U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/26/2010 - 11/29/2010 ** EVENT NUMBERS ** | Fuel Cycle Facility | Event Number: 46427 | Facility: PORTSMOUTH LEAD CASCADE RX Type: URANIUM ENRICHMENT FACILITY Comments: 2 DEMOCRACY CENTER 6903 ROCKLEDGE DRIVE BETHESDA, MD 20817 Region: 2 City: PIKETON State: OH County: PIKE License #: SNM-7003 Agreement: Y Docket: 70-7003 NRC Notified By: JIM MCCLEERY HQ OPS Officer: JOE O'HARA | Notification Date: 11/18/2010 Notification Time: 16:40 [ET] Event Date: 11/18/2010 Event Time: 13:41 [EST] Last Update Date: 11/29/2010 | Emergency Class: NON EMERGENCY 10 CFR Section: PART 70 APP A (c) - OFFSITE NOTIFICATION/NEWS REL | Person (Organization): ALAN BLAMEY (R2DO) TIM MCCARTIN (NMSS) JEFFERY GRANT (IRD) | Event Text OFFSITE NOTIFICATION TO OSHA DUE TO ONSITE FATALITY The American Centrifuge Plant reported an employee collapsed in the Centrifuge Test and Training Facility, was transported offsite to a medical facility, and subsequently died. Initial reports indicate that the employee died of natural causes. The licensee notified Region 2 (D. Hartland) of the event. * * * UPDATE FROM CRABTREE TO KLCO ON 11/19/2010 AT 1054 EST * * * On 11/18/2010, at 1551 EST, the licensee commenced notification of OSHA and completed notification at 1602 EST on the same day. Notified R2DO (Rich), NMSS-E(McCartin) and IRD (Grant). * * * UPDATE AT 1555 EST ON 11/29/10 FROM THOMAS MARTIN TO ERIC SIMPSON * * * The licensee called with administrative corrections (facility, docket and license numbers) to the original event notification. Notified R2DO (Schaffer), NMSS-E(Benner) and IRD (Grant). | Power Reactor | Event Number: 46436 | Facility: FERMI Region: 3 State: MI Unit: [2] [ ] [ ] RX Type: [2] GE-4 NRC Notified By: JIM KONRAD HQ OPS Officer: DONALD NORWOOD | Notification Date: 11/24/2010 Notification Time: 16:00 [ET] Event Date: 11/24/2010 Event Time: 15:15 [EST] Last Update Date: 11/26/2010 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE | Person (Organization): BILLY DICKSON (R3DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | N | N | 0 | Cold Shutdown | 0 | Cold Shutdown | Event Text SAFETY PARAMETER DISPLAY SYSTEM AND EMERGENCY RESPONSE DATA SYSTEM OUT OF SERVICE FOR PLANNED MAINTENANCE "On 11/24/10 at 1515 EST, the Safety Parameter Display System (SPDS) and Emergency Response Data System (ERDS) were removed from service to support activities for a planned maintenance outage on the UPS vital bus power supply. The duration of work is expected to be approximately 48 hours. During this time, the majority of the Control Room indications remain available to the plant staff, and will be used for emergency response, if needed. Information will be communicated to the NRC using other available communication systems, if needed. The plant is currently in Mode 4, and will remain in Mode 4, for the duration of the SPDS and ERDS unavailability. Since the unavailability will last greater than 8 hours, this is considered a Loss of Emergency Assessment Capability, and reportable under 10CFR50.72(b)(3)(xiii). "Followup notification will be made when SPDS and ERDS have been restored." The licensee notified the NRC Resident Inspector. * * * UPDATE AT 1850 EST ON 11/26/10 FROM JIM KONRAD TO S. SANDIN * * * "Update to Event #46436: On 11/26/10 at 1733 EST, regarding Safety Parameter Display System (SPDS) and Emergency Response Data System (ERDS) systems removed from service to support planned maintenance on the UPS vital bus power supply. "Planned work which resulted in the loss of SPDS and ERDS is complete. All Emergency Assessment Capabilities have been restored." The licensee informed the NRC Resident Inspector. Notified R3DO (Dickson). | Power Reactor | Event Number: 46440 | Facility: DRESDEN Region: 3 State: IL Unit: [ ] [ ] [3] RX Type: [1] GE-1,[2] GE-3,[3] GE-3 NRC Notified By: DAN MILLER HQ OPS Officer: HOWIE CROUCH | Notification Date: 11/26/2010 Notification Time: 23:36 [ET] Event Date: 11/26/2010 Event Time: 17:34 [CST] Last Update Date: 11/26/2010 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(v)(D) - ACCIDENT MITIGATION | Person (Organization): BILLY DICKSON (R3DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 3 | N | Y | 20 | Power Operation | 20 | Power Operation | Event Text HIGH PRESSURE COOLANT INJECTION DECLARED INOPERABLE DUE TO A STEAM LEAK "While performing the High Pressure Coolant Injection (HPCI) high pressure run required by SR 3.5.1.6 following Unit 3 refueling outage D3R21, a steam leak developed from the HPCI turbine. The steam leak resulted in a HPCI room high temperature alarm and the HPCI turbine was manually tripped. The U3 HPCI system was declared inoperable and Tech Spec LCO 3.5.1 condition G.1 and G.2 were entered. "The condition is being reported in accordance with 10 CFR 50.72 (b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of the safety function of a system that is needed to mitigate the consequences of an accident. "Maintenance activities are currently in progress to restore system to operable status." The failure resulted in the licensee entering a 14-day LCO action statement for restoration. The licensee has notified the NRC Resident Inspector. | Power Reactor | Event Number: 46441 | Facility: MILLSTONE Region: 1 State: CT Unit: [ ] [2] [ ] RX Type: [1] GE-3,[2] CE,[3] W-4-LP NRC Notified By: RICHARD VIGNEAU HQ OPS Officer: HOWIE CROUCH | Notification Date: 11/28/2010 Notification Time: 17:27 [ET] Event Date: 11/28/2010 Event Time: 15:15 [EST] Last Update Date: 11/28/2010 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): DON JACKSON (R1DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | A/R | Y | 100 | Power Operation | 0 | Hot Standby | Event Text AUTOMATIC REACTOR TRIP AFTER TURBINE TRIP DUE TO LOSS OF CONDENSER VACUUM "Loss of two circulating water pumps in one condenser caused a high main condenser backpressure. The high main condenser back pressure caused an automatic main turbine and reactor trip while critical >15%. "Low steam generator water level following the trip caused an automatic Auxiliary Feedwater actuation. The low water level condition has cleared. Normal post-trip response has been verified and the plant is stable." The licensee removed one circulating water pump from service in preparation of performing scheduled maintenance when the other circulator unexpectedly tripped. The cause of the pump trip is under investigation. During the trip, all rods inserted into the core. There were no primary safety valves that lifted during the transient but main steam safeties "chattered" during the transient and have fully reseated. There is no known primary to secondary leakage. The electrical grid is stable and supplying plant loads in a normal shutdown electrical lineup. The reactor is stable at normal operating pressure and temperature with decay heat being removed via the steam dumps to condenser. The licensee has notified the State of Connecticut Department of Environmental Protection, the town of Waterford, CT, and the NRC Resident Inspector. | Power Reactor | Event Number: 46442 | Facility: VOGTLE Region: 2 State: GA Unit: [ ] [2] [ ] RX Type: [1] W-4-LP,[2] W-4-LP NRC Notified By: AL SWEAT HQ OPS Officer: PETE SNYDER | Notification Date: 11/29/2010 Notification Time: 19:20 [ET] Event Date: 11/29/2010 Event Time: 16:12 [EST] Last Update Date: 11/29/2010 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE | Person (Organization): SCOTT SHAEFFER (R2DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | N | Y | 98 | Power Operation | 98 | Power Operation | Event Text PLANT COMPUTER MAINTENANCE OUTAGE "At 1612 today, November 29, 2010 Unit 2 Integrated Plant Computer (IPC) was shutdown for upgrade work. This includes the SPDS [Safety Parameter Display] system which is a function of the IPC. The IPC will be returned to service in approximately two weeks and SPDS function will be restored at that time. In addition, the ERDS [Emergency Response Data System] is out of service and will be restored in the same time frame. "Per the 50.54.Q that was prepared by our Emergency Preparedness group, notification has been made to the NRC ERDS group (Roger Chow) of the unavailability of the ERDS. While the IPC is out of service, control board indications are being utilized by the control room crew. In addition, the safety-related Plant Safety Monitoring System (PSMS) is operable. Restoration of SPDS and ERDS functions have been given the highest priority during restoration of the system. Both the NRC Ops Center and the NRC ERDS group will be notified when SPDS and ERDS capability have been restored." The licensee notified the NRC Resident Inspector. | |