U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/02/2009 - 04/03/2009 ** EVENT NUMBERS ** | General Information or Other | Event Number: 44946 | Rep Org: NC DIV OF RADIATION PROTECTION Licensee: FLETCHER HOSPITAL Region: 1 City: FLETCHER State: NC County: License #: 045-0370-1 Agreement: Y Docket: NRC Notified By: CLIFF HARRIS HQ OPS Officer: JOE O'HARA | Notification Date: 03/31/2009 Notification Time: 14:41 [ET] Event Date: 03/31/2009 Event Time: 08:30 [EDT] Last Update Date: 03/31/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): MEL GRAY (R1) ANGELA MCINTOSH (FSME) | Event Text AGREEMENT STATE REPORT - CONTAMINATION FOUND ON NUCLEAR MEDICINE PACKAGING The following was received from the state via e-mail: "N.C. Radiation Protection Section was notified on March 31, 2009 by the hospital about a nuclear medicine package received from a nuclear pharmacy in excess of the loose contamination limits. "The swipes performed on the package read 2890 dpm vs the limit of 2200 dpm. The package was placed in hot storage and will be stored for decay. "Licensee notified the carrier and the pharmacy." NC Event Report ID Number is NC-09-20. | Power Reactor | Event Number: 44957 | Facility: MONTICELLO Region: 3 State: MN Unit: [1] [ ] [ ] RX Type: [1] GE-3 NRC Notified By: RANDY SAND HQ OPS Officer: VINCE KLCO | Notification Date: 04/02/2009 Notification Time: 13:30 [ET] Event Date: 04/02/2009 Event Time: 05:43 [CDT] Last Update Date: 04/02/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(v)(B) - POT RHR INOP | Person (Organization): STEVE ORTH (R3) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | N | 0 | Refueling | 0 | Refueling | Event Text RESIDUAL HEAT REMOVAL INOPERABLE "At 0543 [CDT] on April 2, 2009 at the Monticello Nuclear Generating Plant (MNGP) an Operator made the following discovery during performance of his rounds. The flowrate and pressure of the #14 Residual Heat Removal Service Water (RHRSW) pump motor cooling appeared to be low. Investigation found the flow to be approximately 1 gpm. The cooling water supply flow to the pump motor cooler comes from either RHRSW or Service Water. Based on these indications, Operators declared the RHR Shutdown Cooling inoperable and entered actions for Technical Specifications 3.9.7. Actions have been completed to provide an alternate water supply to the RHRSW pump motor oil cooler. Based on the inoperability of the RHR Shutdown Cooling, this event is reportable under 10 CFR 50.72(b)(3)(v), 'An Event or Condition that could have Prevented the Fulfillment of a Safety Function-Capability to Remove Residual Heat.' The station is performing further investigation into the event and will develop corrective actions based on the results of the investigation." The Licensee notified the NRC Resident Inspector. | Power Reactor | Event Number: 44965 | Facility: DUANE ARNOLD Region: 3 State: IA Unit: [1] [ ] [ ] RX Type: [1] GE-4 NRC Notified By: ELLIS VANN HQ OPS Officer: HOWIE CROUCH | Notification Date: 04/03/2009 Notification Time: 03:27 [ET] Event Date: 04/03/2009 Event Time: 00:28 [CDT] Last Update Date: 04/03/2009 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): STEVE ORTH (R3) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | M/R | Y | 100 | Power Operation | 0 | Hot Shutdown | Event Text MANUAL REACTOR SCRAM DUE TO INCREASING REACTOR WATER LEVEL DURING CALIBRATION "This report is being made under [10 CFR] 50.72(b)(2)(iv)(B) for inserting a manual reactor scram due to indicated reactor water level of 205 inches and rising. The exact cause of the reactor water level increase is not known at this time. However, STP [Surveillance Test Procedure] 3.3.3.2-09, 'Reactor Water Level and Pressure Instruments Calibration' was in progress at the time and is likely the cause of the level transient. "In addition, this report is being made under [10 CFR] 50.72(b)(3)(iv)(A) due to PCIS [Primary Containment Isolation System] groups 2, 3 and 4 being received when reactor water level dropped below 170 inches following the reactor scram. All isolations went to completion. This level response is considered normal following a reactor scram from power and reactor water level is currently being controlled in the normal band. All PCIS group isolations were reset." All rods fully inserted during the scram. The plant is in a normal shutdown electrical lineup with offsite sources powering the safety busses. No safety or relief valves lifted during the transient. Decay heat is being removed via the steam bypass to condenser valves. The licensee has notified the NRC Resident Inspector. | |