): HIRONORI PETERSON (R3DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 3 | N | Y | 98 | Power Operation | 98 | Power Operation | Event Text TURBINE VALVE TRIPS DID NOT MEET TECH SPECS "At 2205 on Nov 27, 2009, at the Dresden Nuclear Power Station (DNPS) it was determined that Technical Specification RPS functions 8 and 9, 'Turbine Stop Valve - Closure' and 'Turbine Control Valve Fast Closure, Trip Oil Pressure - Low' are susceptible to single point vulnerability due to a nonconformance to a design standard (IEEE- 279 1968). Based on this single point vulnerability, these RPS functions could potentially have prevented the fulfillment of their respective safety function and therefore this event is reportable per 10 CFR 50.72(b)(3)(v)(D), 'an event or condition that could have prevented the fulfillment of a safety function-mitigate the consequences of an accident.' The station has performed an operability determination, and the safety function remains operable. Actions to restore compliance to referenced design standard are in progress." The licensee has informed the NRC Resident Inspector. | Power Reactor | Event Number: 45526 | Facility: WATERFORD Region: 4 State: LA Unit: [3] [ ] [ ] RX Type: [3] CE NRC Notified By: JOHN JARRELL HQ OPS Officer: JOHN KNOKE | Notification Date: 11/29/2009 Notification Time: 05:08 [ET] Event Date: 11/28/2009 Event Time: 23:44 [CST] Last Update Date: 11/29/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(ii)(A) - DEGRADED CONDITION | Person (Organization): NEIL OKEEFE (R4DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 3 | N | N | 0 | Cold Shutdown | 0 | Cold Shutdown | Event Text CONTAINMENT MINIMUM PATHWAY LEAK RATE WAS EXCEEDED "10CFR50 Appendix J Local Leak Rate Testing determined the total 'as-found' containment minimum pathway leak rate exceeded the maximum allowable containment leak rate per the Containment Leakage Rate Testing Program. This was primarily due to three penetrations that could not be pressurized to full test pressure. The maximum allowable leakage was assigned to both valves in each penetration since the valves can not be tested individually. "This condition is reportable as a condition of the nuclear power plant, including its principal safety barriers, being seriously degraded per 10CFR50.72(b)(3)(ii)(A). The condition was discovered with the plant in Mode 5. Corrective actions have already been completed and all penetrations, as well as total containment leakage, is well within limits established by the Containment Leakage Rate Testing Program." The licensee has notified the NRC Resident Inspector. | Fuel Cycle Facility | Event Number: 45527 | Facility: PADUCAH GASEOUS DIFFUSION PLANT RX Type: URANIUM ENRICHMENT FACILITY Comments: 2 DEMOCRACY CENTER 6903 ROCKLEDGE DRIVE BETHESDA, MD 20817 (301)564-3200 Region: 2 City: PADUCAH State: KY County: McCRACKEN License #: GDP-1 Agreement: Y Docket: 0707001 NRC Notified By: CALVIN PITTMAN HQ OPS Officer: DONG HWA PARK | Notification Date: 11/29/2009 Notification Time: 13:01 [ET] Event Date: 11/28/2009 Event Time: 18:50 [CST] Last Update Date: 11/29/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: 76.120(c)(2) - SAFETY EQUIPMENT FAILURE | Person (Organization): MARVIN SYKES (R2DO) EARL EASTON (NMSS) | Event Text SAFETY EQUIPMENT DISABLED DUE TO A GROUND IN THE AREA CONTROL ROOM ALARM "At 1850 CST, on 11/28/09 the Plant Shift Superintendent (PSS) was notified that the C-333 Unit 6 Cell 5 UF6 Release Detection (PGLD) System was inoperable due to loss of power to the Area Control Room (ACR) alarm for this system. The purpose of the PGLD System is to detect a UF6 release and alert operators in the ACR by sounding an alarm. At the time this was discovered, G-333 Unit 6 Cell 5 was operating above atmospheric pressure. TSR 2.4.4.1 requires that at least the minimum number of detector heads in the cell are operable during steady state operations above atmospheric pressure. With the Unit 6 Cell 5 PGLD system inoperable, none of the required heads were operable. This PGLD System was declared inoperable, TSR LCO 2.4.4.1.B.1 was entered and a continuous smoke watch was put in place within one hour. "Troubleshooting was initiated, a ground was discovered on the alarm circuit, the ground was isolated, and the system was tested and declared operable at 2305 [CST]. This event is reportable as a 24 hour event in accordance with 10CFR76.120(c)(2)(i). This is an event in which equipment is disabled or fails to function as designed when: a) the equipment is required by a TSR to prevent releases, prevent exposures to radiation and radioactive materials exceeding specified limits, mitigate the consequences of an accident, or restore this facility to a pre-established safe condition after an accident; b) the equipment is required by a TSR to be available and operable and either should have been operating or should have operated on demand, and c) no redundant equipment is available and operable to perform the required safety function. "The NRC Resident Inspector has been notified of this event." | Power Reactor | Event Number: 45528 | Facility: SURRY Region: 2 State: VA Unit: [ ] [2] [ ] RX Type: [1] W-3-LP,[2] W-3-LP NRC Notified By: GEOFFREY HILL HQ OPS Officer: PETE SNYDER | Notification Date: 11/29/2009 Notification Time: 13:31 [ET] Event Date: 11/29/2009 Event Time: 10:45 [EST] Last Update Date: 11/29/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL | Person (Organization): MARVIN SYKES (R2DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | M/R | Y | 0 | Startup | 0 | Hot Standby | Event Text TRIP FROM INTERMEDIATE RANGE DUE TO ROD GROUP DEMAND COUNTER DISCREPANCY "During startup physics testing, the reactor operator identified a discrepancy between Group 1 & Group 2 Step Demand Counters for control bank 'B'. Research identified the issue to be associated with failure of a card in the rod control power cabinet. Failure of the card impacts group step counters for control bank 'B', control bank 'D' and shutdown bank 'B.' "Inoperability of more than one group step counter per bank placed Unit 2 in a 6-hour clock to hot shutdown as of 0808 hrs 29 November 2009. Consequently, at 1045 hrs, the decision was made to trip Unit 2 reactor. The decision was based on time required to make repairs, complete post maintenance testing requirements, and maintaining proper control of reactivity. "All systems functioned as required on the trip and initiation of any auxiliary or emergency systems was not required. Current heat removal is via normal plant alignment following refueling outage activities: steam generator blowdown, main feedwater, and steam generator PORV." All control rods fully inserted on the manual trip. The licensee notified the NRC Resident Inspector. | |